ML043560154
| ML043560154 | |
| Person / Time | |
|---|---|
| Site: | Oyster Creek |
| Issue date: | 12/10/2004 |
| From: | Swenson C AmerGen Energy Co, Exelon Corp |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| 2130-04-20317, GL-97-002 | |
| Download: ML043560154 (2) | |
Text
AmerGen M AmerGen Energy Company, LLC Oyster Creek US Route 9 South, P.O. Box 388 Forked River, NJ 08731-0388 www.exeloncorp.corn An Exelon Company GL 97-02 December 10, 2004 2130-04-20317 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 - 0001 Oyster Creek Generating Station Facility Operating License No. DPR-16 NRC Docket No. 50-219
Subject:
Monthly Operating Report -, November 2004 Enclosed is the November 2004 Monthly Operating Report for Oyster Creek Generating Station. The content and format of information submitted in this report is in accordance with the guidance provided by Generic Letter 97-02.
If any further information or assistance is needed, please contact David Fawcett at 609-971-4284.
Sinyl~))
/
C. N. Swenson Vice President, Oyster Creek Generating Station CNS/DIF Enclosure cc:
S. J. Collins, Administrator, USNRC Region I P. S. Tam, USNRC Senior Project Manager, Oyster Creek R. J. Summers, USNRC Senior Resident Inspector, Oyster Creek File No. 04002
I-OPERATING DATA REPORT DOCKET NO.
50-219 UNIT NAME Oyster Creek 1 DATE December 07, 2004 COMPLETED BY Roger B. Gayley TELEPHONE (609) 971-4406 REPORTING PERIOD:
November 2004
- 1. Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 650.00 619.00 3.
4.
5.
6.
Number of Hours the Reactor was Critical Number of Hours Generator On-line Reserve Shutdown Hours Net Electrical Energy Generated (MWHrs)
This Month 261.33 241.52 0.00 122,953.00 Yr-to-Date 7,298.48 7,230.80 0.00 4,373,174.00 Cumulative 225,735.50 221,426.45 918.20 126,767,927.0 UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action No.
Date S: Scheduled (Hours)
Reason 1 Down 2 Comments 1
11/02/2004 S
478.48 C
1 Planned refueling maintenace outage designated 1 R20. The planned duration was 15 days, 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />. The actual duration was 19 days, 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />, 29 minutes.
SUMMARY
- During November, Oyster Creek generated 122,953 net MWh electric, which was 27.6% of its MDC rating. A refueling maintenance outage designated 1 R20 was completed during the month. The outage commenced 11/2/04 at 15:00 hours and was completed 11/22/04 at 13:29 hours, a total of 478.49 hour5.671296e-4 days <br />0.0136 hours <br />8.101852e-5 weeks <br />1.86445e-5 months <br /> duration. The outage duration extended four days beyond schedule resulting in an unplanned energy loss of 57.003 MWhrs.
1 2
Reason:
A Equipment Failure (Explain)
B Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
1 Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
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