ML11356A029
| ML11356A029 | |
| Person / Time | |
|---|---|
| Site: | Indian Point |
| Issue date: | 12/22/2011 |
| From: | Entergy Nuclear Operations |
| To: | Atomic Safety and Licensing Board Panel |
| SECY RAS | |
| Shared Package | |
| ML11356A026 | List: |
| References | |
| RAS 21601, 50-247-LR, 50-286-LR, ASLBP 07-858-03-LR-BD01 | |
| Download: ML11356A029 (3) | |
Text
Entergy CONDITION REPORT I CR-IPJ-2006-02270 Originator: Lizzo,Nicholas
)riginator Group: Operations Watch Mgmt Supervisor Name: Cramer,Thomas A Discovered Date: 07/23/2006 04:49 Condition
Description:
Originator Phone: 8277 Operability Required: N Reportability Required: N Initiated Date: 07/23/2006 04:58 The line downstream of the 1104 valves ("A" reheaters) to 36 FWH shell side is leaking approximately 112 gpm. WRT IP3-06-18192. Rapid Response activated.
Immediate Action
Description:
SM notified - rapid response activated Suggested Action
Description:
Repair.
EQUIPMENT:
Tag Name 1104 REFERENCE ITEMS:
Type Code
- LEVEL OF DEFENSE KEYWORDS TEAM3C WON Tag Suff"IX Name Component Code Process System Code HD Description Observation leak tt IP3-06-18192 TRENDING (For Reference Purposes Only):
Trend Type REPORT WEIGHT EM KEYWORDS IPEC00025699 Trend Code 4
MAMM KW-LEAK.S-WATER EFll RIV000029 Submitted: December 22, 2011
Entergy I CORRECTIVE ACTION CANumber:
Group Assigned By: CRG/CARB/OSRC Assigned To: P&C Eng Codes Mgmt Subassigned To : P&C Eng Codes Staff Originated By: Harrison,Christine B Performed 'By: Azevedo,Nelson F Subperformed By: Hartjen,Harry G Approved By:
Closed By: Azevedo,Nelson F Current Due Date: 08/16/2006 CA Type: DISP - CA Plant Constraint: #NONE CA
Description:
Harrison, Christine B Azevedo,Nelson F Hartjen,Harry G 7/25/2006 11:27:08 8115/2006 14:22:53 8/10/2006 09:27:02 8/15/2006 14:22:53 Initial Due Date: 08/16/2006 Please review and assign further corrective actions as required.
Response
l CR-IP3-2006-02270 Name UTthickness ~asurements were taken around the leaking area on this pipe (UT Report 06UTI71 ). The thinned area was found to be localized on one side.ofthe pipe which is downsstream of a tee. A pipe clamp (Team Inc.) was installed over the leak and thinned area under work order IP3-06-18192. Leak repair was successful and the leak has stopped. CA 00002 has been issued to review the F AC program and detennine if additional inspections.are warrented as a result of this leak.
"'*,bresponse :
Issued CA#2 Closure Comments:
IPEC00025700
Entergy I CANumber:
2 Assigned By: P&C Eng Codes Staff Assigned To: P&C Eng Codes Staff Subassigned To :
Originated By: Hartjen,Harry G Performed By: Hartjen,Harry G Subperformed By:
Approved By:
Closed By: Hartjen,Harry G Current Due Date: I 0/3I/2006 CA Type: ACTION Plant Constraint: #NONE CA
Description:
CORRECTIVE ACTION Group
- I Hartjen,Harry G Hartjen,Harry G
-8110/2006 09:24:00 I 0/30/2006 II :28:34 I 0/30/2006 II :28:34 Initial Due Date: I 0/3112006 I
CR-IPJ-2006-02270 Name Review both Unit 2 and Unit 3 F AC Programs and determine if similar locations to this leak have been inspected for wall thinning. Also determine if and when additional inspections are required to determine if wall thinning is occuring at these similar locations. If additional inspections are required, incorporate inspections into work week schedule, or F AC Program outage scopes.
Response
A review of both Unit 2 and Unit 3 F AC programs was performed to determine if similar locations to the current Reheater Drain line leak have been inspected for wall thinning and determine if and when additional inspections are required to determine if wall thinning is occurring at these similar locations.
Review of the Unit 2 F AC inspection history found that all similar locations have been recently inspected or replaced. No additional inspections are recommended for Unit 2 at this time.
Review of the Unit 3 F AC inspection history found that some similar locations do not have recent inspections and should be inspected. A total of9 additional inspections were identified.
Details of this review, along with the recommended additional inspections are attached.
No on-line exams are recommended due to the high temperature (385 degrees F) of these components, and the congestion of piping in these areas. Therefore the 9 additional inspections are to be performed during the 3RI4 refuel outage.
CA 3 is issued to generate work orders and 3R 14 scope add forms fo~ these inspections.
Subresponse :
Closure Comments:
Attachments:
Resp Description Review ofF AC Inspections due to leak in U3 RHO IPEC00025701