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MONTHYEARML0434403632005-01-12012 January 2005 Summary of Conference Call with Carolina Power & Light Company Regarding Spring 2004 Steam Generator Tube Inspections at Shearon Harris Nuclear Power Plant Unit 1 Project stage: Other 2005-01-12
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Category:Letter
MONTHYEARIR 05000400/20230042024-01-30030 January 2024 Integrated Inspection Report 05000400/2023004 ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000400/20230032023-11-0909 November 2023 Integrated Inspection Report 05000400/2023003 ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published ML23234A1702023-10-0303 October 2023 Issuance of Amendment No. 199 Regarding Administrative Changes to the Renewed Facility Operating License and Technical Specifications ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000400/20230052023-08-23023 August 2023 Updated Inspection Plan for Shearon Harris Nuclear Power Plant, Unit 1 (Report 05000400/2023005) ML23234A2542023-08-22022 August 2023 RQ Inspection Notification Letter IR 05000400/20234022023-07-26026 July 2023 Security Baseline Inspection Report 05000400/2023402 IR 05000400/20230022023-07-24024 July 2023 Integrated Inspection Report 05000400/2023002 IR 05000400/20234402023-07-17017 July 2023 Special Inspection Report 05000400/2023440 and Preliminary Greater than Green Finding and Apparent Violation Cover Letter IR 05000400/20243012023-05-15015 May 2023 Notification of Licensed Operator Initial Examination 05000400/2024301 IR 05000400/20230012023-05-10010 May 2023 Integrated Inspection Report 05000400 2023001 IR 05000400/20234042023-05-0404 May 2023 Cyber Security Inspection Report 05000400/2023404 ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML23118A1392023-04-28028 April 2023 Submittal of Updated Final Safety Analysis Report (Amendment 65), Technical Specification Bases Revision, Report of Changes Pursuant to 10 CFR 50.59 and Summary of Commitment Changes IR 05000400/20234032023-04-0505 April 2023 Security Baseline Inspection Report 05000400/2023403 IR 05000400/20230102023-03-15015 March 2023 Comprehensive Engineering Team Inspection (CETI) Inspection Report 05000400/2023010 ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000400/20220062023-03-0101 March 2023 Annual Assessment Letter for Shearon Harris Nuclear Power Plant - NRC Inspection Report 05000400/2022006 ML23033A5272023-02-0808 February 2023 Correction of Typographical Errors Incurred During Issuance of License Amendment No. 196 IR 05000400/20220042023-02-0707 February 2023 Integrated Inspection Report 05000400/2022004 ML23020A1252023-01-23023 January 2023 Notification of Target Set Inspection and Request for Information (NRC Inspection Report 05000400/2023403) ML22096A0032022-11-18018 November 2022 McGuire Nuclear Station and Shearon Harris Nuclear Power Plant Authorization of RA-19-0352 Regarding Use of Alternative for RPV Head Closure Stud Examinations ML22256A2532022-11-14014 November 2022 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-541, Rev. 2 IR 05000400/20220032022-11-10010 November 2022 Integrated Inspection Report 05000400/2022003 IR 05000400/20223012022-11-0202 November 2022 NRC Operator License Examination Report 05000400/2022301 ML22271A6202022-09-29029 September 2022 Notification of Shearon Harris Nuclear Power Plant Comprehensive Engineering Team Inspection - U.S. Nuclear Regulatory Commission Inspection Report 05000400/2023010 ML22258A1262022-09-14014 September 2022 NRC Operator Licensing Examination Approval 05000400/2022301 ML22242A0022022-09-12012 September 2022 Issuance of Amendments to Adopt TSTF 569, Revision 2, Revise Response Time Testing Definition ML22227A0682022-09-0202 September 2022 Alternative to Certain Inservice Testing Requirements in the American Society of Mechanical Engineers Code for Operation and Maintenance for Certain Target Rock Solenoid Valves IR 05000400/20220052022-08-24024 August 2022 Updated Inspection Plan for Shearon Harris Nuclear Power Plant (Report 05000400/2022005) IR 05000400/20224032022-08-23023 August 2022 Security Baseline Inspection Report 05000400/2022403 ML22126A0082022-08-0909 August 2022 Issuance of Amendment No. 194 Revise Technical Specifications Related to Reactor Protection System Instrumentation P7 IR 05000400/20220022022-08-0505 August 2022 Integrated Inspection Report 05000400/2022002 ML22161B0332022-07-28028 July 2022 Issuance of Amendment No. 193 Regarding Revision of Surveillance Requirements to Remove Shutdown Limitation IR 05000400/20220112022-07-20020 July 2022 Biennial Problem Identification and Resolution Inspection Report 05000400 2022011 IR 05000400/20224022022-06-30030 June 2022 Material Control and Accounting Program Inspection Report 05000400/2022402 (OUO Removed) IR 05000400/20220102022-06-13013 June 2022 Design Basis Assurance Inspection (Programs) Inspection Report 05000400/2022010 ML22138A4012022-05-26026 May 2022 Project Manager Reassignment ML22101A2822022-05-0606 May 2022 Regulatory Audit Summary Related to the Review of License Amendment Regarding Revising the Flood Hazard Protection Scheme IR 05000400/20220012022-05-0404 May 2022 Integrated Inspection Report 05000400/2022001 IR 05000400/20224012022-03-24024 March 2022 Security Baseline Inspection Report 05000400/2022401 ML22020A0072022-03-10010 March 2022 Issuance of Amendment No. 192 Regarding Removal of Extraneous Content and Requirements from the Renewed Facility Operating License and Technical Specifications ML22010A2812022-03-0404 March 2022 Issuance of Amendments to Adopt TSTF-577, Rev. 1 Revised Frequencies for Steam Generator Tube Inspections (EPID L-2021-LLA-0161 IR 05000400/20210062022-03-0202 March 2022 Annual Assessment Letter for Shearon Harris Nuclear Power Plant (Report No. 05000400/2021006) ML21351A4722022-02-10010 February 2022 Issuance of Amendment No. 190 Regarding Revision to Containment Spray Nozzle Test Frequency IR 05000400/20210042022-02-0404 February 2022 Integrated Inspection Report 05000400/2021004 ML22034A5352022-02-0202 February 2022 Notification of Licensed Operator Initial Examination 05000400/2022301 2024-01-30
[Table view] Category:Meeting Summary
MONTHYEARML23157A3202023-06-26026 June 2023 Summary of April 26, 2023, Meeting with Duke Energy to Discuss a Shearon Harris Nuclear Power Plant, Unit 1 Planned License Amendment Request Related to Turbine Control System and Reactor Protection System Circuitry ML23151A1232023-05-31031 May 2023 Public Meeting Summary - 2022 Annual Assessment Meeting Regarding Shearon Harris Nuclear Plant ML22167A1852022-06-30030 June 2022 Summary of June 6, 2022, Meeting with Duke Energy to Discuss Shearon Harris Nuclear Power Plant, Unit 1 Closeout of Generic Safety Issue (GSI) 191 ML22129A0062022-05-10010 May 2022 Summary of April 20, 2022, Meeting with Duke Energy Progress, LLC, to Discuss Proposed License Amendment Request to Revise Reactor Coolant System Pressure Isolation Valve Operational Leakage Surveillance Requirement Frequency (L-2022-LRM 00 ML22130A0302022-05-0909 May 2022 Summary of Public Meeting on 2021 Annual Assessment Meeting Regarding Brunswick Steam Electric Plant, Docket Nos. 50-325 and 50-324; and Shearon Harris Nuclear Power Plant, Docket No. 50-400, Meeting Number 20220350 ML21341A5542021-12-29029 December 2021 Summary of November 29, 2021, Meeting with Duke Energy Progress, LLC and Duke Energy Carolinas, LLC to Discuss a Planned License Amendment Request to Relocate ML21172A2672021-08-13013 August 2021 Regulatory Audit Summary Related to the Review of LAR to Revise 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, Systems and Components for Nuclear Power Reactors, Categorization Process to Reflect an Alternative Seis ML21131A1472021-05-11011 May 2021 Public Meeting Summary 2020 Annual Assessment Meeting Regarding Brunswick Steam Electric Plant, Docket Nos. 50-325 and 50-324; and Shearon Harris Nuclear Power Plant, Docket No. 50-400, Meeting Number 20210385 ML20136A2222020-05-15015 May 2020 Har - Bru 2019 Aam Meeting Summary ML19331A8062020-01-29029 January 2020 Summary of November 13, 2019 Closed Meeting with Duke Energy Carolinas, LLC and Duke Energy Progress, LLC, to Discuss Security-Related Information for Its Licensed Facilities ML19329A0232019-11-27027 November 2019 Summary of October 29, 2019 Conference Call with Duke Energy Progress, LLC Regarding the Fall 2019 Steam Generator Tube Inspections ML19241A2902019-09-24024 September 2019 Summary of August 22, 2019, Meeting with Duke Energy Progress, LLC Proposed License Amendment Request to Adopt Risk-Informed Completion Times ML19220A6702019-08-26026 August 2019 Summary of August 7, 2019, Meeting with Duke Energy Progress, LLC and Duke Energy Carolinas, LLC to Discuss a Proposed License Amendment Request for a Common Emergency Plan ML19113A0652019-05-14014 May 2019 Summary of Meeting with Duke Energy to Discuss Proposed License Amendment Request for Shearon Harris, Unit 1, Technical Specification Changes Associated with Departure from Nucleate Boiling Ratio Safety Limit ML19120A1342019-05-0606 May 2019 3/15/19 Summary of Public Meeting with Nuclear Entergy Institute, Duke Energy, and Southern Nuclear Operating Company Post-Pilot Implementation of Tornado Missile Risk Evaluator Methodology at Vogtle, Units 1 and 2 and Shearon Harris, Unit ML19123A3522019-05-0202 May 2019 Public Meeting Summary - Shearon Harris Nuclear Plant, Docket No. 50-400 ML19087A0622019-04-11011 April 2019 Summary of March 25, 2019, Public Teleconference with Duke Energy to Discuss the Request for Additional Information Response Regarding the Proposed Alternative to the Depth Sizing Qualification Requirement (Duke Energy Fleet Relief Request ML18361A6712019-01-0808 January 2019 Summary of Meeting with Duke Energy Progress, LLC to Discuss License Amendment Request for Shearon Harris Unit 1, Regarding 10 CFR 50.69, Risk-Informed Categorization and Treatment of Structures, ML18352A3572019-01-0808 January 2019 Summary of Meeting with Duke Energy Progress, LLC to Discuss Proposed License Amendment Request for Shearon Harris Nuclear Power Plant, Unit 1, Regarding Emergency Plan Changes ML18355A8142019-01-0707 January 2019 Summary of December 20, 2018, Teleconference Meeting with Duke Energy Progress, LLC to Discuss a Proposed License Amendment Request for Shearon Harris Unit 1, Regarding a Risk-Informed Essential Services Chilled Water System TS ML18094A2632018-08-17017 August 2018 Summary of 01/18/2018, Public Meeting with Nuclear Energy Institute, Duke Energy, Southern Nuclear Operating Co., Entergy Operations, Inc. to Discuss Development of Tornado Missile Risk Evaluator Methodology ML18109A0912018-04-19019 April 2018 Summary of 2017 Annual Assessment Public Meeting Regarding Shearon Harris Nuclear Plant, Docket No. 50-400 ML18088A0732018-04-0303 April 2018 March 27, 2018, Summary of Presubmittal Meeting with Duke Energy Progress, LLC to Discuss a Proposed Relief Request for Shearon Harris Nuclear Power Plant, Unit 1 ML18064A1332018-03-19019 March 2018 Summary of February 27, 2018, Meeting with Duke Energy Progress, LLC to Discuss Proposed License Amendment Request for Shearon Harris Nuclear Power Plant, Unit 1, Regarding Emergency Plan Emergency Action Level Scheme Changes (L-2017-LRM-00 ML17340A1302017-12-22022 December 2017 Summary of November 29, 2017, Meeting with Duke Energy Progress, LLC to Discuss Proposed License Amendment Requests to Implement the Requirement of 10 CFR 50.69 at Brunswick, Shearon Harris, and H. B. Robinson ML17340A0612017-12-0808 December 2017 11/8/17 Summary of Teleconference with Entergy Operations, Inc., Tornado Missile Risk Evaluator with Applicability to Submittals from Duke Energy and Southern Nuclear Operating Co, Inc. ML17244A0742017-09-28028 September 2017 8/17/2017 Summary of Public Meeting with Nuclear Energy Institute and Licensees to Discuss the Tornado Missile Risk Evaluation Tool for Grand Gulf, Shearon Harris, and Vogtle, Units 1 and 2 ML17257A0992017-09-26026 September 2017 Summary of Public Meeting with Nuclear Energy Institute and Licensees to Discuss the Tornado Missile Risk Evaluation Tool for Grand Gulf, Shearon Harris, and Vogtle, Units 1 and 2 ML17223A1212017-08-17017 August 2017 Summary of August 3, 2017, Meeting with Duke Energy Progress, LLC on Proposed License Amendment Request to Implement Fuel Reload Design Methodology Reports for Shearon Harris and H. B. Robinson ML17145A3142017-05-25025 May 2017 EOC Meeting Summary ML16286A0152016-11-0101 November 2016 Summary Of September 29, 2016, Duke Energy Progress, LLC. To Discuss Proposed License Amendment Request Regarding Shearon Harris Nuclear Power Plant, Unit 1, BWR Storage Rack Inserts And The Spent Fuel Pool Criticality Analysis (CAC No. MF8327) ML16235A2382016-10-17017 October 2016 Summary of the July 12-13, 2016 Audit Supporting the U.S. Nuclear Regulatory Commission Review of DPC-NE-1008-P, Nuclear Design Methodology Using CASMO-5/SIMULATE-3 for Westinghouse Reactors ML16125A0992016-05-20020 May 2016 Summary of May 2, 2016, Meeting with Duke Energy Progress, Inc. to Discuss Fuel Reload Design Methodology Reports and Proposed Supplement to a License Amendment Request Regarding Shearon Harris and H.B. Robinson ML16134A1552016-05-12012 May 2016 Public Meeting Summary - 2015 Annual Assessment Public Meeting Regarding Shearon Harris Nuclear Plant ML16112A3772016-04-25025 April 2016 Summary of Meeting with Duke Energy Progress, Inc. to Discuss the Shearon Harris Nuclear Plant, Unit 1, TSTF-425 LAR Request for Additional Information Reponses ML16034A5242016-03-11011 March 2016 Summary of February 1, 2016, Pre-submittal Meeting with Duke Energy Regarding Consolidation of Emergency Operations Facilities ML16035A4802016-02-12012 February 2016 Jsc Meeting Summary Attachment ML15280A2532015-11-25025 November 2015 Summary of Mtg. with Duke Energy Progress Inc. to Discuss Fuel Reload Design Methodology Reports & Proposed License Amendment Request Shearon Harris Nuclear Power Plant Unit 1 and H.B. Robinson Steam Electric Plant Unit No. 2 (MF6701/MF6702 ML15202A4752015-09-24024 September 2015 Summary of Meeting with Duke Energy Progress, Inc. to Discuss Shearon Harris Nuclear Power Plant, Unit 1, Proposed License Amendment Request Regarding Technical Specifications for the Pressurizer and Main Steam Line Safety Valves (MF6233) ML14129A3352014-05-0909 May 2014 Summary of Category 1 Public Meeting - Annual Assessment of Shearon Harris Nuclear Plant ML13312A9882013-11-0808 November 2013 Summary of Public Meeting with Duke Energy Carolinas, LLC, to Provide Opportunities to Discuss the Planned Fukushima-Related Modifications ML13204A2672013-09-27027 September 2013 07/09/13 Summary of Meeting with Duke Energy Regarding a Nonconservative Technical Specification Loss of Offsite Power Voltage Setpoint License Amendment Request ML13218B3692013-09-27027 September 2013 7/30/2013 - Summary of Meeting with Duke Energy Regarding a Change to the Emergency Response Facility Activation Timeliness and Criteria ML13225A2932013-08-12012 August 2013 7/23-24/2013, Summary of Meeting 2013 U.S. Nuclear Regulatory Commission (NRC) Initial Exam Writers' Workshop ML13171A3292013-06-20020 June 2013 Public Meeting Summary, Category 3, NRC Special Inspection on Reactor Vessel Head Nozzle Repair of Shearon Harris Nuclear Plant ML13155A1052013-06-12012 June 2013 May 2, 2013, Summary of Meeting with Duke Energy Concerning the Relocation of the Emergency Operating Facilities ML13151A2262013-05-30030 May 2013 Meeting Summary - Category 1 Public Meeting Annual Assessment - Shearon Harris Nuclear Plant - Docket 50-400 ML12277A0252012-11-0202 November 2012 10/2/12 Summary of Meeting with Duke Energy Carolinas to Discuss Nonconservative Technical Specifications License Amendment Requests ML12242A4322012-08-28028 August 2012 Summary of Category 1 Public Meeting - Regulatory Conference and Predecisional Enforcement Conference ML12107A0012012-04-16016 April 2012 Meeting Summary - Category 1 Public Meeting - Annual Assessment of Shearon Harris Nuclear Plant 2023-06-26
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Text
January 12, 2005 Mr. James Scarola, Vice President Shearon Harris Nuclear Power Plant Carolina Power & Light Company Post Office Box 165, Mail Code: Zone 1 New Hill, North Carolina 27562-0165
SUBJECT:
SUMMARY
OF CONFERENCE CALL WITH PROGRESS ENERGY REGARDING THE SPRING 2004 STEAM GENERATOR TUBE INSPECTIONS AT SHEARON HARRIS (TAC NO. MC3133)
Dear Mr. Scarola:
On May 13, 2004, the Nuclear Regulatory Commission staff participated in a conference call with Carolina Power & Light Company representatives to discuss the results of ongoing inspections of the Shearon Harris Nuclear Power Plant Unit 1 steam generator tubes during a spring 2004 outage. A summary of the conference call is enclosed for your information.
Please contact me if you have any questions.
Sincerely,
/RA/
Chandu P. Patel, Project Manager, Section 2 Project Directorate II Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket No. 50-400
Enclosure:
As stated cc w/encl: See next page
ML043440363 NRR-106 OFFICE PM:PDII/S2 LA:PDII/S2 SC:PDII/S2 NAME CPatel EDunnington BMozafari for MMarshall DATE 12 / 9 /04 12 / 8 /04 1 / 12 /04 COPY Yes Yes No
SUMMARY
OF CONFERENCE CALL WITH CAROLINA POWER & LIGHT COMPANY REGARDING THE SPRING 2004 STEAM GENERATOR INSPECTION RESULTS AT SHEARON HARRIS On May 13, 2004, the NRC staff participated in a phone call with Carolina Power & Light Company (CP&L) representatives to discuss the results of an ongoing steam generator (SG) tube inspection at Shearon Harris Nuclear Power Plant Unit 1 (HNP). HNP has three Westinghouse Model Delta 75 steam generators with thermally treated Alloy 690 tubing. A summary of the phone call is provided below. Although no steam generator tube inspection was planned this spring, CP&L personnel decided to investigate the source of low-level primary-to-secondary system leakage in SG C after a unit trip on May 6, 2004. Based on tritium analysis, the primary-to-secondary leak was determined to have initiated on April 21, 2004, and varied in the range of approximately 5 to 10 gallons per day in the week preceding plant shutdown.
The plant performed a secondary side pressure test to help locate the leaking tube in SG C.
Drips from the leaking tube (R3, C120) were evident once the pressure reached 12 to 20 pounds per square inch gage (psig). Although the staff intended to test up to 750 psig, they were unable to reach pressures greater than approximately 60 psi because the capacity of the nitrogen supply system was exceeded. The licensee was investigating the source of the nitrogen leak during the pressure test. Following the pressure test, a foreign object search and retrieval (FOSAR) examination was performed. A metallic piece was visually identified in SG C above the cold leg tubesheet and adjacent to a flow blocking plate. This piece contacted several tubes and was removed during the FOSAR. The object was approximately 2 1/4-inches long, magnetic, and had an irregular shape with sharp edges. No other loose parts were found in SG C.
Bobbin coil and rotating probe eddy current testing was performed on 15 tubes in the area near the loose part. In addition, the licensee inspected the full length of approximately 20 percent of the tubes with a bobbin coil probe. The 20-percent sample included all peripheral tubes and selected columns of interior tubes. This testing identified three indications in SG C above the cold leg tubesheet (CLT) at the loose part location. All of the indications were associated with the loose part. Additional details are summarized below.
Row Column Location Bobbin Coil Indication +PointTM Comments 3 120 CLT + 0.2" No 73% leaking tube 1 120 CLT + 0.7" Yes 80%
2 121 CLT + 0.5" Yes 45%
The distance in the location column shown above is to the center of the indication. Bobbin coil was not able to detect the through-wall damage in tube Row 3, Column 120 but did detect wear that occurred further away from the top of the cold leg tubesheet in the other two tubes. The bobbin coil also did not show evidence of a loose part at this location. The part was removed before the rotating coil inspections were performed.
At the time of the call the licensee was evaluating the use of a bobbin coil 3-frequency mix technique to evaluate for loose part damage above the top of the tubesheet. The licensee also ENCLOSURE
reviewed historical eddy current data in the loose part region from the bobbin coil examination conducted during the 2003 refueling outage. Tube Row 3, Column 120 and Tube Row 2, Column 121 had no detectable degradation or loose parts signals in the 2003 data. A bobbin coil indication measuring 40-percent through-wall, however, was present in Tube Row 1, Column 120 during the 2003 examination but was missed by both primary (manual) and secondary (computer) analysis. The 40-percent indication depth was estimated using 2003 bobbin coil phase angle analysis. This indication was estimated by 2004 bobbin coil phase angle analysis to have grown to 66-percent through-wall. Investigation into why this indication was not called by the computerized data screening (CDS) system used for secondary analysis revealed a set-up error in the CDS parameters. When the inspection parameters were entered into the CDS system for different regions of the HNP steam generators, a 1/2-inch gap (from 1/2 inch above the tubesheet to 1 inch above the tubesheet) was inadvertently created in the tube analysis. This CDS input error caused the computerized tube analysis to skip the portion of the tube containing the 40-percent through-wall bobbin indication in tube Row 1, Column 120 during the 2003 analysis.
Based on the 2004 eddy current test results, the licensee planned to insitu pressure test the tubes in Row 3, Column 120 and Row 1, Column 120. All three tubes with wear damage were to be plugged and stabilized. The licensee had planned to review the FOSAR tapes from the 2003 outage.
Based on vendor analysis of pre-outage data collected from the loose part monitors from all steam generators, the licensee planned a FOSAR at the top of the tubesheet in SG A during the 2004 outage. A small piece of material was detected during this examination and was removed from the SG.
At the conclusion of the call, the NRC staff expressed interest in the results from the review of the 2003 FOSAR tapes. In addition, the NRC staff indicated they would be evaluating the HNP information to determine if there were any issues with potential generic implications.
Finally, the NRC staff questioned why the licensee was not planning more rotating probe inspections at the top of the tubesheet given the bobbin coil examination did not detect the through-wall damage in Row 3, Column 120.
Subsequent to the conference call, the NRC staff was informed that the loose part that caused the damage in SG C was visible on the 2003 FOSAR inspection tape. Insitu pressure test results, including tests corresponding to a main steamline break pressure and three times the normal operating differential pressure (3X NODP), were also provided to the NRC staff. The indication in Row 1, Column 120 did not leak or burst at a 3X NODP pressure (the insitu test was a partial tube test). The indication in Row 3, Column 120 had a calculated temperature corrected leak rate of approximately 23 gallons per day at a steamline break pressure and did not burst at the 3X NODP proof test pressure. These insitu pressure test results demonstrated the tubes with loose part damage retained adequate structural integrity. The test results also provided data supporting that the SG had adequate leakage integrity.
Mr. James Scarola Shearon Harris Nuclear Power Plant Carolina Power & Light Company Unit 1 cc:
Steven R. Carr Associate General Counsel - Legal Department 2
Progress Energy Service Company, LLC Mr. Robert P. Gruber Post Office Box 1551 Executive Director Raleigh, North Carolina 27602-1551 Public Staff NCUC 4326 Mail Service Center Resident Inspector/ Harris NPS Raleigh, North Carolina 27699-4326 c/o U. S. Nuclear Regulatory Commission 5421 Shearon Harris Road Chairman of the North Carolina New Hill, North Carolina 27562-9998 Utilities Commission Post Office Box 29510 Ms. Margaret A. Force Raleigh, North Carolina 27626-0510 Assistant Attorney General State of North Carolina Mr. Herb Council, Chair Post Office Box 629 Board of County Commissioners Raleigh, North Carolina 27602 of Wake County P. O. Box 550 Public Service Commission Raleigh, North Carolina 27602 State of South Carolina Post Office Drawer 11649 Mr. Tommy Emerson, Chair Columbia, South Carolina 29211 Board of County Commissioners of Chatham County Ms. Beverly Hall, Section Chief P. O. Box 87 Division of Radiation Protection Pittsboro, North Carolina 27312 N.C. Department of Environment and Natural Resources Mr. Terry C. Morton, Manager 3825 Barrett Drive Support Services Raleigh, North Carolina 27609-7721 Shearon Harris Nuclear Power Plant Carolina Power & Light Company Mr. Chris L. Burton P. O. Box 165, Mail Zone 1 Manager New Hill, North Carolina 27562-0165 Performance Evaluation and Regulatory Affairs PEB 7 Mr. David H. Corlett, Supervisor Progress Energy Licensing/Regulatory Programs Post Office Box 1551 Shearon Harris Nuclear Power Plant Raleigh, North Carolina 27602-1551 Carolina Power & Light Company P. O. Box 165, Mail Zone 1 Mr. Benjamin C. Waldrep New Hill, NC 27562-0165 Plant General Manager Shearon Harris Nuclear Power Plant Carolina Power & Light Company P. O. Box 165, Mail Zone 3 New Hill, North Carolina 27562-0165 Mr. John H. ONeill, Jr.
Shaw, Pittman, Potts & Trowbridge 2300 N Street, NW.
Washington, DC 20037-1128 Mr. Robert J. Duncan II Director of Site Operations Shearon Harris Nuclear Power Plant Carolina Power & Light Company Post Office Box 165, Mail Zone 1 New Hill, North Carolina 27562-0165