ML052310588

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Fax Transmittal from D. Dodson of Millstone Power Station to B. Gott of USNRC, Regarding NRC Event Notification No. 41607 (5 Pages) Exemption 2)
ML052310588
Person / Time
Site: Millstone  Dominion icon.png
Issue date: 04/17/2005
From: Douglas Dodson
Dominion Nuclear Connecticut, Northeast Nuclear Energy Co (NNECO)
To: Gott B
NRC/FSME
References
FOIA/PA-2005-0207
Download: ML052310588 (5)


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APR-1-2005 15:00 MILLSTONE 860 44.3 5893 P.03

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4 1 1 7/O5 Attachment 8 NRC Event Notification Form (Sheet 1 of 2)

NRC CONTACr (NAME) _i// 6L oz NRC EVENT NUMBER: AAUP-7

'NOTIFICATION

_/330 TIME rAC3LlTYOR ORGANIZATION UrrIOFNME J3I-1 4 -vT 1 hVENT TIME (EST7OR EW) EVjENrVT Dt or1RFr#' POWER (%)and M0DE tiE F0~k.R *) aud MODJE Al.

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GENERLEMRGENCY TS Dcviation (i) TS Required Shut- MMi)(A) Detraded Conditon down SE AREAEMERGENCY _ (iv)(A) ECCS Discharge to (t)(8) Unanalyzed Cond;s RCS fion that Dcgadcs Safety 60 Day Optional (10)(R) RPS ActuatiOn (iv)(A) SpCdefid System Ac.

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INFORMATION ONLY Oxis) Los OtherAsce-mON CEMTNtEtU Comms (si) Emesgency Siren

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APR-19-2005 15:00 MILLSTONE 860 443 5893 P.04 Attachment 8 NRC Event Notification Form (Sheet 2 of 2)

NOTIFICATIONS E 0 L BE ANYTIG UNUSUAL OR NO yS NO Q UNDER!MOD? (EXPLAIN SHEET 1)

NRC RESIDENT DID ALL SYSTEMS FUNCTION YESi NO e-

- AS REQUIREDI (EXPLAIN SHEET 1)

STATE MODE OF OPEAION UNTIL CORRECT.

LOCAL - - ESTh(TD RESTARTIDATE: xiso OTHER GOV AGENCIES _ ADDITlONAL INFO ON BACK: YES NO09" MEDI)JFRESS RELEASE RADIOLOGICAL RELIASXS CHECKOR ILLINAPPLICABLZ IT6,S LIQUID GASEOUS UNPLANNED PLANNED ONGOING TERMINATED RELEASE RELEASE RELEASE RELEASE MONITORED UNMONMIORE OFFSITE T S. Rld ALARMS AREAS RELEASE _ EXCEEDED EVACUATED PERSONNEL EXPOSED OR OFPSITE PROTECITvE ACTIONS State rekae path in desceipo on CONTAMTNATED RECOMMNDED RcIesc Rate %T.J LIMIT ROO GUI2DE Toil  % T.S. LIT ROO GUIDE (Cifz) AAtivity (0)

Noble Ou 0.ICilsec 10O Cl ledine 10 PCi,=c QOl.Ci Pariulate I ,CtsCec I nmC Liquid (cocludrng Oinum & dissolved noble psu) 10 lCihnin 0.1 Cl

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Toul Activity PLANT STACO CONIDIENSERJAIR MAIN S OTHEI EJECIOR STEAM LINE SLOWDOWN 1.AD MONITOR READ-INGS: E~o _____  ?'4-2 If __ _

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LOCATION OF THE LEAK (O.e., SO#. valvec pipe, cte):

LEAK RATEl UN1TS pngpd T.S. LIITS: SUDDEN OR LONG-TERMA l l lDEYI-lOPMENT LEKSAT DATE lCOOLAACTIVITY UNITS: PRD4ARY - SECOlDARy-LIST OF SAFETY RELATED EQUIMN NOT OPERATINoAq-SMIMSEO Signature: 4 4 uue: 'rim: 2 tO0 Level of Use 1RAC 14 Reference w Rev. 001-04 99 of 115

15:00 MILLSTONE iPR-18-20O5 APR-18-2005 15: 00 MILLSTONE 860 443 593Z a. U.5 Attachment to April 17, 2005 Event Notification Summary of Event At approximately 0830 on April 17, 2005 Millstone Unit 3 experienced an automatic reactor trip from full power. The Reactor is in a stable shutdown condition and is proceeding to Mode 5 cold shutdown. No release of radioactivity other than those minor releases associated with normal plant operation has occurred. There were no personnel injuries associated with the event.

In addition to the Reactor Trip, half-train Safety Injection (SI) and half-train Main Steam Isolation (MSI) actuations occurred. Control room personnel were successful at manually initiating full SI and MSI. SI has since been terminated and RCS pressure control has been restored. Multiple steam line safety valves (MSSV) lifted with at least one M SSV indicating a failure to reclose. As a result, an ALERT was declared at approximately 0853 due to the failure of at least one MSSV failing to reclose. All MSSV's are currently closed. Auxiliary Feedwater (AFW) actuated automatically as expected, however; the turbine driven auxiliary feedwater pump (TDAFWP) tripped on start-up and was subsequently reset locally. Both motor driven auxiliary feedwater pumps (MDAFWPs) operated as expected to maintain steam generator water levels. Due to the additional inventory injected to the Reactor Coolant System (RCS) as a result of the SI actuation, the pressurizer filled and a primary system safety valve (PSSV) actuated at a lower than expected pressure. All PSSV's are currently closed, however; there is indication of leakage past either a PSSV or Pilot Operated Relief Valve (PORV). Upon alignment of the Charging system to Refueling Water Storage Tank recirculation flow path, 2 valves had indication of packing leakage. Those packing leaks have been terminated.

The cause of the event is under investigation.

HM1 IlLLIUNh 860 443 5893 P.06 Attachment to April 17,2005 Event Notification Summary of Event Event No. 41607 Update to previous information:

The previously reported time of the ALERT declaration should be corrected to read 0842. Millstone Unit 3 entered Mode 4 at approximately 1903 on April 17, 2005. The event at Millstone Unit 3 was terminated at 1905. The cause of event is under investigation. A recovery plan is being formulated.