ML15261A108

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Discusses 950620 Meeting W/Representatives from Oconee Engineering Dept in Atlanta Re Overview of Engineering Activities at Site.W/List of Attendees & Handout
ML15261A108
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/28/1995
From: Casto C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To: Hampton J
DUKE POWER CO.
References
NUDOCS 9507120028
Download: ML15261A108 (28)


Text

June 28, 1995 Duke Power Company ATTN: Mr. J. W. Hampton Vice President Oconee Site P. 0. Box 1439 Seneca, SC 29679

SUBJECT:

MEETING

SUMMARY

- OCONEE NUCLEAR STATION - JUNE 20, 1995 Gentlemen:

On June 20, 1995, representatives from the Oconee Engineering Department met with members of the Region II staff in Atlanta. Mr. Davis led the discussion for Duke Power. Mr. Davis provided the staff with an overview of.engineering activities at the site.

Enclosed is a copy of the handout provided during this meeting. Also enclosed is a list of attendees at the meeting.

Mr. Gibson expressed the staff's appreciation for this update. The meeting was beneficial in providing the staff with your management perspective of ongoing engineering activities.

Sincerely, Original signed by Jerome J. Blake for Charles A. Casto Charles A. Casto, Chief Engineering Branch Division of Reactor Safety Docket Nos. 50-269, 50-270, 50-287 License Nos. DPR-38, DPR-47, DPR-55

Enclosures:

As stated (2) cc w/encls:

(See page 2) 9507120028 950628 PDR ADOCK 05000269 P

PDR

DPC 2

cc w/encls:

County Supervisor of Mr. J. E. Burchfield Oconee County Compliance-Walhalla, SC 29621 Duke Power Company P. 0. Box 1439 Manager, LIS Seneca, SC 29679 NUS Corporation 2650 McCormick Drive Mr. A. V. Carr, Esq.

Clearwater, FL 34619-1035 Duke Power Company 422 South Church Street Mr. G. A. Copp Charlotte, NC 28242-0001 Licensing - EC050 Duke Power Company Mr. Robert P. Gruber P. 0. Box 1006 Executive Director Charlotte, NC 28201-1006 Public Staff - NCUC C

P. 0. Box 29520 Ms. Karen E. Long Raleigh, NC 27626-0520 Assistant Attorney General N. C. Department of Justice Mr. Robert B. Borsum P. 0. Box 629 Babcock and Wilcox Company

Raleigh, NC 27602 Nuclear Power Generation Division 1700 Rockville Pike, Suite 525 Distribution w/encls:

Rockville, MD 20852 L. A. Wiens, NRR R. Carroll, RH Mr. J. Michael McGarry, III, Esq.

R. V. Crlenjak, RH Winston and Strawn G. A. Hallstrom, RH 1400 L Street, NW PUBLIC Washington, D. C. 20005 NRC Resident Inspector Office of Intergovernmental U.S. Nuclear Regulatory Commission Relations Route 2, Box 610 116 West Jones Street Seneca, SC 29672 Raleigh, NC 27603 Mr. Max Batavia, Chief Bureau of Radiological Health South Carolina Department of Health and Environmental Control 2600 Bull Street Columbia, SC 29201 SEND TO PUBLIC DOCUMENT ROOM?

YES NO OFFICE I:DRP SIGNATURE NAME RCrlenjak DATE 06/

/95 06/

/95 06

/95 06/ /95 06/ /95 COPY?

ES NO YES NO YES NO YES NO YES NO YES NO OFFICIAL REC COPY DOCUMENT NAME:

s:\\drs\\eb\\ocomtg.sum r

DUKE POWER COMPANY OCONEE ENGINEERING UPDATE JUNE 20, 1995

Duke Power Company Oconee Nuclear Site Engineering Division Agenda

  • Plant Status
  • Engineering Interfaces
  • SelfAssessment
  • Work Processes
  • Design Basis
  • Major System/Equipment Issues
  • Open Discussion/Feedback 2

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  • U1 & U2 at 100%, U3 in EOC15 RFO (35 Days)
  • One Unit Trip (U2) in last 6 months, Two in last 10 months
  • INPO Indicators a INPO 1 Rating for 6th consecutive time

> HPI unavailability, YTD upper quartile o EFW unavailability, YTD upper quartile

> EAC unavailability, YTD just below upper quartile

> Failed fuel, U1 and U2 zero, U3 zero on restart

  • 1995 YTD Capacity Factor, Ul 92%, U2 85%, U3 101%

> U1 CRDM Thermal Barrier Replacement (12 Days)

> U2 Expansion Joints/CRDM (19 days) 4

Engineering Interfaces

  • Plan-of-the-Day (POD) Meetings
  • Nuclear Excellence Quality Steering Team (NEQST) Meetings
  • Outage Meetings
  • Regulatory Review Meetings
  • Plant Operational Review Committee (PORC)
  • Nuclear Safety Review Board (NSRB)
  • Business Excellence Steering Teams (BEST) 5 Self Assessment Process

===.

Background===

a Utilized INPO Criteria n Performed with Duke Personnel

>> October 10, 1994-October 20, 1994

  • Progress to Date

> Correlated the findings with ongoing initiatives

- Group Manager assigned for each initiative

-Total Findings 46

- Findings Closed to-date - 12

- Findings to be Completed in 1995 - 14

- In progress - 20 3

Self Assessment Process

  • Continuing Initiatives

> Self Assessment to be Performed in 1995

> Plan to use outside assistance 7

Work Processes

  • Planning and Work Management Process
  • Backlog Management
  • Operations and Maintenance Support
  • Calculation Process
  • Training and Qualification Process 8

Planning and Work Management Process

Background

a Limited integration of Work Management (WM) processes

> WM identified as an area for improvement 9

Planning and Work Management Process

  • Progress to Date

> WM application in place - PLAN

> Engineering has been trained on the application a Currently entering work activities 10 5

Planning and Work Management Process

  • Continuing Initiatives

> Development of a resource loading application

> Development of a long range operational plan for engineering li Backlog Management

  • Background a Backlog of Work Orders (WO) on-hold for Engineering a 13,000 documents out-of-date

> Large backlog of overdue Problem Investigation Process (PIP) actions

  • Progress to Date

> Clear ownership and expectations for WO's on-hold

> Eliminated document backlog (cost: 20 person - years)

> Accurate as-built drawings available

> Overdue PIP Actions at zero Increased awareness of problems that backlogs create 12

Backlog Management

  • Continuing Initiatives a Reducing numbers of WO's on-hold for Engineering a Vital-to-Operations (VTO) Drawings updated before systems are returned to service a Updating documents within 60 days of outage a Maintain overdue PIP's at zero a Holding managers/supervisors accountable for backlogs a Measuring and trending program 13 Operations and Maintenance Support
  • Background a Lacked focus on operator workarounds

>> Reliability of some equipment not adequately addressed a Engineering Support Program (ESP) for Systems/Equipment not clearly defined

  • Progress to Date

> Operator workaround list formalized a Weekly management focus on workarounds

> Site focus on top equipment reliability issues

> Maintenance Procedure Upgrade on Emergency Power Project (EPP)

> ESP clearly defined in directive 14

Operations and Maintenance Support

  • Continuing Initiatives a Management focus on minimizing operator workarounds

) PM Optimization o Implementation of ESP for Maintenance Rule Systems/Equipment 15 Calculation Process

  • Background

> Audits & inspections (e.g., SWSOPI) identified concerns with accuracy, thoroughness of calculations

> Similar concerns identified at all 3 Duke nuclear sites

  • Progress to Date

> Placed greater emphasis on timely update of calculations affected by modifications -now done within 60 days of field completion

>> Revised directive to clarify expectations and responsibilities

> Communicated expectations 16

Calculation Process

  • Continuing Initiatives a Developing calculation database that allows searching, sorting & cross-referencing a Training on Instrument Setpoint/Uncertainty Calculations directive planned a Enhanced work management process will allow more effective resource allocation

> Human performance improvement training for supervisors/engineers doing analytical work 17 Training & Qualification Process

  • Background a 1994 Engineering Reorganization a Job Functions Redefined

> Position Specific Guides (PSGs) Developed a Program Based on INPO's "Guidelines for Training and Qualification of Engineering Support Personnel" 18

Training and Qualification Process

  • Progress to Date o Program Re-Accredited by INPO Fall '94

> Incumbents assessed to PSG's, needs identified

> Individual Training Plans Developed a Engineering Training and Job Enrichment Team Developed

> Incumbents not on special assignment have completed the Initial Training Program

> Engineering Continuing Training Program 19 Training and Qualification Process

  • Continuing Initiatives o PSG's are Living Documents

) Needs Assessment On-Going

> Teammates Actively Involved 20 10

Design Basis Issues

  • Emergency Power Project
  • Design Basis Documentation
  • Oconee Safety Related Designation Clarification (OSRDC)
  • Testing 21 Emergency Power Project
  • Background a Many open issues and commitments

>> Progress toward completing work not satisfactory

> Some commitments missed, dates extended a Project team formed in October 1994 with dedicated Project Manager 22

Emergency Power Project

  • Progress to Date a Project team divided work into four categories:

- Category 1: 72 tasks-potential operability issues completed June 1, 1995

- Category 2: 41 tasks-operations and maintenance programs

- Category 3: 71 tasks-modifications

- Category 4: 5 tasks-configuration control

> Budgeted project work hours - 40 person years

> Project hours expended to-date - 24 person years o NRC inspection June 5 - 16, 1995 23 Emergency Power Project

  • Continuing Initiatives

> Complete remaining project commitments Implement Category 3 Modifications 24 12

Design Basis Documentation

> Project started in 1989

> Not a reconstitution, unless design basis missing

  • Progress to Date

> $2.5 Million spent to-date o 64 of 89 complete

> All remaining DBD's in progress 25 Design Basis Documentation

  • Continuing Initiatives a Project to complete 12-31-95

> Ensure appropriate tests exist for design basis functions 26 13

Oconee Safety-Related Designation Clarification Project (OSRDC)

  • Background

) 1993 EDSFI/SWSOPI identified QA classification issues

> Internal/external questions on basis for QA classification n 83-28 response not clear a Duke committed to increase testing and maintenance requirements for SSCs important to safety.

  • Progress to Date

)> Formed OSRDC team to clarify licensing basis and develop QA-5 program

> Submittal to NRC 4/12/95 I NRC meetings held 27 Oconee Safety-Related Designation Clarification Project (OSRDC)

  • Continuing Initiatives a Verify QA-1 SSC's Categorized Properly

- Design document review is complete, verification begun

- Documents reviewed for post-licensing commitments, tabulation begun

- Tabulation due to NRC 7/10/95

- Final repository for QA classification will be Equipment Data Base (EDB)

> Identify non QA-1 SSCs that mitigate accidents

- Contractors hired; pilot accident review has begun a Develop augmented quality standards program (QA-5) for non QA-1 SSCs - to begin 4th quarter 1995 28 14

Service Water

Background

a Duke LPSW SITA (1987) a NRC SWSOPI (Fall 1993) a NRC SWSOPI follow-up inspections (Fall 1994)

Progress to Date

> Plan for resolution presented during Duke/NRC meeting on Feb. 24,1995.

> Majority of issues resolved/closed 29 Service Water Continuing Initiatives

> Complete 8 of 9 remaining SWSOPI issues by end of 1995

> Complete GL 89-13 (9th issue) in 1996.

> CCW upgrade modification

-upgrade portions to QA1

- LPSW supply to CCW pumps

- auto restart CCW pump

- complete by end of 1997 30 15

Testing

  • Background

> Inconsistent testing philosophies and programs a Several events during testing

  • Progress to Date a Formed Testing Quality Improvement Team

> Developed testing directive a Formed IST and Appendix J working groups

  • Continuing Initiatives

> Implement testing directive o Develop on-line Post Maintenance/Post Modification Testing database 31 Major System/Equipment Issues

  • CRDM Slow Trip Times
  • Valves
  • SSF Design Margins
  • DC Ground Detection/Location
  • Batteries
  • Trip Reduction
  • Major Modifications
  • Maintenance Rule 32 16

CRDM Slow Trip Times

  • Background a NEQST Top Site Issue a Detected slow drives during outages

> Type A drives on Unit 1 and Unit 2

> Apparent root cause - crud build-up a BWOG Project 33 CRDM Slow Trip Times Progress to Date

> Automatic trip time recording feature

> Scheduled outages on Unit 1 and Unit 2 for testing

> Installed modified thermal barriers Continuing Inititatives

> Unit 1 Refueling Outage - Replace or refurbish slow drives (14 presently identified)

> Unit 2 Refueling Outage - Replace or refurbish slow drives (1 presently identified)

> Complete BWOG Project

> Continue trip time testing during shutdowns w Monthly 10% rod movement on Units 1 and 2 34 17

Valves

  • Background a NEQST Top Site Issue n $5.7 million station valve budget

> INPO SOER

> Regulatory Bulletins

  • Progress to Date

> Established Valve Working Group

> Developed Obsolete and Problem Valve List

> Expanded Valve Diagnostics Program

  • Continuing Initiatives a Continued emphasis on regulatory and equipment issues relative to valves

> Generic letter on Pressure Locking/ Thermal Binding 3

SSF Design Margins

  • Background

>> NEQST Top Site Issue a DBD effort identified restrictive U1 seal leakage limits

> Annual SSF drill identified weakness in meeting 10 minute activation time

  • Progress to Date

> Completed detailed margin evaluation a Enhanced procedures to shorten activation times

> Additional focus on training 36 18

SSF Design Margins

  • Continuing Initiatives

> Upgrade seal leakage instrumentation

> Activation Time

- Develop technical basis for establishing SSF ASW at 14 minutes.

- Reduce operator actions required 37 Emergency Feedwater System Overpressure

  • Background

> NEQST Top Site Issue

> Excessive pump discharge pressures at low flow rates

>> Turbine Driven Emergency Feedwater (TDEFDW) pump turbine steam control valve

  • Progress to Date

> Replacing Motor Driven EFW Pump Automatic Recirculation Control (ARC) Valves

  • Continuing Initiatives

> Install Strainers in Steam Supply Lines x Reduce overspeed trip setpoint for TDEFDW pump turbine 38 19

DC System Detection/Location

  • Background
  • Policy for clearing grounds not clear
  • Limited ability to locate grounds D Effects of multiple grounds not well understood
  • Progress to Date

> Established multi-site DC Task Force x Issued criteria for ground detector settings

  • Developed policy for locating grounds x Completed design study on effects of multiple grounds
  • Continuing Initiatives D Develop Selected License Commitment (SLC) to control station response based on magnitude of ground a Search for optimum ground location equipment 39 Batteries
  • Background a Performance tests indicated capacity of some Exide batteries less than original rating
  • Progress to Date a Manufacturer investigating root cause

> Currently operable due to capacity margin in battery sizing calculation a Service tests demonstrated capacity adequate for design discharges

  • Continuing Initiative

> Evaluate revised battery capacity curves to determine adequacy for application a Investigate replacement options a Take action based on root cause 40 20

Trip Reduction

  • Background

> Increased Trend in Reactor Trip Frequency

  • Progress to Date a Reviewed Reactor Trip Reports a Reviewed responses to selected SPIP recommendations a Recommendations to station management

> Modifications selected for implementation a Human Performance Program improvements highest priority

> Reviewed Feedwater/Condensate System trips 41 Trip Reduction

  • Continuing Initiatives a Human Performance Improvement Plan a Modifications beginning Unit 1 RFO 42 21

Major Modifications

  • Completed

> Upgraded Nuclear Instrumentation System

> Deleted N16 Decay Tank

> Replaced Reactor Building Cooling Unit Cooling Coils 43 Major Modifications

  • Implementation in Progress

) Replace Inverters and Chargers a Upgrade Nuclear Instrumentation System

> Replace ARC Valves for MDEFWP's

>> Reroute RCS Highpoint Vent Piping

)> Fiber Optic Communication technology

)> Replace LPSW Piping for HPI Motor Cooler Discharge

> 230KV Switchyard Degraded Grid Protection Upgrade

> Vehicle Barrier System Addition 44 22

Major Modifications

  • PLANNED

>> Automatic Feedwater Isolation for MSLB

> CCW System Upgrade

> OAC Replacement

> Add 2/3 Logic for MSRH/MSRH Drain Tank Trip (SPIP)

> ICS Upgrade

> Keowee ACB Upgrades a Keowee Voltage Regulator Upgrades

> Keowee Overspeed and Trip Protection

> Phase 3 Dry Cask Storage Maintenance Rule Implementation

  • Background

> Multi-site team began implementation March 1, 1994

> Coordinated with License Renewal

> Followed NUMARC 93-01

  • Progress to Date

> Site implementation in progress x Performance monitoring is being transferred to the system engineers

> Removal-from-Service Risk Assessment Matrix implemented

  • Continuing Initiatives

> Implement directives and training

> Implement Maintenance Rule June 1996 23

Summary

  • Long standing issues being resolved
  • Strong interface with station
  • Sensitive to NRC feedback
  • Work Management Process improving
  • Focusing on long range planning
  • Engineering management team committed 47 24