ML14178A256

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Insp Rept 50-261/92-19 on 920615-19.Violations Noted.Major Areas Inspected:Licensee Program for self-assessment of Problems,Followup of Previous Insp Item & Review Results of Testing Re GL 89-10
ML14178A256
Person / Time
Site: Robinson 
Issue date: 07/15/1992
From: Hunt M, Jape F, Casey Smith
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A254 List:
References
50-261-92-19, GL-89-10, NUDOCS 9208110103
Download: ML14178A256 (13)


See also: IR 05000261/1992019

Text

REG(

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.: 50-261/92-19

Licensee: Carolina Power and Light Company

P. O. Box 1551

Raleigh, NC 27602

Docket No.: 50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: June 15-19, 1992

Inspectors:

SM. Hunt

Date Signed

Approved by:

/9-

2

F. Jape, Chief

Date Signed

Test Programs Section

Engineering Branch

Division of Reactor Safety

SUMMARY

Scope:

This special, announced inspection was conducted to examine the licensee's

program for self-assessment of problems, followup of a previous inspection item,

and to review results of testing as related to Generic Letter 89-10.

Results:

The requirements of T.S. Section 6.5.1.6, concerning oversight activities of the

PNSC with regard to reviews of LERs, ACRs and SCRs, were verified as having

been satisfied. The licensee performs root cause analysis of LERs, ACRs, and

SCRs using investigative techniques such as Change Analysis, Barrier Analysis, and

Events and Causal Factors Charts. These root cause analyses were found to be

.

generally acceptable with a few exceptions. The developed corrective action plans

were consistent with the identified root causes and the corrective

9206110103 920722

PDR

ADOCK OBOOO261

0

PDR

2

action program monitored implementation of the corrective actions to assure

completion. A previously identified item related to GL 89-10, NRC Report No. 50

261/91-201 was closed. The review of the calculation for MOV FW-V2-6A,

related to the Generic letter 89-10 MOV Program identified one violation, 50

261/92-19-01, of Criterion III to Appendix B 10 CFR 50. (paragraph 4a.)

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

  • R. Barnett, Manager, Outages and Modification
  • C. Baucom, Project Specialist, Regulatory Compliance
  • W. Biggs, Manager, Nuclear Engineering Department Site Unit
  • S. Billings, Technical Aide, Regulatory Compliance
  • R. Chambers, Plant General Manager
  • S. Farmer, Manager, Engineering Programs
  • W. Gainey, Jr., Manager, Plant Support
  • M. Grantham, Nuclear Engineering Department, HESS/Mechanical
  • J. Harrison, Manager, Regulatory Compliance
  • P. Musser, Manger, Engineering and Technical Support, Nuclear

Assurance Department

  • J. Pearson, Nuclear Engineering Department, HESS/Mechanical
  • D. Stadler, Onsite Licensing Engineer/Nuclear Licensing

NRC Resident Inspectors

  • L. Garner, Senior Resident Inspector
  • C. Ogle, Resident Inspector
  • Attended exit interview

2.

Action on Previous Inspection Findings (92702)

Closed, VIO, 50-261/91-201

During an inspection of the licensee's Generic Letter (GL) 89-10, "Safety

Related Motor-Operated Valve Testing and Surveillance Program," a violation

was identified. Report No. 50-261/91-201, was issued on July 25, 1991,

and the notice of violation was forwarded in a letter issued October 4,

1991. The violation concerned the lack of documentation of corrective

actions taken for MOV FW-V2-6A, Feedwater Isolation Valve, which had a

galled valve stem. As a result of the violation the licensee has revised its

corrective action program to require complete documentation. In addition

the operations procedure for shutdown of the unit was revised to require

cycling of the three feedwater block valves during cool down to prevent

thermal binding of these valves which was determined to be a contributor to

the opening difficulties on valve FW-V2-6A. Additionally, during the recent

outage the valve stem was replaced. This violation is closed.

2

3.

Evaluation of Licensee Self-Assessment Capability (40500)

T. S. Section 6.5.1.6 describes the responsibilities of the PNSC and

specifies reviews to be performed by this onsite organization. Violations of

the TS are required to be investigated and a report prepared that evaluates

the event and provides recommendations to prevent recurrence. The PNSC

reviews these reports and evaluates the adequacy of the developed

corrective action plan. Additionally, station problems documented as ACRs,

or SCRS, are reviewed by the PNSC to ensure that an adequate root cause

analysis has been performed and an effective corrective action plan has been

developed. The inspectors performed an evaluation of the licensee's

self-assessment capability by reviewing monthly PNSC meeting minutes

covering a period from March 15, 1991 to March 20, 1992. Selected action

items dispositioned by the PNSC at these meetings were independently

reviewed using the investigative techniques delineated in the "NRC HPIP

Procedure and Module Manual."

a.

Licensee Event Reports

The inspectors reviewed the events and their root causes documented

on the following LERs and evaluated the proposed corrective actions

to determine their adequacy.

o

LER No.91-004, Rod Control System Urgent Failure

o

LER No.91-007, Failure to Perform Surveillance Test

0

LER No.91-009, Over Temperature Delta Temperature Channel

Inoperable due to Summator Module Lag Constants

0

LER No.91-013, Diesel Driven Fire Pump inoperable

0

LER No.92-002, Failure to Test all Circuits Associated with

the Auxiliary Feedwater Auto-Start

0

LER No.92-004, T.S. Violation During ILRT

The root causes for these plant events ranged from random hardware

failure to human errors and procedural deficiencies. The inspectors

determined that the root causes identified by the licensee were for the

most part correct with exception of the following examples. The root

cause for the event documented on LER 91-007 was given as human

error. Application of the guidance delineated in the NRC HPIP manual

identified the root cause to be inadequate communications which

3

resulted in less than adequate shift-turnover. The licensee's

developed corrective plan was considered adequate, however, in that

administrative controls were established to ensure adequate communi

cation and work control during shift changes. Additionally, plant

personnel were indoctrinated on the use of the new administrative

controls. Another example of inadequate root cause analysis was

identified on LER 91-013. The licensee identified the root cause as

failure of the design engineering program to replace existing 1000

120OF thermostats with 120 0-140aF thermostats. The inspectors

discovered, however, that the primary causal factor was failure of the

CAP to initiate corrective action for a station problem that was

identified in October 1989 and which was documented on WR/JO

89-AJMF1. Discussions with licensee's personnel revealed that the

CAP was in a process of transition at the time the deficiency was

identified. This probably was the reason why it failed to initiate

corrective action for an identified and documented station problem. A

definitive evaluation of this root cause can not be made, however,

because of its indeterminate status. The licensee's implemented

corrective action for LER 91-013 was considered adequate based on

change out of the thermostats and an increase in the power rating of

the associated heater.

b.

Adverse Condition Reports/Significant Condition Reports

ACRs and SCRs dispositioned by the PNSC during regular monthly

meetings were independently reviewed by the inspectors for root

causes in order to evaluate the licensees self-assessment capability.

Objective evidence reviewed during this effort are listed as follows:

SCR No.89-022

SCR No.89-015

SCR No.89-018

SCR No.90-013

ACR No.91-009

ACR No.91-034

ACR No.91-283

ACR No.91-286

ACR No. 92-20

4

The inspectors determined that the licensee used various investigative

techniques during the performance of root cause analyses. Among

these were Barrier Analysis, Changes Analysis, and Events and Causal

Factor Charts. Based on review of the above ACRs/SCRs the

inspectors concluded that the root causes identified by the licensee

were generally correct. ACR No.91-286 was a typical example and

involved failure of the narrow range OTDT RTD instrumentation circuit

to meet TS requirement of 0.75 seconds time delay. This event was

also reported to the NRC on LER 91-009-01. The licensee correctly

identified the root causes documented on ACR No.91-286.

Additionally, the inspectors reviewed the close-out package and

verified that the developed corrective action plans for the three

primary causal factors specified in the LER had been completed in

accordance with the Licensee's commitments. SCR No.88-022

further demonstrated the licensee's capability to perform effective

self-assessments. This SCR involved an event wherein the reactor

vessel cavity boron concentration was inadvertently diluted to less

than 1950 ppm during a RFO with fuel off loaded. The inspectors

used the guidance of the NRC HPIP Module and determined the near

root causes to be in the functional areas of training, procedures,

supervision, and communications. The licensee's developed

corrective action plans for the seven causal factors identified in the

Event and Causal Factor Chart fell within the functional areas

identified by the NRC HPIP module.

Some inadequate root cause analyses were identified by the

inspectors. Typical of this small sample was ACR No.91-034. This

ACR involved an event related to inadequately revised calibration

procedures required per plant modification M-959. Licensee

management determined the root cause to be indeterminate. The

inspectors, however, identified the near root causes as inadequate

design control. Specifically, the postmodification/calibration test

requirements and test acceptance criteria were not adequately

specified in the plant modification package. The immediate corrective

action of revising the loop calibration procedures to be technically

adequate was necessary but not sufficient to prevent recurrence of a

similar problem. Discussions with the senior resident inspector

revealed that the licensee's response to an NOV involving a civil

penalty more adequately addressed the required corrective actions for

the deficiency documented on ACR 91-034.

The inspectors also selected ACR No.92-186 for review of problem

assessment activities. The ACR was written to identify a tripping

condition which occurred while the A Emergency Diesel Generator

(EDG) was undergoing an over-speed trip test. A similar condition had

occurred on a B EDG while it was undergoing post maintenance

overspeed trip testing. In each instance, the same condition, fuel rack

unlatched, was found. The A EDG was operational at the time the

trip occurred, while the B EDG was still in post maintenance test

status.

As a result of the EDG A trip, an investigation team was organized to

determine the cause of the fuel rack unlatched condition. The team

consisted of knowledgeable engineering personnel, an operations

person and a maintenance supervisor and craftsman. Additional

personnel provided special assistance when needed.

The team conducted root causes analysis which included a description

of the event, equipment failure/conditions affecting the event, a

chronological description, and summarized the factors that influenced

human behavior. A list of proposed corrective actions to preclude

recurrence was prepared. Corrective actions for contributing factors

and improvements based on the investigation were recommended.

The team used various causal factors check sheets to assess each

aspect of the event. These check sheets were applicable to any

investigation and contained a group of questions that could be applied

to any situation.

The inspectors concluded that the investigation was thorough and the

method of reaching the solution was acceptable. The recommendation

seemed to fit the findings of the investigating team.

c.

Conclusion

The inspectors concluded that the licensee management generally

performed an adequate root cause analysis for LERs. ACRs and SCRs.

The developed corrective action plans were also consistent with the

identified root causes to ensure implementation of effective corrective

actions. Additionally, the corrective action program monitors

implemented corrective action plans to verify completion of corrective

actions. The inspectors attended the PNSC monthly meeting on

June 17, 1992 to observe the depth of review of overall plant

performance. The meeting was well conducted with a prepared

agenda. The agenda items were presented to the committee members

in a clear and understandable manner, and the committee reviews

were thorough and in depth.

6

Within this area no violations or deviations were identified.

4.

Generic Letter 89-10. Safety-related Motor-Operated Valve Testing and

Surveillance (TI 2515/109)

The inspectors performed a limited review of the licensee's Motor Operated

Valve (MOV) program.

a.

Differential Pressure Testing (DP)

The testing of MOVs, either static or under DP conditions is performed

using VOTES diagnostic equipment. The acceptance criteria is

furnished to the testing personnel by the licensee's Nuclear

Engineering Department (NED). The traces produced by the

diagnostic equipment are screened by on-site personnel to verify the

required thrust is developed and is within the thrust window. The

traces are also reviewed for acceptable motor current, packing load,

and verification that the maximum thrust at torque switch trip (TST) is

below the maximum allowable thrust. Once these items are verified,

the trace data is forwarded to NED for detailed analysis. The

inspectors were advised that if during the NED review a discrepancy is

found, the site is notified and corrective action is initiated.

The inspectors reviewed the test traces with the licensee

representatives for the following valves:

Thrust at

Thrust

Valve ID

Thrust Range

Flow cutoff

at TST

Number

LBS

LBS

LBS

CC-735

8,883 - 12600

833

9359

CC-730

3351 - 12600

3427

5775

CC716B

3351 - 12600

3560

4236

RHR-744B

6669.6 - 126000

4461

9693

RHR-744A

6669.6 - 126000

6020

23,422

SI-870B

8099 - 12600

2552

8571

SI-870A

8099 - 12600

5616

9595

SI-864B

12856 - 21600

Static only

19085

CVC-350

1482 - 7200

Static only

. 2239

FW-V2-6B

38211 - 63000

Static only

44863

FW-V2-6C

38211 - 63000

Static only

38573

FW-V2-6A

38211 - 63000

Static only

43010

No problems were identified with these tests.

7

The inspectors reviewed the status of feedwater MOV FW-V2-6A to

examine the corrective actions taken to improve the operability of the

valve. The licensee had made changes to improve the operation of

the valve in the open direction. The TOLs had been tripping during

the opening stroke of FW-V2-6A. The tripping was determined to be

the result of thermal binding of the valve. Thermal binding occurs

when the valve is closed while at high temperature and allowed to

cool in the closed position which causes the seats to tighten on the

wedge gate disc. Then on the next attempt to open the valve after

cool down, a high thrust is required to unseat the valve. This high

thrust requirement causes the valve actuator motor to stall, causing

the TOLs to trip.

On June 15, 1991, an operability review determinated that thermal

binding was occurring. In January 1992, the licensee performed

calculations Nos. RNP-M/MECH-1398, 1399 and 1400 which

recommended a lighter spring pack to stay within the torque rating of

the actuators based on the postulated accident differential pressures

of 50 psid. The operating procedures were revised to require cycling

of the feedwater valves FW-2V-6A, B and C, during unit cool down.

Lighter spring packs were installed during the June 1992 outage in

the valve actuator of each valve to reduce the thrust at the end of the

close cycle. The lighter spring packs were installed as the result of

the calculated differential pressure across the valves of 50 psid. This

value was based on the postulated assumption that feedwater

regulating valves located down stream of each block valve will close

in seven seconds after a safety injection (SI) signal is received and the

reactor feedwater pump trips and coasts to a stop. The design basis

differential pressure report DP-027FW for the motor operated valves

(MOVs) in the feedwater system for the Robinson Nuclear Plant

acknowledged that if the feedwater regulating valves were in the

manual mode at the time the SI signal was received, the block valve

would see some, "substantial though indeterminate AP." This report

assumed that the flow control valve would close and cause minimum

flow across the block valve, but in any case did mention that the line

pressure is assumed to be 580 psig during accident conditions with

the feedwater regulating valves in the manual position. The

assumption held to in the evaluation is that the feedwater regulating

valves will always be closed first.

8

On June 15, 1992, Feedwater Regulating Valve FCV-478 was given a

close command but did not close sufficiently to reduce the differential

pressure across Block Valve FW-2V-6A. FW-2V-6A torqued out

before completely closing off the flow to Steam Generator A. Work

request WR/JO 92-AJEH2 was written to check the stroke and adjust

the positioner of FCV-478. The inspector inquired about the condition

of FW-V2-6A and why it did not close fully. The reason given was

the discharge pressure of the condensate pump was greater than the

50 psid. The inspector then questioned the licensee concerning the

basis for the assumption that the reactor feedwater pump tripping

would cause the DP across-the block valve to be less than 50 psid.

It appears that an unverified assumption was made by the licensee

that the condensate pump is also tripped when a safety injection

signal is received. The condensate pump trip is a manual action taken

by the operator, and is not initiated by an automatic trip signal.

The H. B. Robinson FSAR Table 15.1.5.2, ACTUATION SIGNALS

AND DELAYS FOR MSIV, SIS AND FEEDWATER SAFETY ACTIONS,

states that the main feedwater regulating valve closure occurs seven

seconds after the SI signal. When the licensee recalculated the

differential across the valve with the condensate pump still operating

the DP was calculated to be 480 psid at closing and 375 psid at

opening. The licensee immediately issued the necessary work

requests to reset the torque switches on these three valves to enable

the actuator to develop the required thrust without tripping the torque

switch before closure is accomplished.

The failure on the part of the licensee to consider the DP across the

three feedwater valves with the condensate pumps operating, and

setting the feedwater block valves to close at a pressure less than

actual is identified as violation 50-261/92-19-01: Inadequate design

control involving unverified assumptions related to D/P for Valves FW

2V-6A,B, and C.

10 CFR50, Appendix B, Criterion III states in part "... design control

measures shall provide for verifying or checking the adequacy of

designs ....

Contrary to the above, on June 15, 1992, Feedwater

Block Valve FW-2V-6A did not fully close due to the differential

pressure across-the valve having been calculated at a lower value than

existed in the system. The differential pressure had been calcualted

to be 50 psid across each of the three feedwater block valves and the

valves had been adjusted for closure at that pressure. Upon inquiry

by the NRC Inspectors, the licensee recalculated the differential

pressure to be 480 psid. The differential pressure was the result of

9

the condensate pump operating, which was assumed to trip upon

receipt of a safety injection signal allowing the valves to close under

the lower diffferential pressure.

b.

Schedule

The licensee was returning the unit to operation after the completion

of a refueling outage. The MOV testing scheduled during the outage

was completed as planned. The licensee differential pressure tested

23 MOVs and static tested 42 MOVs. Other planned maintenance

items such as the installation of VOTES sensors, electrical and

mechanical preventive maintenance, and the replacement of torque

switches was accomplished during the outage as scheduled, with the

exception of 4 torque switch replacements which were delayed due to

parts availability.

c.

Maintenance

The licensee has developed procedure TMM-032, TECHNICAL

SUPPORT MANAGEMENT MANUAL PROCEDURE; MOTOR

OPERATED VALVE PROGRAM, for the purpose of establishing,

implementing, and maintaining an overall program for motor operated

valves. This procedure references various maintenance documents as

guidelines for maintaining MOVS. The inspector reviewed a draft

revision of MMM-003, Appendix A, POST MAINTENANCE TESTING,

which defines the post maintenance testing required at the completion

of various MOV maintenance activities. The control of switch

settings is maintained under procedure CM-1 11, LIMITORQUE LIMIT

SWITCH AND TORQUE SWITCH MAINTENANCE. This appears to be

an adequate procedural control for accomplishing the MOV GL 89-10

program.

d.

Training

The licensee has a group of craftsmen that travel between the nuclear

plants and perform the testing of MOVs during outages. The test

data taken are initially reviewed by the site personnel and later by the

NED. Licensee representatives informed the inspector that some of

-the site instrumentation and control (I&C) personnel had been trained

in the use of the diagnostic equipment, but due to the heavy work

load during the recent outage, they were not involved in the testing

completed this outage. The licensee has scheduled classes for

training in the use and analyzing of the Votes equipment and traces

for selected site personnel. The inspector noted that a MOV training

10

for selected site personnel. The inspector noted that a MOV training

class was in session during this inspection.

5.

Exit Interview

The inspection scope and results were summarized on June 19, 1992, with

those persons indicated in paragraph 1. The inspectors described the areas

inspected and discussed in detail the inspection results listed below.

Proprietary information is not contained in this report. The violation 50

261/92-19-01, Inadequate design control involving unverified assumptions

related to DIP for Valves FW-2V-6A, B, and C, was discussed and no

dissenting comments were received.

Acronyms and Initialisms

ACR

Adverse Condition Report

CAP

Corrective Action Program

DP

Differential Pressure

EDG

Emergency Diesel Generator

GL

Generic Letter

HPIP

Human Performance Investigation Process

I&C

Instrumentation and Control

ILRT

Integrated Leak Rate Test

LER

Licensee Event Report

MOV

Motor Operated Valve

NOV

Notice of Violation

NRC

Nuclear Regulatory Commission

OTDT

Over-temperature delta-temperature

PPM

Parts Per Million

PNSC

Plant Nuclear Safety Committee

psid

Pounds Per Square Inch Differential

RFO

Refueling Outage

RTD

Resistance Temperature Device

SI

Safety Injection

SCR

Significant Condition Report

TS

Technical Specification

TST

Torque Switch Trip

TOL

Thermal Overload Limit

VOTES

Valve Operation Test & Evaluation System

WR/JO

Work Request/Job Order