ML13311B116
| ML13311B116 | |
| Person / Time | |
|---|---|
| Site: | San Onofre |
| Issue date: | 02/09/1981 |
| From: | Joy J SOUTHERN CALIFORNIA EDISON CO. |
| To: | |
| Shared Package | |
| ML13311B118 | List: |
| References | |
| NUDOCS 8102230566 | |
| Download: ML13311B116 (5) | |
Text
AC40 - RA NRC MONTHLY OPERATING REPORT DOCKET NO.
5 I)ATE 29l/81 COMPLETED BY
,IJM
.1Y TELEPHONE -- (714)492-7700 OPERATING STATUS
- 1. Unit Name:
SAN ONOFRE NUCLEAR GENERATTNG STATT N-UNIT 1
- 2. Reporting Period:
January 1, 1981 through January 31, 1981
- 3. Licensed Thermal Power (MWt):
1 347
- 4. Nameplate Rating (Gross MWe):
456
- 5. Design Electrical Rating (Net MWe):
436
- 6. Maximum Dependable Capacity (Gross MWe):
456
- 7. Maximum Dependable Capacity (Net MWe):
436
- 8. If Changes Occur in Capacity Ratings (Items Number 3 Through 7) Since Last Report, Give Reasons:
N.A
- 9. Power Level To Which Restricted, If Any (Net MWe):
N.A.
- 10. Reasons For Restrictions, If Any:
N.A.
This Month Yr.-to-Date Cumulative
- 11. Hours In Reporting Period 744 744 119,528
- 12. Number Of Hours Reactor Was Critical 0
0 84,611.4
- 13. Reactor Reserve Shutdown Hours 0
0 0
- 14. Hours Generator On-Line 0
0 81,114.1
- 15. Unit Reserve Shutdown Hours 0
.0 0
- 16. Gross Thermal Energy Generated (MWH) 0 0
1 04, 084,261
- 17. Gross Electrical Energy Generated (MWH) 0 0
35.526,434
- 18. Net Electrical Energy Generated (MWH) 0 0
33,664,042
- 19. Unit Service Factor 0
0 67.9
- 20. Unit Availability Factor 0
0 67.9
- 21. Unit Capacity Factor (Using MDC Net) 0 0
68.8
- 22. Unit Capacity Factor (Using DER Net) 0 0
68.8
- 23. Unit Forced Outage Rate 100 100 14.5
- 24. Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
Steam Generator Repair In Progress
- 25. If Shut Down At End Of Report Period, Estimated Date of Startup:
April 15, 1981
- 26. Units In Test Status (Prior to Commercial Operation):
N A Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION 81022 30 &6 SCE Psso(t) 371 NEW 8/78
AVERAGE DAILY UNIT POWER LEVEL DOCKETNO. 5O-206 UNIT SONGS 1 DATE 2/9/81 COMPLETED BY J M-JOY TELEPHONE (714)492-7700 MONTH January 1981 DAY AVERAGE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 0
10 2
0 18 0
3 0
19 0
4 0
20 0
5 0
21 0
6
-022 0
7 0
23 0
8 0
24 n
9 0
25 0
10 0
26 0
I1 0
27 0
12 0
8 0
13 0
29 0
14 0
-30 0
15 0
31 0
16 371ANEW_8/78 PSSO (1) 371 N EW 8/78
UNIT SHUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-206 UNIT NAME SONGS-1 DATE 2/09/81 COMPLETED BY J. M. JOY REPORT MONTH January, 1981 TELEPHONE (714) 492-7700 Licensee Cause & Corrective No.
Date Event Action to Report Prevent Recurrence 55 80-07-12 F
4153 B
1 80-014 CC HTEXCH STEAM GENERATOR TUBE REPAIR F: Forced Reason:
Method:
Exhibit F Instructions S: Scheduled A-Equipment Failure (Explain)
I-Manual for Preparation ofData B-Maintenance or Test 2-Manual Scram.
Entrv Sheets for Licensee C-Refieling 3-Automatic Scram.
Eveni Report ([ER) File (NURI:C D-Regulatory Restriction 4-Other (Explain) 0161 F-Operator Training & License Examination F-Administrative G-Operational Error (Explain)
Exhibit H-Sime Source 4--Ohei (Explain)
PSSOElv o
371 NEW r/78
SUMMARY
OF OPERATING EXPERIENCE FOR THE MONTH DOCKET NO.50-206 UNIT SONGS-1 DATE 4/09/81 COMPLETED BY J.M. JOY TELEPHONE
.(714) 492-7700 The unit remained in cold shutdown for the entire month for steam generator tube repair.
Psso(1) 371 NEW 8/78
REFUELING INFORMATION DOCKET N050-206 UNIT SONGS-1 DATE 2/09/81 COMPLETED BY J.M.JOY TELEPHONE (714) 492-7700
- 1. Scheduled date for next refueling shutdown.
Not yet determined.
- 2. Scheduled date for restart following refueling.
April 15, 1981
- 3. Will refueling or resumption of operation thereafter require a Technical Specification change or other license amendment?
Yes What will these be?
Proposed Change No. 88 to POL DPR-13, Appendix A, Technical Specification 3.5.2, Control Rod.Insertion Limits.
- 4. Scheduled date for submitting proposed licensing action and supporting information.
February 8, 1981
- 5. Important licensing considerations associated with refueling, e.g.
new or different fuel design or supplier, unreviewed design or performance analysis methods, significant changes in fuel design, new operating procedures.
None
- 6. The number of fuel assemblies.
a) In the core 157 b) In the spent fuel storage pool. 94
- 7. Licensed spent fuel storage capacity.
216 Intended change in spent fuel storage capacity.
None
- 8. Projected date of last refueling that can be discharged to spent fuel storage pool assuming present capacity.
April 1983 Psso(l) 371 NEW 8/78