ML101190441

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E-Mail from Khanna to Khanna, Crystal River Information
ML101190441
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 10/08/2009
From: Meena Khanna
NRC/NRR/DE/EMCB
To: Meena Khanna
Office of Nuclear Reactor Regulation
References
FOIA/PA-2010-0116
Download: ML101190441 (3)


Text

Orf, Tracy From:

Khanna, Meena., &1L-Sent:

Thursday, October 08, 2009 11:36 PM To:

Khanna, Meena

Subject:

FW: crystal river information....

From: Chan., Terence Sent: Thursday, October 08, 2009 12:01 PM To: Khanna, Meena; Manoly, Kamal Cc: Nove, Carol; Rezai, All; Naujock, Don; Lubinski, John; Evans, Michele; Sullivan, Ted; Hardies, Robert; Karwoski, Kenneth

Subject:

RE: crystal river information....

Meena, Kamal, If you need NDE support, please let us know. Do you know how the licensee determined the crack to:be 360 degrees, full height?

Terence

-From:

Holmnber, Mel Sent: Thursday, Octob&r 08, 2009 9:40 AM To: Billk,.Tom; Bozga, John; Hills, David; Jones, Donald; Meghani, Vijay; Neurauter, James; Sanchez Santiago, Elba; Shai~kh, Atif,ý Cc: Mitchell,Matthew; Chan, Terence; Gavula, James; Hiser, Allen; Benson, Michael; Modes, Mi Gray, Harold
  • *ubifa.&*

ii Crvstalrv' vr information....mpio (b)(5)

Exemption 5 From: Krsek, Robert Sent:'Thursday, October 08, 2009 8:34 AM To: Holmberg, Mel

Subject:

crystal river information....

they made an event report today....

From Monday:

Crystal.River - Crack on Exterior Containment Wall Picture 032.ip-q Hydro-demolition of the RB opening was restarted on Friday morning. Licensee reports hydro-demolition is nearing the liner plate. Licensee is investigating a vertical crack (1/2",wide, about 18" deep) found in the area of hydro-demolitionthat extends outsidelthe area being worked as evidenced by water leaking through the.

crack and coming out an area that isoutsiide the hydro-demolition.Work area. A root cause investigation is in progress. Sargent and Lundy is involved with the investigation and.corrective actions. This issue will be turned over to theSteam Generator Replacement (SGR) inspection team (led by R.Chou) who will be on'-site today.

(Contin'ue t0o follow. bass to0Containment TRG and Structural TRG Lead, Goutam Baqchi: assigned to Dave Garmon)

From Tuesday:

Information in this record was deleted in ccr wtb.the Freedom of Infotmaton Act.

Exen~ons.=

1.) Crystal River.- Crack on Exterior Containment Wall (10/5) - Update (same picture as yesterday's summary []Picture 032Ji )1 The plant is in-mode 6, admin Yellow risk. Head is removed and level is approximately 134.5 feet (6" below RV flange) and 101F. Fuel in vessel With time to boil at 16 minutes. The equipment hatch is closed. Repairs were completed on the NI plate seals. Cavity fill schedule to start tonight at 22:00. Plant risk will remain Yellow until the refueling cavity is filled.

Hydro-demolition for the: containment opening continues. Licensee will perform a modification to support outside lift systemm as'a result of the crack identified in concrete, A root cause investigation is in progress.

Sargent and Lundy, is involved with the investigation and corrective actions, as well as operability and functionality determinations.

The licensee believes that the crack in the concrete on the containment exists all the way around the containment and all the way up and down (360 degrees, full height of containment). This is per site VP discussion with Region II. Crack was found while making an approximately 25 ft X 25ft concrete cut for the Steam Generator Replacement project. All indications are that theeliner is still intact, and there are no indications of liner problems. Crack is about 1/2 inch wide and.10 inches in from outside edge of concrete -

running around the containment - located just at the layer of horizontal tendons. Licensee is assessing and evaluating implications (polar crane support, S/G lift devices-support, as well as operability of containrment)i.

NOTE: License Renewal Application received by the NRC on December 18, 2008 for Crystal River <- click hyper-link to view the status of this application process.

The licensee was contacted by the State of Florida DEP Coordinator and asked whether they were in an unusual event due to contaminated water leaking from a crack in containment. The licensee corrected the misinformation and May contact the local press to inform them of the crack issue to preclude any further misunderstandings. (Pass update to Structural TRG Lead (Goutam: Baqchi) and Containment TRG Lead (Brian Lee). Pass to.License Renewal Points of Contact (Samson Lee, Jerry Dozier and James Medoff) and to OPA (Scott Burnell):. Assioned to Bob Bernardo).

This item has also been screened in as an Issue for Resolution (IFR), IOEB contact: Bob Bernardo.

2

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