ML052310588

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Fax Transmittal from D. Dodson of Millstone Power Station to B. Gott of USNRC, Regarding NRC Event Notification 41607 (5 Pages) Exemption 2)
ML052310588
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/17/2005
From: Douglas Dodson
Dominion Nuclear Connecticut, Northeast Nuclear Energy Co (NNECO)
To: Gott B
NRC/FSME
References
FOIA/PA-2005-0207
Download: ML052310588 (5)


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APR-1-2005 15:00 MILLSTONE

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NRC Event Notification Form (Sheet 1 of 2)

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GENERLEMRGENCY TS Dcviation (i)

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APR-19-2005 15:00 M ILLSTONE 860 443 5893 P.04 NRC Event Notification Form (Sheet 2 of 2)

NOTIFICATIONS E

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Rev. 001-04 99 of 115

iPR-18-20O5 15:00 MILLSTONE APR-18-2005 15: 00 M ILLSTONE 860 443 593Z

a. U.5 Attachment to April 17, 2005 Event Notification Summary of Event At approximately 0830 on April 17, 2005 Millstone Unit 3 experienced an automatic reactor trip from full power. The Reactor is in a stable shutdown condition and is proceeding to Mode 5 cold shutdown. No release of radioactivity other than those minor releases associated with normal plant operation has occurred. There were no personnel injuries associated with the event.

In addition to the Reactor Trip, half-train Safety Injection (SI) and half-train Main Steam Isolation (MSI) actuations occurred. Control room personnel were successful at manually initiating full SI and MSI. SI has since been terminated and RCS pressure control has been restored. Multiple steam line safety valves (MSSV) lifted with at least one M SSV indicating a failure to reclose. As a result, an ALERT was declared at approximately 0853 due to the failure of at least one MSSV failing to reclose. All MSSV's are currently closed. Auxiliary Feedwater (AFW) actuated automatically as expected, however; the turbine driven auxiliary feedwater pump (TDAFWP) tripped on start-up and was subsequently reset locally. Both motor driven auxiliary feedwater pumps (MDAFWPs) operated as expected to maintain steam generator water levels. Due to the additional inventory injected to the Reactor Coolant System (RCS) as a result of the SI actuation, the pressurizer filled and a primary system safety valve (PSSV) actuated at a lower than expected pressure. All PSSV's are currently closed, however; there is indication of leakage past either a PSSV or Pilot Operated Relief Valve (PORV). Upon alignment of the Charging system to Refueling Water Storage Tank recirculation flow path, 2 valves had indication of packing leakage. Those packing leaks have been terminated.

The cause of the event is under investigation.

HM1 I lLLIUNh 860 443 5893 P.06 Attachment to April 17,2005 Event Notification Summary of Event Event No. 41607 Update to previous information:

The previously reported time of the ALERT declaration should be corrected to read 0842. Millstone Unit 3 entered Mode 4 at approximately 1903 on April 17, 2005. The event at Millstone Unit 3 was terminated at 1905. The cause of event is under investigation. A recovery plan is being formulated.