ML16127A317

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Notice of Violation from Insp on 890213-17.Deviation Noted: Dedicated Control Board Displays for Instruments Not Specifically Identified & Trend Info for Four Variables Not Available on Dedicated Recorders Nor Stored in Computer
ML16127A317
Person / Time
Site: Oconee  
Issue date: 03/16/1989
From: Julian C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16127A316 List:
References
RTR-REGGD-01.097, RTR-REGGD-1.097 50-269-89-07, 50-269-89-7, 50-270-89-07, 50-270-89-7, 50-287-89-07, 50-287-89-7, NUDOCS 8904030471
Download: ML16127A317 (2)


Text

ENCLOSURE 1 NOTICE OF DEVIATION Duke Power Company Docket Nos. 50-269, 50-270, 50-287 Oconee License Nos. DPR-38, DPR-47, DPR-55 The following deviation was identified during a Nuclear Regulatory Commission (NRC) inspection conducted on February 13-17, 1989.

In Duke Power Company document, "Regulatory Guide 1.97, Revision 2 - Review for Oconee Nuclear Station," transmitted September 28, 1984, they committed to comply with Regulatory Guide 1.97, "Instrumentation for Light-Water-Cooled Nuclear Power Plants to Assess Plant Environs Conditions during and following an accident", unless specific exceptions were described.

Page 5-7 of the Oconee review document states, "dedicated control board displays for the instruments designated as Types A, B and C, Category 1 or 2 and qualified for use throughout all phases of an accident will be specifically identified on the control panels so that the operator can discern that they are available for use under accident conditions."

Page 5-6 of the Oconee review document states, "recording of instrumentation readout information is provided for at least one of the redundant channels."

It also states, "the trend or transient information will be available on dedicated recorders or stored in computer memory for display on demand."

Page 5-8 of. the Oconee review document states, "servicing, testing, and calibration programs are specified to maintain the capability of the monitoring instrumentation."

These statements and commitments are consistent with the requirements of Regulatory Guide 1.97.

Contrary to the above:

(a) Dedicated control board displays for the instruments designated as Types A, B, and C, Category 1 or 2 were not specifically identified:

8904030471 890316 PDR ADOCK 05000269 PNU

Duke Power Company 2

Docket Nos. 50-269, 50-270, 50-287 Oconee License Nos. DPR-38, DPR-47, DPR-55 (b) Trend information for the following four variables was not available on dedicated recorders nor stored in computer memory for display on demand:

1.

RCS hot leg water temperature

2. Auxiliary feedwater flow
3. Steam generator level
4. Degrees of subcooling (c) The inverter output voltmeters [defined as Type D, Category 2 in the RG] were not included in the-calibration program, and had not been calibrated since the original construction of the units according to records.

The Deviation applies to Units 1, 2 and 3.

Please provide to the U.S. Nuclear Regulatory Commission, ATTN:

Document Control Desk, Washington, DC 20555, with a copy to. the Regional Administrator, Region II, and a copy to the NRC Resident Inspector, Oconee, in writing within 30 days of the date of this Notice, the reasons for the deviation, the corrective steps which have been taken and the results achieved, the corrective steps which will be taken to avoid further deviations, and the date when your corrective action will be completed.

Where good -cause is shown, consideration will be given to extending the response time.

FOR THE NUCLEAR REGULATORY COMMISSION Caudle A. Julian, Chief Engineering Branch Division of Reactor Safety Dated at Atlanta, Georgia this

<i 4 day of March 1989