ML111661466

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Forwards Monthly Operating Rept for Jan 1981
ML111661466
Person / Time
Site: Kewaunee Dominion icon.png
Issue date: 02/06/1981
From: Mathews E
Wisconsin Public Service Corp
To:
NRC OFFICE OF MANAGEMENT AND PROGRAM ANALYSIS (MPA)
Shared Package
ML111661467 List:
References
CON-NRC-81-21 NUDOCS 8102170083
Download: ML111661466 (6)


Text

REGULATURY INFORMATION DISTRIBUTION SYSTEM (RIDS)

ACCESSION NBR:8102170083 DUC.DATE: 81/02/06 NOTARWD: NO DOCKET #

FACILa50-305 Kewaunee Nuclear Power Plant, Wisconsin Public Servic 05000305 AUTH.NAME AUTHUR AFFILIATION MATHEWSE.R. Wisconsin Public Service Corp.

RECIP.NAME RECIPIENT AFFILIATION Office of Management and Program Analysis

SUBJECT:

Forwards monthly operating rept for Jan 1981.

DISTRIBUTION CODE: A008S COPIES RECEIVED:LTR .L ENCL S  :

TITLE: Annual, Semi-Annual & Monthly Operating Reports (OL Stage)

NOTES:I&E:3 copies all material, 05000305 RECIPIENT COPIES RECIPIENT COPIES 10 CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL ACTION: VARGA,S. 04 7 7 INTERNAL: D/DIRtHUM FACO7 1 DIRDIV OF LIC 1 1 I&E. 06 1 2 MPA 13 2 2 NRC PDR 02 1 BR09 1 1 OR ASSESS BR 10 1 1 IL 01 1 EG 1

EXTERNAL: ACRS 11 1 BROOKHAVEN 12 1 1 1 1 05 1 1 LPOR 03 NSIC C,

,7A(

TOTAL NUMBER OF COPIES REUUIRED: LTTR ENCL .21

NRC-81-21 WISCONSIN PUBLIC SERVICE CORPORATION

0. Box C'1200, Gren Bay, Wisconsin 54305 February 6, 1981 Director Office of Management Information &

Program Control U. S. Nuclear Regulatory Commission Washington, D. C. 20555 Gentlemen:

Docket 50-305 Operating License DPR-43 Kewaunee Nuclear Power Plant Monthly Operating Report The narrative "Summary of Operating Experience" and completed forms covering plant and component availability for the Kewaunee Nuclear Power Plant for January, 1981, are enclosed.

Very truly yours, E. R. Mathews, Vice President Power Supply & Engineering snf Enc.

cc - Mr. J. G. Keppler, Reg Dir US NRC - Region III Mr. Ted Cintula US NRC - Maryland National Bank Bldg Washington, D. C. 20555 Mr. Robert Nelson, NRC Resident Inspector '900 RR #1, Box 999, Kewaunee, WI 54216

DOCKET 50-305 KENAUNEE NUCLEAR POWEE PLANT SUMBARY OF OPERATING EXPERIENCE JANUARY, 1981 OPERATIONS: on January 21, speed control was lost to Beater Drain Pump 1B. Unit load was reduced to 90% for repairs. The unit was returned to full load on January 21.

MAINTENANCE: A sticking relay in a service water strainer control circuit was replaced.

Replaced a temperature controller for a control room air conditioning unit.

Replaced a defective summer for overpover setpoint calculation.

Replaced a seal on a waste gas compressor.

Replaced a check valve in an air line for diesel generator air start motors.

Replaced a cracked motor housing on a component cooling valve.

10

  1. -A VE R AGE Z 0A I LY UNIT PO*R LEEiEV EL DOCKET NO- 50-305 UNIT- KEWAUNEE COMPLETED BY- G. H.,RUITER TELEPHONE- 414-388-2560 1225 REPORT MONTH JANUARY, 1981 AVERAGE DAILY DAY POWER LEVEL (iWE-NET) 522 2 518 3 518 4 514 5 517 6 514 7 518 8 514 9 514 10 518 11 514 12 518 13 518 14 518 15 518 16 522 17 518 18 518 19 521 20 518 21 509 22 518 23 522 24 518 25 518 26 517 27 522 28 518 29 514 30 518 31 517

OPE B ATING DATA REPORT DOCKET SO- 50-305 COMPLETED B- G. B. BUITER OPE RATING STATUS TELEPHONE- 414-388-2560 1225 1 UNIT NAME KEWAUNEE 2 BEPORTING PERIOD JANUARY, 1981

  • NOTES Unrestricted unit operations for *
  • the entire reporting period.
  • 3 LICENSED THEBMAL POWER (MIT) 1650
  • 4 NAMEPLATE RATING (GROSS MNE) 560 *
  • 5 DESIGN ELECTBICAL BATING (NET MWE) 535 *
  • i 6 MAIIMUM DEPENDABLE CAPACITY (GBOSS MWE) 545 *
  • 7 MAXIMUM DEPENDABLE CAPACITY (NET HWE) 522 8 IF CHANGES OCCUR IN CAPACITY RATINGS (ITEMS DUBBER 3 THROUGH 7) SINCE LAST REPORT, GIVE REASONS None 0

9 POWER LEVEL TO WHICH RESTRICTED, IF ANY (NET WE) None 10 REASONS FOR RESTRICTIONS, IF AN!

9 THIS MONTH YR-TO-DATE CUMULATIVE 11 HOURS IN REPORTING PERIOD 744 744 58129 6 12 NUMBER OF HOURS REACTOR WAS CRITICAL 744.0 744.0 49066.6 61 13 REACTOR RESERVE SHUTDOWN HOURS 0.0 0.0 2330.5 14 HOURS GENERATOR ON-LINE 744.0 744.0 47952.9 is 15 UNIT RESERVE SUTDOWN HOURS 0.0 0.0 10.0 16 GROSS THERMAL ENERGY GENERATED (MIS) 1223429 1223429 73910653 17 GBOSS ELECTRICAL ENERGY GENERATED (MWH) 402700 402700 24396900 18 NET ELECTRICAL ENERGY GENEBATED (MW8) 385002 385002 23215972 19 UNIT SERVICE FACTCS 100.0 100.0 82.5 20 UNIT AVAILABILITY FACTOR 100.0 100.0 82.5 0 21 UNIT CAPACITY FACTOR (USING MDC NET) 99.1 99.1 76.2 22 UNIT CAPACITY FACTOR (USING DER NET) 96.7 96.7 74.7 23 UNIT FORCED OUTAGE RATE 0.0 0.0 5.4 0 24 SHUTDOWNS SCHEDULED OVER NEXT 6 MONTHS (TYPE, DATE, AND DURATION OF EACH)

Befueling shutdown of 6-veek duration scheduled to start April 18, 1981.

25 IF SHUT DOWN AT END OF REPORT PERIOD, ESTIMATED DATE OF STARTUP - N/A

U NIT SRUTD 0 W NS AND P 0 E B ED U CTI 0 NS DOCKET NO: 50-305 UNIT NAME: Kevaunee DATE: January 2, 1981 COMPLETED BY: G. N.Raiter TELEPHONE: 414-388-2560 x225 a

REPORT HORTH - JANUARY, 1981 0

I NO. I DATE ITYPE iDURATIOUIREASONIMETHODI LEE N5BER ISIS I COMPONENT I COMM ENTS

  • ' II I I I I I -4 No shutdowns during the month of JANUARY.
  • I
  • I
  • I 0
  • I 0
  • I

I S SI SI S

0 SI SI S

S SI S I TYPE REASON METHOD SYSTEM 9 COMPONENT CODES 0 F: Forced A-Equipment Failure (Explain) I-Manual From HUREG-0161 S: Scheduled B-Maintenance or Test 2-Manual Scram 0 C-Refueling 3-Automatic Scram D-Regulatory Restriction 4-Continuations E-Operator Training G License Examination 5-Load Reductions 0 F-Administrative 9-0ther G-Operational Error (Explain)

H-0ther (Explain)

I