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MONTHYEARML12073A3542012-03-0909 March 2012 30-Day Report Pursuant to 10 CFR 50.46, Changes to or Errors in an Evaluation Model Project stage: Request ML12300A2012012-10-26026 October 2012 NRC Request for Additional Information on Errors Reported Per 10 CFR 50.46, ME9119 Project stage: RAI ML12348A0552012-12-0707 December 2012 Response to RAI Regarding 10 CFR 50.46 Notification of Change in Peak Cladding Temperature for Large Break Loss of Coolant Accident Analysis Project stage: Request ML13060A4172013-03-0101 March 2013 NRC Request for Additional Information on Errors Reported Per 10 CFR 50.46 (TACs ME9119, ME9120, ME9121) Project stage: RAI ML13102A0332013-04-0404 April 2013 Response to NRC RAI Regarding 10 CFR 50.46 Notification of Change in Peak Cladding Temperature for Large Break Loss of Coolant Accident Analysis Project stage: Request ML13237A0022013-08-23023 August 2013 NRR E-mail Capture - Oconee Nuclear Station, Units 1, 2, and 3, NRC Request for Additional Information on Errors Reported Per 10 CFR 50.46 (TACs ME9119, ME9120, ME9121) Project stage: RAI ML13309A4462013-09-12012 September 2013 E-mail from R.Guzman to T.Byrne Request for Additional Information on Errors Reported Per 10 CFR 50.46 (TACs ME9119, ME9120, ME9121) Project stage: RAI RA-13-1002, Response to Supplemental NRC RAI Regarding 10 CFR 50.46 Notification of Change in Peak Cladding Temperature for Large Break Loss of Coolant Accident2013-10-10010 October 2013 Response to Supplemental NRC RAI Regarding 10 CFR 50.46 Notification of Change in Peak Cladding Temperature for Large Break Loss of Coolant Accident Project stage: Request ML13338A3452013-12-0505 December 2013 Closure Evaluation for Report Concerning Significant Emergency Core Cooling System Evaluation Model Errors/Changes Project stage: Other 2013-12-05
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Category:E-Mail
MONTHYEARML23349A0272023-12-15015 December 2023 Acceptance of Requested Licensing Action License Amendment Request to Revise Technical Specification 5.5.2 ML23284A3322023-10-11011 October 2023 Request for Additional Information Alternative Request (RA-22-0174) (L-2022-LLR-0060) ML23270B8362023-09-26026 September 2023 Code Case N-752 Audit September 26, 2023, E-mail Providing Additional Information Regarding the Use of Owner'S Requirements and Engineering Judgment in Lieu of Code and Standards ML23267A0032023-09-21021 September 2023 RP Inspection Document Request ML23269A0412023-08-22022 August 2023 Code Case N-752 Audit; August 22, 2023, E-mail Providing Additional Information Regarding Design and Quality Program Requirements ML23172A0132023-06-20020 June 2023 Duke Fleet - Correction to June 2, 2023, Request for Additional Information Proposed License Amendment Request to Revise Restrictive Surveillance Requirement Frequencies ML23153A1892023-06-0202 June 2023 Duke Fleet - Request for Additional Information Proposed License Amendment Request to Revise Restrictive Surveillance Requirement Frequencies ML23151A3482023-05-30030 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML23144A0862023-05-24024 May 2023 Acceptance of Requested Licensing Action Proposed Relief Request (RA-23-0018) to Use ASME Code Case 853 ML23142A2732023-05-22022 May 2023 Duke Fleet - Request for Additional Information Proposed Alternative for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) ML23125A1452023-05-0505 May 2023 Change in Estimated Review Schedule and Level of Effort for Proposed Alternative to Use Code Case N-752 ML23124A1212023-05-0404 May 2023 Acceptance of Requested Licensing Action Duke Fleet Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) ML23095A0052023-04-0404 April 2023 002 Radiation Safety Baseline Inspection Information Request ML23086C0362023-03-27027 March 2023 Request for Additional Information Steam Generator Tube Inspection Report (03R31) ML23073A2282023-03-13013 March 2023 Duke Fleet- Adoption of TSTF-554, Revision 1, Revise Reactor Coolant Leakage Requirements - Acceptance Review ML23058A0562023-02-27027 February 2023 Acceptance of Amendment to Revise Surveillance Frequencies for RCS Pressure Isolation Valve Operational Leakage Testing and Reactor Trip System Instrumentation ML23048A1512023-02-16016 February 2023 Acceptance Review - Proposed Alternative for Steam Generator Welds (L-2023-LLR-0003) ML23038A1832023-02-0707 February 2023 Request for Additional Information Alternative Request (RA-22-0174) to Use ASME Code Case N-752 ML23031A1552023-01-17017 January 2023 1/17/2023 Email from John Moses, Deputy Director, Division of Rulemaking, Environmental, and Financial Support, to Diane Curran, Counsel to Beyond Nuclear and the Sierra Club, Request for Extension of Scoping Comment Period for Oconee EIS ML22294A0812022-10-21021 October 2022 Nrc/Duke Steam Generator Inspection Call for November 8, 2022 NRC-2100-2022, EN 55999 Valcor Coil Shell Assemblies Final Notification (004)2022-09-12012 September 2022 EN 55999 Valcor Coil Shell Assemblies Final Notification (004) ML22251A2902022-09-0808 September 2022 Request for Additional Information Additional Mode Change Limitations Applicable to the Adoption of Technical Specifications Tasks Force Traveler (TSTF) No. 359, Revision 9 ML22235A6552022-08-23023 August 2022 Acceptance of Requested Licensing Action Proposed Alternative to Use ASME Code Case N-752 NRC 2110-2022, EN 55999 - Valcor Engineering Corporation (009)2022-07-18018 July 2022 EN 55999 - Valcor Engineering Corporation (009) ML22234A1262022-07-0808 July 2022 Email from NRC to Duke - Feedback on Trp 76 RAI Responses - July 8, 2022 ML22234A1272022-06-14014 June 2022 Email from NRC to Duke - Feedback on Trp 76 RAI Responses - June 14, 2022 ML22154A2142022-06-0101 June 2022 Email from NRC (Angela Wu) to Duke (Paul Guill) - Oconee SLRA - 2nd Round RAI B2.1.7-4b ML22157A0012022-06-0101 June 2022 Email from NRC (Angela Wu) to Duke (Paul Guill) - Oconee SLRA - Additional NRC Comments on RAI 4.6.1-1a ML22124A2052022-05-0404 May 2022 Summary of May 4, 2022, Clarification Call with Duke Energy Carolinas, LLC, Application to Revise TS 3.7.7, Low Pressure Service Water (LPSW) System ML22124A1612022-05-0303 May 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - 2nd Round RAI B2.1.7-4a ML22122A0192022-04-28028 April 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - 2nd Round RAI B2.1.9-2a ML22122A1322022-04-27027 April 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - 2nd Round Requests for Additional Information (FE 3.5.2.2.2.6 - Irradiation Structural) ML22115A1412022-04-25025 April 2022 NRR E-mail Capture - Duke Common EOF Relocation - Request for Addition Information ML22130A0112022-04-25025 April 2022 Email: Oconee SLRA - RAI 4.6.1-1a - NRC Staff Comments ML22112A1892022-04-22022 April 2022 Acceptance Review for Additional Mode Change Limitations Applicable to the Adoption of TSTF- 359, Revision 9 ML22112A0072022-04-20020 April 2022 Email from Marieliz Johnson (NRC) to Steve Snider (Duke) - Oconee SLRA - Request for Confirmation of Information 3.5.2.2.2.6-L ML22113A0082022-04-20020 April 2022 Email from Marieliz Johnson (NRC) to Steve Snider (Duke) - Oconee SLRA - Request for Additional Information 3.1.2-1 ML22088A0452022-03-28028 March 2022 Radiation Safety Baseline Inspection Initial Information Request Inspection Report 2022002 ML22081A0052022-03-21021 March 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - 2nd Round RAI B4.1-3 ML22080A0792022-03-16016 March 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - Requests for Additional Information - Set 4 (2nd Round Rais) ML22075A2032022-03-11011 March 2022 Email from Duke to NRC - Follow-Up Items from March 7, 2022 Public Meeting ML22074A0022022-03-11011 March 2022 Email from Duke to NRC - Follow-up Item from March 7, 2022 Public Meeting - SSW Tendon AMP ML22069A0022022-03-0808 March 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - Requests for Confirmation of Information - Set 4 ML22063A4502022-03-0404 March 2022 Request for Additional Information Application to Revise TS 3.7.7, Low Pressure Service Water (LPSW) System, to Extend the Completion Time for One Required Inoperable LPSW Pump ML22063A1152022-02-23023 February 2022 Email from Duke to NRC - Follow Up Item from February 17, 2022 Public Meeting ML22038A1572022-02-0707 February 2022 NRR E-mail Capture - Duke Energy Fleet - Acceptance of License Amendment Request Regarding Adoption of TSTF-541, Revision 2 ML22035A1892022-01-31031 January 2022 Email from NRC (Angela Wu) to Duke (Paul Guill) - Oconee SLRA - Request for Public Meeting ML22018A0272022-01-18018 January 2022 2022 All RFI Responses - Exercise and Program Inspections - Revl ML22019A1032022-01-18018 January 2022 Email from Angela Wu (NRC) to Steve Snider (Duke) - Oconee SLRA - Requests for Additional Information - Set 3 ML22012A0432022-01-11011 January 2022 SLRA - Requests for Additional Information - Set 2 2023-09-26
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From: Boska, John Sent: Friday, March 01, 2013 2:18 PM To: Alter, Kent R Cc: Guill, Paul F
Subject:
Oconee Nuclear Station, Units 1, 2, and 3, NRC Request For Additional Information on Errors Reported per 10 CFR 50.46 (TACs ME9119, ME9120, ME9121)
On March 9, 2012, Duke Energy Carolinas, LLC (Duke), submitted a report on emergency core cooling system (ECCS) analysis errors, ADAMS Accession No. ML12073A354, for Oconee Nuclear Station, Units 1, 2, and 3. On October 26, 2012, the Nuclear Regulatory Commission (NRC) staff issued a request for additional information (RAI), ML12300A201. On December 7, 2012, Duke replied to the RAI, ML12348A055. The NRC staff is reviewing the submittal and has determined that additional information is needed to complete its review. The specific questions are found below. Please provide a response to this RAI within 30 days of the date of this email.
REQUEST FOR ADDITIONAL INFORMATION:
- 1. For the analyses completed pertaining to the ECCS bypass error for the lowered loop design, a 2.506-ft peak power location was used, and the analyses for the ECCS bypass error for the raised loop design used a 9.536-ft peak power location. In the December 7, 2012, supplemental letter, the effects of the end-of-bypass timing error are expressed in terms of liquid inventory available to reach the lower plenum and initiate a bottom-up core reflood. The effects of an adiabatic heatup, which is terminated by the core reflood, are also discussed. In consideration of these phenomena, it would appear that a higher elevation in the core would be a more limiting location to evaluate the effects of an error associated with end-of-bypass timing.
Provide information to demonstrate that the bottom-peaked power shape being used for the lowered loop design is conservative and/or appropriate.
- 2. After evaluating a 177 fuel assembly (FA) lowered loop (LL) plant with column weldments modeled for a 205 FA plant, details of the column weldments for a 177 FA plant were developed. The model for column weldments of a 177 FA plant were then used for the analyses of a raised loop (RL) plant. Two 177 FA raised loop cases showed that the newly developed column weldments increased PCT for an unruptured fuel segment by 3 degrees Fahrenheit.
It was also reported that the column weldments in a lowered loop plant increased PCT by 11.5 degrees Fahrenheit for an unruptured fuel segment and 26.2 degrees Fahrenheit for a ruptured fuel segment. This result was bounded by generically estimating the effect of column weldments to be an increase in PCT of 80 degrees Fahrenheit.
Column weldments in a raised loop plant increased PCT by 8.9 degrees Fahrenheit for an unruptured segment, which is less than the effect seen in the lowered loop design.
- a. Provide justification to show that analyzing column weldments modeled for a 177 FA plant has an effect on PCT of the same magnitude in a lowered loop plant as in a raised loop plant.
- b. Describe the nodalization for the column weldments used in RELAP5 analyses.
- c. Provide simplified drawings to compare the column weldment design for a 205 fuel assembly plant to the column weldments for the 177 fuel assembly plant.
John Boska Oconee Project Manager, NRR/DORL U.S. Nuclear Regulatory Commission 301-415-2901 email: john.boska@nrc.gov