ML14190A419
| ML14190A419 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 10/29/1980 |
| From: | Miner S Office of Nuclear Reactor Regulation |
| To: | Office of Nuclear Reactor Regulation |
| References | |
| NUDOCS 8011070157 | |
| Download: ML14190A419 (3) | |
Text
01 ptREG&(
Ao RUNITED STATES 0
NUCLEAR REGULATORY COMMISSION WASHINGTON, D. C. 20555 October 29, 1980 Docket No. 50-261 LICENSEE:
CAROLINA POWER AND LIGHT COMPANY FACILITY: H. B. ROBINSON STEAM ELECTRIC PLANT, UNIT NO. 2
SUMMARY
OF MEETING HELD ON OCTOBER 15, 1980 WITH CAROLINA POWER AND LIGHT COMPANY TO DISCUSS H. B. ROBINSON 2 A meeting was held on October 15, 1980 between members of Carolina Power and Light Company (CP&L) and the NRC staff to discuss the recent and future inspections of the H. B. Robinson steam generators. The attendees list is attached.
CP&L has calculated from the eddy current inspections in April and August/
September, small corrosion rates for the steam generators. We indicated that because of the differences in inspection techniques between the April and August/September inspections there is a large uncertainty in the calcu lated corrosion rates.
Therefore, because of this and the current condition of the steam generators, we requested that CP&L, prior to full power operation of Robinson, provide the following:
1.
During the upcoming cycle, CP&L should commit to conduct a steam generator eddy current inspection prior to exceeding six effective full power months of operation. The inspection should utilize the same techni ques as employed during the August/September inspection. At least 45 days prior to the inspection, CP&L should submit to the staff for review, a report providing the scope and inspection techniques.
- 2. The current Tech Spec limits for total leakage (0.35 gpm) was acceptable provided CP&L recommends acceptable limits for ramp and step changes in leakage rates which if exceeded, the plant would be shut down and the steam generator inspected. Scope and -inspection techniques should be provided to the NRC for review at that time.
- 3. CP&L should provide a report on the steam generator chemistry control, improvements to date and planned future improvements. This could be submitted after the plant has reached full power operation.
- 4. A member of the NRC staff and/or consultant representing the staff should be allowed to witness any future inspections of the steam generator.
80110711570
Meeting Summary for H. B. Robinson 2 2 -
October 29, 1980 CP&L were in general agreement with the staff requests and will, within a few days, provide a letter providing their detailed responses to our requests.
Sydney Min r, Project Manager Operating Reactors Branch #1 Division of Licensina cc:
See next page VI
Meeting Summary for H. R. Robinson 2 3 -
October 29, 1980 Docket Files NRC PDR ORBI Reading NRR Reading H. Denton E. Case
- 0. Eisenhut R. Purple T. Novak R. Tedesco G. Lainas G. Zech S. Varga T. Ippolito R. Clark R. Reid D. Crutchfield
. J. Youngblood Schwencer J. Miller J. Wetmore B. Grimes H. Collins F. Pagano EPDB, DL Project Manager OELD OSD (3)
S. Showe, I&E C. Parrish R. Fraley, ACRS (16)
Principal Staff Participants Licensee Short Service List