|
---|
Category:Inspection Report Correspondence
MONTHYEARML16336A1062016-12-0101 December 2016 Notification of Conduct of a Triennial Fire Protection Baseline Inspection ML0919801252009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - Tdb ML0919801262009-06-17017 June 2009 10/27/2008 Oyster Creek License Renewal Commitments Inspection, Entrance Meeting ML0919801272009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - TBD ML0919801282009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - TBD ML0919801292009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - TBD ML0919801302009-06-17017 June 2009 12/03/2008 Oyster Creek License Renewal Commitments Inspection Exit Meeting ML0919802342009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - TBD ML0919802332009-06-17017 June 2009 License Renewal Commitments Inspection, Exit Meeting - TBD ML0914903592009-05-0606 May 2009 Fatigue Monitoring Program ML0914903602009-05-0606 May 2009 Feeder for Oyster Creek ML0914903612009-05-0606 May 2009 Results of Detailed Review; Water Chemistry Management Program ML0712400082007-05-0303 May 2007 Drywell Trench Photographs During 4/29/07 Maintenance Outage IR 05000219/20060092006-11-0606 November 2006 (SGI) IR 05000219-06-009 on 10/02/06-10/05/06 for Oyster Creek Nuclear Generating Station; Physical Protection IR 05000219/20060042006-10-24024 October 2006 IR 05000219-06-004, on 07/01/2006 - 09/30/2006, Oyster Creek, Fire Protection, Maintenance Effectiveness, and Surveillance Testing IR 05000219/20060062006-06-20020 June 2006 IR 05000219-06-006, on 04/24/2006 - 05/19/2006, Oyster Creek; Biennial Baseline Inspection of the Identification and Resolution of Problems IR 05000219/20050112006-01-0909 January 2006 EA 05-199 Oyster Creek Generating Station -Final Significance Determination for a White Finding and Notice of Violation (NRC Event Followup Inspection Report No. 05000219/2005011) IR 05000219/20040032004-11-0202 November 2004 EA 04-142, Oyster Creek Generating Station - Final Significance Determination for a Green Finding (NRC Inspection Report 05000219-04-003) ML0227701532002-10-0404 October 2002 Notification of Conduct of a Triennial Fire Protection Baseline Inspection IR 05000219/20020052002-05-28028 May 2002 IR 05000219-02-05; on 03/31-05/11/2002; Amergen Energy Company, LLC; Oyster Creek Generating Station; Integrated Report. No Violations Identified IR 05000219/20010132002-03-11011 March 2002 IR 05000219/2001-013, on 12/31/01-02/09/02, Amergen, Oyster Creek Generating Station, Equipment Alignment, Event Follow Up. Two non-cited Violations Noted IR 05000219/20010102002-01-17017 January 2002 IR 05000219/2001-010, Oyster Creek Generating Station, Inspection on 11/11/2001 - 12/30/01 Related to Emergent Work. No Violations Noted IR 05000219/20010052001-06-11011 June 2001 NRC Inspection Report 05000219/2001005 ML0631204891966-04-15015 April 1966 IR 05000219-66-001, on 03/22-23/1966, Oyster Creek, Construction Inspection Report Including Drywell Testing IR 05000219/19660011966-04-15015 April 1966 1966/04/15-IR 05000219-66-001, on 03/22-23/1966, Oyster Creek, Construction Inspection Report Including Drywell Testing 2016-12-01
[Table view] |
Text
IJ~ Vyl I flfl~-~- *. .'TIrr~~ iN O~-~
Results of Detailed Reviews Water Chemistry Management Program Scope of Inspection The inspectors reviewed the licensee's activities to implement commitment number 24, item 2, of the Oyster Creek NRC License Renewal Safety Evaluation Report. This commitment added the "B"Isolation Condenser Shell into the scope of Oyster Creek license renewal. In addition, it required the licensee to develop a Water Chemistry Management Program to manage the loss of material and crack initiation and growth aging effects.
Non-destructive evaluations (NDE) were performed on the interior of the "B"Isolation Condenser shell to provide reasonable assurance that the aging effects of the water in the shell will not impact the intended safety function of the Isolation Condenser.
The inspectors observed the non-destructive evaluations on the interior of the "B" Isolation Condenser shell and independently reviewed the results. The NDE (work order C2017561-11 ) included an interior visual inspection of the shell, ultrasonic testing in two locations that were previously UT tested in 1996 and 2002, UT testing in areas of identified pitting and corrosion and spark testing of the final interior shell coating. The inspectors compared the UT results with those measured in 1996 and 2002 to verify the..
corrosion rates would not impact the operability of the Isolation Condenser. Also, the UT results were reviewed against the minimum wall criteria for the Isolation Condenser shell.
Findings and Observations No findings of significance were identified. The inspectors identified no instances of inadequate implementation of the Water-Chemistry Management Program.
(,Ica !ý