ML14178A448

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Insp Rept 50-261/94-03 on 931226-940122.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation & Esfs Walkdown & Plant Safety Review Committee Activities
ML14178A448
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 02/18/1994
From: Christensen H, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A446 List:
References
50-261-94-03, 50-261-94-3, NUDOCS 9402280095
Download: ML14178A448 (15)


See also: IR 05000261/1994003

Text

pfR REsG

UNITED STATES

0

NUCLEAR REGULATORY COMMISSION

REGION I

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/94-03

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: December 26, 1993 - January 22, 1994

Lead Inspector:

1 - -Yc-3/'14

.J1

W. T/ Orders, Synior dsident Inspector

Date Signed

Other Inspectors:

C. R. Ogle, Resident Inspector

P. A. Balmain, Resident Inspector, Vogtle

P. Byron, Resident Inspector, Brunswick

C. W. Rapp, Region II Inspector

M. N. Miller, Region II Inspector

J. L. Starefos, Project Engineer

Accompanying Personnel:

E. Wang, Reactor Engineer (Intern)

Approved by:

t i2<

H. 0. Christensen, Chief

Date Signed

Reactor Projects Section IB

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

engineered safety feature system walkdown, plant safety review committee

activities, followup of previously identified items and verification of the

completion of Confirmation of Action Letter commitments.

Results:

A non-cited violation was identified which involved the failure to make timely

NRC notification of licensed operator termination and failure to respond.to a

notice of violation within specified time, paragraph 3;

a violation was

.identified

which involved inadequate debris intrusion control measures

employed during maintenance, paragraph 4; a second violation was identified

involving the licensee's failure to post the response to a radiological

working condition violation, paragraph 6.

9402280095 940218

PDR

ADOCK 05000261

G

PDR

REPORT DETAILS

1.

Persons Contacted

  • G. Attarian, Chief Electrical Engineer
  • R. Barnett, Manager, Projects Management

C. Baucom, Shift Outage Manager

  • D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance

J. Benjamin, Shift Outage Manager, Outages and Modifications

S. Billings, Technical Aide, Regulatory Compliance

  • B. Clark, Manager, Maintenance
  • T. Cleary, Manager, Technical Support

D. Crook, Senior Specialist, Regulatory Compliance

  • C. Dietz, Vice President, Robinson Nuclear Project
  • W. Dorman, Acting Manager, Regulatory Affairs

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

S. Farmer, Manager, Engineering Programs, Technical Support

B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

  • M. Herrell, Manager, Training
  • S. Hinnant, Director, Site Operations

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

E. Lee, Shift Outage Manager, Outages and Modifications

A. McCauley, Manager, Electrical Systems, Technical Support

R. Moore, Acting Operations Manager

0. Morrison, Shift Supervisor, Operations

  • M. Page, Manager, RESS Mechanical

D. Nelson, Shift Outage Manager, Outages and Modifications

  • C. Olexik, Robinson Assessment Section

A. Padgett, Manager, Environmental and Radiation Control

  • M. Pearson, Plant General Manager

D. Seagle, Shift Supervisor, Operations

M. Scott, Manager, Reactor Systems, Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

0. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

The Unit began the report period continuing the forced outage,

which began on November 17.

The Unit remained shutdown throughout

the report period while the licensee implementing corrective

actions to equipment and personnel deficiencies identified during

the forced outage and as required by an NRC Confirmation of Action

Letter issued on November 19, 1993.

2

3. Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

The inspectors reviewed shift logs, Operation's records, data

sheets, instrument traces, and records of equipment malfunctions

to verify equipment operability and compliance with TS. The

inspectors verified that the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, were cognizant of in

progress surveillance and maintenance activities, and were aware

of inoperable equipment status through work observations and

discussions with Operations staff members. The inspectors

performed channel verifications and reviewed component status and

safety-related parameters to verify conformance with TS.

Shift

changes were routinely observed, verifying that system status

continuity was maintained and that proper control room staffing

existed. Access to the control room was controlled and operations

personnel carried out their assigned duties in an effective

manner. Control room demeanor and communications were

appropriate.

Plant tours were conducted to verify equipment operability, assess

the general condition of plant equipment, and to verify that

radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were

properly implemented.

b.

Notification Of Unusual Event Due To Both EDGs Being

Inoperable

At 3:12 p.m. on January 17, 1994, the licensee declared an

Unusual Event when it was concluded that both EDGs were

inoperable. The A EDG was declared inoperable when the

licensee found water dripping onto the diesel's control

cabinet and current transformer cubicles. The B EDG had

previously been removed from service to support maintenance

and modification work. The licensee suspended work on the B

EDG and removed the clearance. The Unusual Event was exited

at 5:13 p.m. that day, following restoration and successful

testing of the B EDG.

The inspectors were notified of the event, reported to the site,

and witnessed the licensee's event response. In general the

inspectors concluded the response was satisfactory. The

3

inspectors also verified that appropriate notifications were

performed in accordance with regulatory requirements.

The licensee determined the source of the water leaking onto the

diesel to be coming from valve EV-6646, an EAC 2 Solenoid Valve.

Service water was spraying from the body to bonnet joint on the

valve, into the air intake enclosure of EAC-2. A portion of this

spray entered a normally open damper which penetrates the A EDG

room immediately above the current transformer and generator

control cubicles.

The licensee theorized that the valve failure occurred as a result

of freezing conditions experienced in the EAC air intake

enclosure. It was also noted that the air intake dampers on the

EAC were not properly closing which probably exacerbated the

situation.

The inspectors witnessed the satisfactory testing of B EDG in

accordance with procedure OP-604, Diesel Generators A and B, and

the system's return to service.

c.

Failure To Make Timely NRC Notifications

On December 28, 1993, the licensee informed the resident staff

that a notification to the NRC concerning the status of a licensed

operator as well as a violation response, were not made within the

prescribed timeframes.

The late notification involved a licensed operator who terminated

his employment effective October 29, 1993. The required written

notification to the NRC concerning the status change was not made

until December 24, 1993, which exceeded the allowed 30-day

reporting requirement specified in 10 CFR 50.74.

The late violation response involved the licensee's written

response to a violation documented in NRC Inspection Report

50-261/93-26. The licensee's response was dispatched on

December 29, 1993.

In as much as the Notice of Violation was

dated November 26, 1993, the response exceeded the allowed 30-day

response timeframe of 10 CFR 2.201.

An Adverse Condition Report was generated by the licensee in

response to these incidents. The inspectors were informed that

these events were reviewed with the cognizant individuals and that

a generic checklist/scheduling aid to track the timeliness of NOV

responses and LERs would be generated.

Additionally, the licensee stated that a process to allow track of

required correspondence to the NRC on issues related to licensed

operators would be developed.

4

The failure to communicate the notification and violation response

in accordance within the specified timeframes is a violation.

This violation will not be subject to enforcement action however,

because the licensee's effort in identifying and correcting the

violation meet the criteria specified in Section VII.B of the

Enforcement Policy.

This is identified as a non-cited violation, NCV:

94-03-01,

Failure To Make Timely NRC Notification Of Licensed Operator

Termination And Failure To Respond To A Notice Of Violation Within

Specified Timeframe.

d.

Confirmation of Action Letter Followup Efforts

On November 18, 1993, CP&L management made the decision to

place Robinson Unit 2 in cold shutdown due to a concern with

a mis-configured core reload.

Confirmation of Action Letter

(CAL) was issued documenting the licensee's planned actions

to identify the root cause of the mis-configuration,

determine the cause of detected nuclear instrumentation

anomalies, evaluate operator performance, and assess the

status of not only Robinson's organization, but also plant

equipment, to determine if the facility was ready for

restart.

The Resident Inspection Staff, assisted by Region II

inspectors, conducted independent reviews of the licensee's

actions. The issues inspected during this report period are

detailed below.

i)

General Plan For Restart Readiness

The inspectors reviewed procedure PLP-059, Plan

For Restart Readiness And Startup and Power

Ascension, Rev. 4. The procedure delineates the

licensee's program designed to complete a self

assessment for readiness to safely startup and

operate Robinson Nuclear Plant following the

forced outage which began on November 17, 1993.

Completion of this self-assessment is based upon

verification of the successful completion of the

"Startup Required Actions", specified in the NRC

Confirmation Action Letter dated November 19,

1993, as well as a review of system readiness,

organizational readiness, operational readiness

and verification of core configuration.

The Plant Manager was responsible for determining whether

improvement items identified during these reviews were

required to be completed before unit startup or long term

issues. The review of Systems Readiness augmented the

requirements of procedure PLP-027, System Startup Readiness

5

Determination, to include affirmations by the responsible

Systems Engineers that their respective systems were ready

to support safe, reliable operation. The affirmations were

based on reviews of system conditions that may have changed

since completion of PLP-027 reviews following Refueling

Outage 15, completion of "Startup Required Actions" and

verification that required activities are included in the

Startup And Power Ascension Schedule.

The review of Organizational Readiness performed

by each Unit Manager and the Plant Manager,

required each Unit Manager to affirm that their

organizations and personnel were prepared to

support plant operation and to demonstrate this

preparation to the Site Vice President.

Finally, the review of Operational Readiness was performed

to ensure each shift supervisor and operating crew were

satisfied with the plant material condition and were

prepared to operate the plant safely. A collective

evaluation was performed which led to the Plant Manager's

recommendation to the Vice President that plant heatup

activities commence.

ii) Action Item: Barriers To Prevent Repeating Industry

Events

The licensee addressed this issue with both long and short

term corrective actions.

The short term actions were listed

as Corrective Action #5 in the Nuclear Instrumentation

Incident Evaluation Team's (NIIET), Recommended Corrective

-Actions Prior to Restart memo to C.R. Dietz dated

November 24, 1993. The team recommended that Operations

Management ensure that Operations personnel do not develop

tunnel vision by concentrating only on Reactivity

Management. It was recommended that Operations Management

revisit the March 24, 1993, letter from Kenneth Strahm to

R.-A. Watson of CP&L which highlights the need to maintain

control of key primary plant parameters. The inspectors

reviewed the March 24, 1993, Strahm letter which contains

descriptions of six events which occurred during the

previous 12 months.

Each of the events related to operator

inattention during restart.

The inspectors also reviewed the December 18, 1993, memo

from the Acting Operations Manager to the Operations Staff

listing his expectations. The listed expectations appeared

to be adequate, addressing all aspects of the operators'

duties and responsibilities.

In addition, the inspectors reviewed the Pearson to Dietz

January 6, 1994, memo which documents the close out of

6

Corrective Action No. 5. The inspectors also reviewed the

January 7, 1994, memo (RAP/94-0060) from the Plant Manager

to Operation shift crew members which documents his

discussions with them.

Long term corrective actions were listed as Corrective

Action No. 14 for ACR 93-284. The corrective actions

include the following:

.

Communicate the importance of

incorporating industry operating

experience to enhance the equipment and

personnel performance at Robinson.

.

Use the power range NI indication event as a

case study to reinforce the importance of

barriers in the event and compare with the

operating experience from a similar 1989 event

at HNP, in series of employee information

meetings for all site employees.

Have one or more of the Investigation Team

members participate in the employee

meeting presentations.

Emphasize, during these employee meeting

presentations, the expectation that

managers and employees should consider how

lessons learned from industry experience

can be most beneficial or can be related

to experience at Robinson.

C. R. Dietz documented the closure of this item in his

January 21, 1994, memo to W. Dorman, Corrective Action

Program Manager. The licensee has assembled a notebook of

Operating Experiences for Plant Startup and plans to have

the onshift crews review it and have related discussions

prior to commencing selected major evolutions.

The inspectors concluded from their review and discussions

with licensee personnel that the licensee has completed both

the long and short term corrective actions.

iii)

Action Item: Independent System Walkdowns

Between January 4 and January 11, 1994, the inspectors

conducted detailed walkdowns of portions of the AFW, SI, and

A EDG systems. They were performed as an independent review

of the material condition of the systems as well as a check

on the thoroughness of the system engineer/SRO walkdowns

conducted as part of the PLP 27/59 process.

7

During the walkdowns, the inspectors observed a number of

deficiencies on each of the systems which had not been

detected by the system engineer/SRO walkdowns. The

deficiencies were identified to the system engineers for

disposition. Although the deficiencies were minor and did

not impact the operability of the systems, the number and

ease of discovery of the deficiencies, concerned the

inspectors about the thoroughness of the remainder of the

PLP 27/59 walkdowns. During discussions with licensee

management about these concerns, the inspectors became aware

of two factors that may have contributed to the lack of

walkdown thoroughness observed by the inspectors. One

factor was that plant management's initial expectations for

the performance of the walkdowns were not adequately

communicated to site personnel.

This was recognized by

management during the walkdown process and further guidance

was provided. Additionally, all Engineering Tech Support

Management was not uniformly performing verifications of the

walkdowns.

Following the discussions between licensee

management and the inspectors on this point, Engineering

Technical Support Management performed a series of intensive

verifications of the plant walkdowns. The inspectors were

informed that these walkdowns revealed additional

deficiencies, none of which however, impacted system

operability.

Overall, the inspectors concluded that the system walkdowns

were an enhancement in the licensee's system readiness

evaluation process. Although the walkdowns were sufficient

to determine system operability, they lacked the

thoroughness to identify all readily apparent system

deficiencies. Weak management oversight contributed to this

deficiency.

During the walkdowns, the inspectors noted that a number of

limit switch cover bolts were missing for actuators on the

following valves:

SI-866A (1 bolt missing); SI-867A (1 bolt

missing); and SI-867B (2 bolts missing).

The inspectors

questioned the impact of these missing cover bolts on the EQ

qualification of these motor operated valves. The

inspectors were provided documentation by the licensee that

demonstrated that the missing cover bolts did not impact

valve operability. The inspection also reviewed completed

maintenance work requests on these valves during RFO-15.

The packages required that the limit switch covers be

installed following maintenance. These observations were

discussed with the cognizant supervisor and the maintenance

manager. The inspectors were informed that based on these

observations, the licensee was in the process of conducting

a walkdown of readily accessible MOVS. Approximately 25

percent of the accessible MOV population was subsequently

  • 0

8

inspected and only one other case of a missing cover bolt

had been detected.

During the EDG A walkdown, the inspectors observed that the

EDG A configuration did not match the controlled drawings.

Similarly drawing/system configuration errors were observed

during the AFW system walkdown. While none of the

deficiencies were significant, each was easily recognizable

by comparing the drawing to the system. While following up

on this deficiency the inspectors were informed by plant

management that it was not an explicit expectation that

drawing be used during the system engineer/SRO walkdowns.

The inspectors were also informed that the EDG A walkdown

was "preliminary" and that the PLP 27/59 for this system was

being held in abeyance pending the results of

troubleshooting on the EDG B.

During the SI system walkdown, the inspectors observed that

no flow existed through the "C" SI pump thrust bearing

cooler. Though the pumps were not required in the existing

plant configuration, SW flow had existed through the cooler

earlier that day. The inspectors were informed by the

system engineer and Operations Manager that the SW flow had

been throttled to prevent overflowing SW drains. The

inspectors were also informed that fluctuations in the SW

system pressure due to service water booster pump testing

was responsible for this observed change in SW flow.

iv) Action Item: Improve Shift Turnover Briefings

The inspectors reviewed revisions to Procedure OMM

008, Minimum Equipment List and Shift Relief, to

determine if the revisions provided additional

guidance to ensure sufficient information is turned

over for a proper relief. The inspectors reviewed

document change form 93-P-2301 and its accompanying 10

CFR 50.59 determination for revision 71 of the

procedure. The inspectors noted that procedure OMM

008 had been revised to add new shift relief

responsibilities for the Work Control-Center Senior

Control Operator (Section 5.1.5) and additional

turnover checklist for the offgoing Work Control

Center Senior Control Operator, Auxiliary Operators,

Fire Protection Technical Aide, and Makeup Water

Treatment Auxiliary Operator (sections 5.1.5, 5.1.7,

and 5.1.9)

The inspectors concluded that procedure OMM-008 had

been enhanced and that the additional attachments will

improve shift turnovers for several positions in the

control room.

09

v)

Action Item:

Expectations For Pre-job Briefings

The inspectors reviewed the licensee's restart

closeout package 02-13 which included Document Change

Form 93-P-2033 with a 10 CFR 50.59 determination for

revision 41 of procedure GP-003, Normal Plant Startup

From Hot Shutdown To Critical.

The inspector verified

that procedure GP-003 section 5.2, Instructions For

Taking The Reactor Critical contains instruction steps

(5.2.1, 5.2.2, and 5.2.3) to require that a Management

Designated Monitor (MDM) be assigned and given

permission to take the reactor critical. A pre-shift

briefing, SWAG/Outage Turnover meeting review and a

pre-job briefing checklist are also required to be

completed prior to taking the reactor critical.

The inspector also reviewed Document Change Form 93-P

2183 for revision 37 of Procedure GP-005, Power

Operation and the revised procedure. The inspector

verified that section 5.2, which deals with warming up

the secondary was revised to incorporate instruction

steps (5.2.1 and 5.2.2) to require MDM permission

prior to performing the evolution. A pre-shift

briefing, SWAG/Outage Turnover Meeting Review and Pre

job Briefing checklist and also required prior to

performing the evolution.

The inspector reviewed revisions to the outage

management manual and verified that a-format for shift

turnover meetings was developed and instructions were

incorporated to identify infrequently performed

evolutions and notify a MDM prior to the evolution.

Procedure PLP-037, Conduct of Infrequently Performed

Tests and Evolution Section 5.3.2 provides

requirements from the content of pre-job briefings and

management expectations for conduct of the evolutions.

A pre-Job Briefing Checklist (Attachment T.6) is

incorporated into the implementing documents and is

required to be performed prior to conducting the

evolution.

The inspectors concluded that the above changes

enhanced the guidance for the conduct of pre-job

briefings.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, and approved procedures. The

10

inspectors determined that these activities did not violate LCOs

and that required redundant components were operable. The

inspectors verified that required administrative, material,

testing, radiological, and fire prevention controls were followed.

In particular, the inspectors observed/reviewed the maintenance

activities detailed below.

WR/JO 94ABHC1

Examine A Diesel Switches/Mag Amps

For Water Damage

WR/JO 94AAMN

Remove, Inspect Air Start Check

Valves On A EDG

b.

Failure To Follow Procedure During Maintenance In Diesel

Room

The inspectors witnessed licensee activities to

resolve an electrical ground on the A EDG per WR/JO

94-ABHC1.

During the conduct of this effort, the

inspectors observed steel shot on the floor inside the

EDG control cabinet.

This observation was confirmed

by the I & C supervisor.

Additional shot was found

elsewhere in the control cubicle; in the current

transformer cubicle; in a drip pan beneath the engine

blower; and in the generator enclosure itself.

As a result of this discovery, the licensee conducted a

boroscope examination of accessible areas in the generator

enclosure and vacuumed accessible portions of the generator

housing.

Examination of the vacuum cleaner's contents

following the vacuuming of the generator enclosure and other

adjacent areas revealed approximately 35 steel shot.

The licensee determined the source of the steel shot to be

the use of a paint stripping machine in the A EDG room

during the refueling outage. The licensee stated that the

machine was only used briefly in the A EDG room in attempt

to remove paint from the floor. The inspectors learned that

the machine had also been used in the hallway in the

auxiliary building and in the charging pump room. On

January 19, 1994, the inspectors were informed that

approximately 3 steel shot were discovered in the C charging

pump motor frame, but none-were found in room's electrical

cubicles.

Technical Specification 6.5.1.1, Procedures, Tests, and

Experiments requires, in part, that written procedures be

established, implemented, and maintained covering the

activities recommended in Appendix A of Regulatory Guide

1.33, Rev 2., 1978, including general procedures for the

control of maintenance. Maintenance Management Manual

Procedure, MMM-001, Maintenance Administration Program

1*1

requires the use of adequate debris intrusion control

measures during the performance of maintenance.

Contrary to the above, inadequate debris intrusion control

measures were used on November 15, 1993, during paint

stripping efforts on the Emergency Diesel Generator A room

floor. As a result, steel shot was introduced into

Emergency Diesel Generator A as well as its associated

generator control and current transformer cubicles. This is

identified as Violation, VIO 94-03-02: Failure To Employ

Adequate Debris Intrusion Control Measures.

5.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements.

For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, testing was accomplished

by qualified personnel in accordance with an approved test procedure,

and test instrumentation was properly calibrated. Upon test completion,

the inspectors verified that the systems were properly returned to

service. Specifically, the inspectors witnessed/reviewed portions of

the following test activities:

SP-1289

B EDG Failure To Start Test

EST-048

Control Rod Drop Test (Refueling Outage)

OP-604

Diesel Generators A and B

No violations or deviations were identified.

6.

Plant Support - Radiological Controls (71707)

Failure To Post A Response To A Radiological Working Condition Violation

On January 5, 1994, the inspectors observed that the licensee's response

to violation 50-261/93-26-01 and 93-26-03 had not been posted as

required by 10 CFR 19.11 (a)(4)(e). These violations involved

inadequate control .of locked high radiation area keys and improper

control of a basket containing an irradiated bolt in the spent fuel

pool.

The licensee's response was dispatched on December 29, 1993.

Hence, the Response was not posted within the 2-day timeframe specified

in 10 CFR 19.11 (a)(4)(e).

10 CFR 19.11 requires that the licensee's

response to a violation involving radiological working conditions be

posted within 2 days of dispatch.

Contrary to the above, on January 5, 1994, the licensee failed to follow

10 CFR 19.11 (a)(4)(e), in that, the response to violations 50-261

93-26-01 and 93-26-03 were not posted within two working days of

dispatch.

12

The inspectors noted that this violation was similar to NCV 92-24-03

documenting the failure to post a violation involving deficiencies

associated with contaminated vacuum cleaner servicing in July 1992.

7.

Review of Licensee Event Reports (92700)

The below listed LERs were reviewed to determine if the information

provided met NRC requirements. The determination included: adequacy of

description, verification of compliance with Technical Specifications

and regulatory requirements, corrective action taken, existence of

potential generic problems, reporting requirements satisfied, and the

relative safety significance of each event.

LER 91-002, Reactor Trip Due To Lo-Lo Steam Generator Level.

LER 92-002, Failure To Test All Circuitry Associated With Auxiliary

Feedwater Auto Start.

LER 92-015, Seismically Inoperable Service Water System Due To Corroded

Piping.

LER-92-022 , Potential For ESF Inoperability Due To Procedure

Defect.

LER-92-001, Degraded Condition Due To Inoperability Of Containment

Isolation Valve.

The corrective actions for the above LERs have been completed and

no violations or deviations were identified. These items are

closed.

8.

Licensee Action on Previous Findings (92701, 90702) (Followup)

(Closed) IFI 93-28-05, Documentation Of Lead-Lag Controller Accuracy.

Inspection Report 93-28 documents IFI 923-28-05, regarding an

inspector request for documentation to support the lead-lag

controller accuracy used in an error analysis of the pressurizer

pressure instrumentation. The lead-lag controller accuracy used

in the analysis was one percent instead of the two percent

specified in MMM-006, Calibration Program.

On January 17, 1994, the inspectors were provided a copy of Engineering

Evaluation, EE 94-012. This evaluation reviewed sixty-six calibration

of lead/lag units. Based on this review, the engineering evaluation

concluded that assigning a one percent calibration tolerance to the

lead-lag controllers was acceptable.

Based on the information presented in the EE, the inspectors have no

further questions. This item is closed.

13

(Closed) DEV 93-33-02, Failure To Install RHR Pump Suction Pressure

Instrumentation As Committed To In Response To Generic Letter 88-17.

The licensee performed an evaluation for Modification 1011,

"Instrumentation for Mid-Loop Operation" and determined that the

monitoring of RHR pump discharge pressure would be more appropriate.

The monitoring was implemented as required during Refueling Outage 13

(Spring, 1991).

This item is closed.

(Closed) VIO-92-28-02, SI-895K Valve Open When Safety Injection System

Is In Standby Mode.

Due to personnel error, open position was indicated

in OP-202. The licensee has revised OP-202. The inspector reviewed the

latest revision of OP-202, Revision 32, and found the position of SI

895K to be in the correct position of CLOSED. In addition, the

individual involved has been counseled. This item is closed.

(Closed) VIO-92-31-01, The Contaminated Process Equipment Area (CPEA)

Posting For The Charging Pump Room Entrance Door Was Removed. The

corrective action includes revising The Lesson Plans For Contracted

Health Physics Technicians to emphasize that, although CPEA designation

is not standard to the industry, it is used at HB Robinson as part of

the Contamination Control Program. This item is closed.

(Closed) VIO 92-02-01, Failure to Follow The Procedure When Stroke

Timing The Primary Sampling System Containment Isolation Valve. The

inspector reviewed OST-701, Inservice Inspection Valve Test,

Revision 26, the latest revision.

Changes have been made to reflect

the current testing method. In addition, Valve Data Sheet in OST-701

has been revised to eliminate any inconsistencies discovered between the

test data sheet and the test acceptance criteria. This item is closed.

9.

Exit Interview (71701)

The inspection scope and findings were summarized on January 28, 1994,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. Dissenting comments were not received

from the licensee. The licensee did not identify as proprietary any of

the materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

NCV 94-03-01

Failure To Make Timely Notifications To

The NRC Relative To Operator Termination

And Response To A Violation

VIO 94-03-02

Failure To Employ Adequate Debris

Intrusion Control Measures

VIO 94-03-03

Failure To Post Response To Radiological

Working Conditions Violation

(III

14

10.

List of Acronyms and Initialisms

ACR

Adverse Condition Report

CCW

Component Cooling Water

CFR

Code of Federal Regulation

CPEA

Contaminated Process Equipment Area

DEV

Deviation

DG

Diesel Generator

EAC

Evaporative Air Conditioner

EDG

Emergency Diesel Generator

EE

Engineering Evaluation

ESF

Engineered Safety Features

GP

General Procedure

HNP

Harris Nuclear Plant

INPO

Institute of Nuclear Power Operations

LER

Licensee Event Report

MDAFW

Motor Driven Auxiliary Feedwater

MST

Maintenance Surveillance Test

NCV

Non-cited Violation

NI

Nuclear Instrumentation

NOV

Notice of Violation

OMM

Operations Management Manual

OP

Operating Procedure

OST

Operations Surveillance Test

PI

Pressure Indicator

PLP

Plant Program

RNP

Robinson Nuclear Project

SI

Safety Injection

TS

Technical Specification

URI

Unresolved Item

VIO

Violation