ML061390034

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Licensees Meeting Slides for May 16, 2006 Public Meeting Byron Unit 1 and Braidwood Unit 2 Request for Deferment of Downstream Effects Related Modifications
ML061390034
Person / Time
Site: Byron, Braidwood  
Issue date: 05/16/2006
From:
Exelon Nuclear
To:
Office of Nuclear Reactor Regulation
References
Download: ML061390034 (15)


Text

Nuclear Bwron Unit l and Braidwood Unit 2 Request for Deferment of Downstream Effects Related Modifications May 16,2006 Page 1

Exelon Attendees Bruce Rash - Corporate Engineering Design Director Brian Davenport - Corporate Engineering John Panici Braidwood Design Engineering Joseph Bauer - Corporate Licensing Douglas Walker Corporate Licensing Dan Brush - Project Manager Ivo Garza - Sargent and Lundy Presenter: Brian Davenport Corporate Engineering Page 2

AGENDA

> Request for Deferment of Downstream Effects related plant changes until Spring 2008 for Bryron Unit 1 and Braidwood Unit 2, only.

) Summarize GSI-1 91 Analyses & Testing

> Plant Change Implementation Plans

> Downstream Effects Analyses Performed

> Downstream Effects Plant Changes Needed

> NRC Decision Requested Page 3

GSI -191 Resolution Schedule Full Scope:

> Byron Unit 2 (Spring 2007)

) Braidwood Unit 1 (Fall 2007)

Sump Screen ReplacementlDefer Downstream only:

) Byron Unit 1 (Fall 2006)

Braidwood Unit 2 (Fall 2006)

Replacing all Sump Scre ens prior 12/31/07 in accordance w-lith GL schedule.

Page 4

Decision R e quest

> Approval to Defer Downstream Effects related plant changes until Spring 2008 Refueling Outages, for Byron Unit 1 and Braidwood Unit 2, only,

) Work Scope to be Deferred

> ECCS Throttle Valve / Orifice Work

> CS Pump Cyclone Separator Removal / Modification

> Proposed Schedule

> Byron Unit 1 Spring 2008 Refueling Outage

> Braidwood Unit 2 -

Spring 2008 Refueling Outage Page 5

ANALYSIS STATUS:

Analysis/testing performed to ensure adequate NPSH for ECCS Pumps

) NEI 02-01 Walkdowns (all 4 units complete)

I Debris Generation Analysis performed

Containment Transport Analysis performed

> Includes Computational Fluid Dynamics (CFD) model H

Head Loss Analysis (per GR/SER) performed

) Vendors Strainer, Head Loss Testing performed (wlo chemical effects)

> Bypass testing performed

> Downstream Effects analysis performed (per WCAP 16406-P)

) Scheduled testing

> Chemical Effects Testing (completion June 2006)

Supplemental head loss testing (completion June 2006)

Performing analyses in accordance with recommended NEI and GRISER Guidelines Page 6

Plant Change Implementation

) Install new replacement sump strainers in each sump (2 sumps per unit)

> New strainer size approximately 3000 sq.fti/sump; current total strainer area - 150 sq.ft.

> New screen mesh size will be smaller than current (1/1 2" versus 3/16" currently)

> Remove fiberglass insulation on mid-section of steam generators & connecting piping within ZOI, replace with Reflective Metal Insulation (RMI) (Unit 1 at each plant)

> Alleviates fiber debris load at sump screen

> Unit 2 at each plant is virtually all RMI insulation

> Install trash racks for debris interception

> Upstream of new sump screens Minimizing fiber, debris load mainly RMI, Coatings, and Latent debris.

Installing maximum strainer area that fits inside plant sumps.

Page 7

At.creen.nstallation i~~~Pg le Nl m

Screen Installation

w
. :.k I

I I

Downstream Effects Analysis

> Analysis performed based on WCAP 1 6406-P

> Equipment Evaluated for wear and plugging

> Residual Heat Removal (RHR) Pumps and Heat Exchangers

> Safety Injection (SI) Pumps

> Charging I Safety Injection (CV) Pumps

> Containment Spray (CS) Pumps, Spray Eductors and Nozzles

> Flow Orifii (restricting and flow element)

> Throttle Valves

> Instrumentation

> Piston Check Valves

Relief Valves

> Reactor fuel and vessel internals l component wear is minimal for 30 day mission time. l Page 1 0

Downstream Effects Plant Change Implementation

> Identified two plant changes due to possible plugging issues

> ECCS Throttle valves (8/Unit)

> Replacement of trim and some pressure retaining parts on 8 valves/unit and downstream orifii

> CS Pump Cyclone Separator removal from the seal purge line

> Flowserve preliminary solution replaces separator with a pressure breakdown device.

Changes to ECCS throttle valves needed; removal of cyclone separator preliminary scope determined with pump seal vendor.

Page 1 1

Downstream Effects Challenges GSl-1 91 Full Scope Schedule I

GSHl91 Full Scope ScheduleI Full evaluation and shop testing needed to confirm acceptable impact on ECOS systems. Insufficient time to ensure proper requirements are met.

Safet Impact o Margin Improvements

> Removing fibrous insulation from ZOI areas and replacing with RMI

<(Unit 1 at both Byron & Braidwood )

> New Strainers Size Approximately 3000 sq.ft./sump; 2 sumps/unit; current strainer area - 150 sq.ft.

> New screen mesh size will be smaller than current (1/12" versus 3/1 6' currently)

> Adding trash racks upstream of new sump screens for large debris interception

> Mitigating Factors (Bulletin 2003-01 measures)

> Existing FME controls

) Improvements to the loose debris surveillances

> EOP changes to speed up cooldown in the event of a Small Break (SB) LOCA Planned Improvements increase margni and lower risk.

Page 13

Safet Impact

> RSik Perspective

> Short duration (12/31/07 - Spring 2008) from Generic Letter required implementation schedule

> Large Break LOCA generates/transports max. debris to sumps

> S1 and CV are only really needed for smaller LOCA's

> Sensitivity study of potential flow blockage indicates that 50% flow reduction of Si cold leg injection still provides adequate core cooling.

> Qualitative Risk assessment indicates a small incremental increase in risk.

> Cyclone separator concern much less likely due to reduction of fibrous insulation in ZOI inside containment o Not likely to significantly impact CS Pump operation.

I Additional 4 months results in very small incremental risk increase l

Page 14

Closing Remarks

) Bruce Rash-Exelon Corporate Engineering Design Director

> Approval to Delay Downstream Effects related plant changes until Spring 2008 Refueling Outages for Byron Unit 1 and Braidwood Unit 2, only,

> Work Scope to be Deferred

> ECCS Throttle Valve / Orifice Work

> CS Pump Cyclone Separator Removal / Modification D Proposed Schedule

> Byron Unit 1 Spring 2008 Refueling Outage

> Braidwood Unit 2 -

Spring 2008 Refueling Outage Page 15