NRC 2002-0050, to License Amendment Request 229 TS LCO 3.5.2, ECCS-Operating, & LCO 3.5.3, ECCS-Shutdown

From kanterella
(Redirected from ML031600959)
Jump to navigation Jump to search
to License Amendment Request 229 TS LCO 3.5.2, ECCS-Operating, & LCO 3.5.3, ECCS-Shutdown
ML031600959
Person / Time
Site: Point Beach  NextEra Energy icon.png
Issue date: 05/30/2003
From: Cayia A
Nuclear Management Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NRC 2002-0050
Download: ML031600959 (24)


Text

N Committed to Nuclear Excellen Point Beach Nuclear Plant Operated by Nuclear Management Company, LLC NRC 2003-0050 10 CFR 50.90 May 30, 2003 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 DOCKETS 50-266 AND 50-301 POINT BEACH NUCLEAR PLANT, UNITS 1 AND 2 SUPPLEMENT 2 TO LICENSE AMENDMENT REQUEST 229 TECHNICAL SPECIFICATION LCO 3.5.2, ECCS - OPERATING, AND LCO 3.5.3, ECCS - SHUTDOWN

Reference:

(1) Letter from NMC to NRC dated September 12, 2002 (2) Letter from NMC to NRC dated March 27, 2003 In reference (1), Nuclear Management Company, LLC (NMC), submitted a request for an amendment to the Technical Specifications (TS), in accordance with the provisions of 10 CFR 50.90, for Point Beach Nuclear Plant (PBNP), Units 1 and 2. The purpose of the proposed amendment was to revise TS 3.5.2, ECCS - Operating, and TS 3.5.3, ECCS - Shutdown, to add a surveillance to verify the emergency core cooling system (ECCS) piping is full of water every 31 days. This proposed amendment was consistent with NUREG-1431, Standard Technical Specifications, Westinghouse Plants, Revision 2. Supplement 1 to the original submittal was provided in Reference (2). Based on a potential for incorrectly interpreting the originally proposed requirement, that supplement proposed clarifying changes to the TS Bases.

During a conference call between the Nuclear Regulatory Commission (NRC) and NMC on May 15, 2003, NRC staff requested additional information regarding aspects of the proposed amendment. Attachment I to this letter provides our response to the staff's questions. The Bases for the proposed TS were enhanced to incorporate aspects of the additional information being provided. Attachment II provides the revised TS Bases. The originally proposed TS is unchanged. Enclosures (a), (b) and (c) provide supporting information for the staff's questions.

NMC requests approval of the proposed license amendment by November 2003, with the amendment being implemented within 45 days. The approval date was administratively selected to allow for NRC review but the plant does not require this amendment to allow continued safe full power operation.

In accordance with 10 CFR 50.91, a copy of this application, with attachments, is being provided to the designated Wisconsin Official.

6590 Nuclear Road

  • Two Rivers, Wisconsin 54241 Telephone: 920.755.2321

NRC 2003-0050 Page 2 I declare under penalty of perjury that the foregoing is true and correct.

Execyted,os May 30, 2003.

JG/kmd Attachments: I Response to Request for Additional Information 11 Revised Technical Specification Bases Pages

Enclosures:

(a) Westinghouse Electric Company, Nuclear Safety Advisory Letter NSAL-02-6 (b) PBNP Piping and Isometric Drawings, Auxiliary Coolant System (c) PBNP RHR Pump Assembly Drawing cc: (w/o enclosures)

Project Manager, Point Beach Nuclear Plant, NRR, USNRC Regional Administrator, Region 111, USNRC NRC Resident Inspector - Point Beach Nuclear Plant PSCW

NRC 2003-0050 Attachment I Page 1 of 4 ATTACHMENT I RESPONSE TO REQUEST FOR ADDITIONAL INFORMATION LICENSE AMENDMENT REQUEST 229, SUPPLEMENT 2 TECHNICAL SPECIFICATION LCO 3.5.2, ECCS - OPERATING, AND LCO 3.5.3, ECCS - SHUTDOWN POINT BEACH NUCLEAR PLANT, UNITS I AND 2

NRC 2003-0050 Attachment I Page 2 of 4 1.0 RESPONSE TO REQUEST FOR ADDITIONAL INFORMATION License Amendment Request (LAR) 229 was made pursuant to 10 CFR 50.90 to modify Technical Specification (TS) 3.5.2, ECCS - Operating and TS 3.5.3, ECCS - Shutdown, to add a surveillance to require verification that the Emergency Core Cooling System (ECCS) piping is full of water every 31 days.

The following information is provided in response to the Nuclear Regulatory Commission staff's request for additional information during a telephone conference on May 15, 2003. The staff's questions pertained to Supplement I to LAR 229, dated March 27, 2003. The questions are restated with NMC's response following.

NRC Question 1. Residual Heat Removal (RHR) pumps In page 4 of Attachment 1, you stated that RHR (residual heat removal) pump casings do not need to be vented because they are at system low points and because of their configuration.

What is the location of the high point vents with the capability of venting the RHR pumps? Do you have any diagrams and/or information that will help us to understand the venting system?

NMC Response Enclosures (b) and (c) to the letter transmitting this response provide Piping and Isometric Drawings of the Point Beach Nuclear Plant (PBNP) Auxiliary Coolant System and a RHR pump assembly drawing. The RHR pump casings are at the system low point and their configuration is such that gases are unlikely to collect there. The enclosed drawings show how the discharge volute of the RHR pump provides a direct path from the pump casing to the discharge piping.

Gases that may come out of solution within the pump casing will likely rise up out of the casing and flow into the discharge piping due to the system configuration. The high point vents on the discharge piping are located to facilitate removal of this gas. Venting the accessible ECCS piping outside containment will minimize any voids and pockets of entrained gases.

NRC Question 2. "Nominal Amount" of noncondensible gas In page 4 of Attachment 1, you mentioned that pumping a "nominal amount" of noncondensible gas into the reactor after a SI (safety injection) signal or during shutdown does not significantly affect ECCS (emergency core cooling system) performance. Please define "nominal amount" of gas, address the location of the gas, and provide the basis for your conclusion.

NMC Response The term "nominal amount" of noncondensible gas is not quantitatively defined. Rather, it is qualitatively defined as an amount of gas that is insufficient to jeopardize operation of the ECCS. A "nominal amount" of noncondensible gas would be expected to accumulate in the ECCS piping under normal plant operation between periodic venting of the system.

Enclosure (a) to the letter transmitting this response contains information regarding the likelihood of nitrogen release and entrainment in RHR piping adversely impacting system performance. Although assessed for MODE 6 reactor operation, the conclusion in that document is that RHR pump operability will not be affected by nitrogen entrained in SI accumulator discharge water. The system is tolerant of small amounts of entrained gases and the ability of the RHR pumps to provide shutdown cooling will not be affected.

NRC 2003-0050 Attachment I Page 3 of 4 Long term plant operating experience at PBNP has shown that, under normal conditions, the ordinary buildup of any gases in the ECCS system has not been sufficient to significantly affect ECCS operation. In the past, the system has been maintained in a standby mode for long periods without appreciable gas buildup (and without venting of ECCS piping). The resistance to gas accumulation in PBNP's ECCS is aided by the static head of water provided by the refueling water storage tank, which helps minimize the release of gas from solution.

Since normal standby operation does not result in buildup of excessive amounts of gas in the PBNP ECCS, periodic venting of the system is sufficient to maintain system operability without the need for quantitative measuring of gas volumes.

The proposed surveillance is only intended to ensure system operability under normal standby operation. Unlike the nominal amounts of gas that may accumulate in ECCS piping under normal conditions, operation with degraded equipment (e.g., excessive back leakage from SI accumulator check valves) introduces a potential for excessive gas buildup in a relatively short time period. Although periodic venting of the ECCS may provide an additional method of monitoring and early detection of such degradation, this surveillance is not intended for such a purpose because the 31 day periodicity of this venting is not frequent enough to identify excessive gas buildup in a timely manner. Degradation that could cause excessive gas buildup within a shorter time period than the 31 day frequency of the proposed TS (e.g., unusual decreasing levels in the SI accumulators) is more appropriately addressed via other means available as part of the PBNP corrective action process. The intent of the proposed TS is only to prevent slow, long-term gas buildup from accumulating in sufficient quantities to adversely impact pump and system operability. Periodic venting of the ECCS minimizes such gas accumulation.

Qualitative evaluation of the amount of gas vented (e.g., two seconds of venting prior to achieving a clear stream of water) is adequate for concluding that ECCS operability has not been compromised. Additionally, processes and procedures are in place (including the corrective action process) to ensure that large amounts of gas encountered during venting would be appropriately evaluated for their impact on system operability.

The proposed Bases for TS 3.5.2, ECCS - Operating, have been enhanced to incorporate the substance of the above information. The following changes are provided to the initially proposed Bases (additions shown underlined in context; deletions in strikethrough).

SR 3.5.2.2 The ECCS pumps are normally in a standby, nonoperating mode. As such, flow path piping has the potential to develop voids and pockets of entrained gases. Maintaining the St ECCS pumps and accessible portions of ECCS suction piping, including cross-connect piping to RHR, free of gas quantities that could ieopardize ECCS operabilitV suffGicent to rnder the S pump inoperable, ensures that the system will perform properly, injecting its full capacity into the RCS upon demand. This is accomplished by venting the SI pumps and accessible portions of ECCS suction piping. Performance of this SR also includes venting accessible portions of the piping from the ECCS pumps to the RCS. This will also prevent pump cavitation and minimize pumping noncondensible gas (e.g., air, nitrogen, or hydrogen) into the reactor vessel following an SI signal or during shutdown cooling. The 31 day Frequency takes into consideration the gradual nature of gas accumulation in the ECCS piping and the procedural controls goveming system operation.

NRC 2003-0050 Attachment I Page 4 of 4 The revised TS Bases more clearly delineate that periodic venting of the SI pumps and accessible portions of the ECCS piping is sufficient to demonstrate that the ECCS is sufficiently full of water to assure operability and thereby satisfy the surveillance requirement.

The installed vents in the ECCS system that are accessible from outside the containment structure provide adequate means for venting to ensure that the ECCS piping is sufficiently full of water to maintain ECCS operability. As described in Enclosure (a) to the letter transmitting this response, pumping of nominal amounts of noncondensible gas into the reactor vessel following an SI signal or during shutdown cooling does not significantly affect system performance.

2.0 ENVIRONMENTAL EVALUATION No changes to the initially proposed TS result from this additional information. Furthermore, NMC has determined that this supplement does not involve a significant hazards consideration, authorize a significant change in the types or total amounts of effluent release, or result in any significant increase in individual or cumulative occupational radiation exposure. Therefore, we conclude that the proposed amendment meets the categorical exclusion requirements of 10 CFR 51.22(c)(9) and that an environmental impact appraisal need not be prepared.

NRC 2003-0050 1 Page 1 of 4 ATTACHMENT 11 REVISED TECHNICAL SPECIFICATION BASES PAGES LICENSE AMENDMENT REQUEST 229, SUPPLEMENT 2 TECHNICAL SPECIFICATION LCO 3.5.2, ECCS - OPERATING, AND LCO 3.5.3, ECCS - SHUTDOWN POINT BEACH NUCLEAR PLANT, UNITS I AND 2

ECCS - Operating B 3.5.2 BASES ACTIONS (continued) An event accompanied by a loss of offsite power and the failure of an EDG can disable one ECCS train until power is restored. A reliability analysis (Ref. 5) has shown that the impact of having one full ECCS train inoperable is sufficiently small to justify continued operation for 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

With more than one component inoperable such that both ECCS trains are not available, the facility is in a condition outside design and licensing basis. Therefore, LCO 3.0.3 must be immediately entered.

B.1 and B.2 If the inoperable trains cannot be returned to OPERABLE status within the associated Completion Time, the plant must be brought to a MODE in which the LCO does not apply. To achieve this status, the plant must be brought to MODE 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and MODE 4 within 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

The allowed Completion Times are reasonable, based on operating experience, to reach the required plant conditions from full power conditions in an orderly manner and without challenging plant systems.

SURVEILLANCE SR 3.5.2.1 REQUIREMENTS Verifying the correct alignment for manual, power operated, and automatic valves in the ECCS flow paths provides assurance that the proper flow paths will exist for ECCS operation. This SR does not apply to valves that are locked, sealed, or otherwise secured in position, since these were verified to be in the correct position prior to locking, sealing, or securing. A valve that receives an actuation signal is allowed to be in a non-accident position provided the valve will automatically reposition within the proper stroke time. This Surveillance does not require any testing or valve manipulation. Rather, it involves verification that those valves capable of being mispositioned are in the correct position. The 31 day Frequency is appropriate because the valves are operated under administrative control, and an improper valve position would only affect a single train. This Frequency has been shown to be acceptable through operating experience.

SR 3.5.2.2 The ECCS pumps are normally in a standby, nonoperating mode. As such, flow path piping has the potential to develop voids and pockets of entrained gases. Maintaining the ECCS pumps and accessible portions of ECCS suction piping, including cross-connect piping to RHR, free of gas quantities that could jeopardize ECCS operability, ensures that the system will perform properly, injecting its full capacity into the RCS Point Beach B 3.5.2-6 Unit 1 - Amendment No.

Unit 2 - Amendment No.

ECCS - Operating B 3.5.2 BASES SURVEILLANCE upon demand. This is accomplished by venting the SI pumps and REQUIREMENTS accessible portions of ECCS suction piping. Performance of this SR (continued) also includes venting accessible portions of the piping from the ECCS pumps to the RCS. This will also prevent pump cavitation and minimize pumping noncondensible gas (e.g., air, nitrogen, or hydrogen) into the reactor vessel following an SI signal or during shutdown cooling. The 31 day Frequency takes into consideration the gradual nature of gas accumulation in the ECCS piping and the procedural controls goveming system operation.

SR 3.5.2.3 Periodic surveillance testing of ECCS pumps to detect gross degradation caused by impeller structural damage or other hydraulic component problems is required by the ASME Code. This type of testing may be accomplished by measuring the pump developed head at only one point of the pump characteristic curve. This verifies both that the measured performance is within an acceptable tolerance of the original pump baseline performance and that the performance at the test flow is greater than or equal to the performance assumed in the plant safety analysis. SRs are specified in the Inservice Testing Program, which implements the requirements of the ASME OM Code, providing the activities and Frequencies necessary to satisfy the requirements.

SR 3.5.2.4 and SR 3.5.2.5 These Surveillances demonstrate that each automatic ECCS valve actuates to the required position on an actual or simulated SI signal and that each ECCS pump starts on receipt of an actual or simulated SI signal. This Surveillance is not required for valves that are locked, sealed, or otherwise secured in the required position under administrative controls. The 18 month Frequency is based on the need to perform these Surveillances under the conditions that apply during a plant outage and the potential for unplanned plant transients if the Surveillances were performed with the reactor at power. The 18 month Frequency is also acceptable based on consideration of the design reliability (and confirming operating experience) of the equipment. The actuation logic is tested as part of ESF Actuation System testing, and equipment performance is monitored as part of the Inservice Testing Program.

Point Beach B 3.5.2-7 Unit 1 - Amendment No.

Unit 2 - Amendment No.

ECCS - Operating B 3.5.2 BASES SURVEILLANCE SR 3.5.2.6 I REQUIREMENTS (continued) Periodic inspections of the containment sump suction inlet ensure that it is unrestricted and stays in proper operating condition. The 18 month Frequency is based on the need to perform this Surveillance under the conditions that apply during a plant outage, and on the need to have access to the location. This Frequency has been found to be sufficient to detect abnormal degradation and is confirmed by operating experience.

REFERENCES 1. FSAR, Section 6.1.1.

2. 10 CFR 50.46.
3. FSAR, Section 6.2.1.
4. FSAR, Chapter 14, "Accident Analysis."
5. NRC Memorandum to V. Stello, Jr., from R.L. Baer, "Recommended Interim Revisions to LCOs for ECCS Components,"

December 1, 1975.

Point Beach B 3.5.2-8 Unit 1 - Amendment No.

Unit 2 - Amendment No.

ENCLOSURES to NRC 2003-0050 (a). Westinghouse Electric Company, Nuclear Safety Advisory Letter NSAL-02-6, Nitrogen Release to RHR During SI Accumulator Low Pressure Blowdown Tests, Dated 4/8/02 (b). PBNP Piping and Isometric Drawings, Auxiliary Coolant System (9 pages)

(c). PBNP RHR Pump Assembly Drawing

Nuclear Safety \./

> Westinghouse Electric Company Advisory Letter This is a notification of a recently identified potenti3t safety issue pertaining to basic components supplied by Westinghoise.

This information is being provided to you so that a review of this issue can be conducted by you to determine if any action is required.

P.O. Box 355, Pittsburgh, PA 15230

Subject:

Nitrogen Release to RHIR Durin SI Accumulator Lov Number: NSAL-02-6 Pressure Blowvdovii Tests Basic Component: RIIR Pump lDate: 4/8/02 Plants: D. C. Cook Units I andi 2. Comaicie Peak Units I and 2, Millstone 3, Farley Units I and 2, Vogtle Units and 2, South Texas Units I and 2, Virgil Sutimer Substantial Safety Hazard or Failure to Comply Pursuant to 10 CFR 21.21(a) Yes O No O Transfer of Information Pursuant to 10 CFR 21.21(b) Yes E Advisory Information Pursuant to 10 CFR21.21(d)(2) Yes ]

References:

OE12618, OE10468

SUMMARY

Many plants veriFy thc operability of the safety injection accumUlator discharge check valves by a low pressure blowdown test desigicd to stroke the check valvcs to the full open position.

Reccntly, two opcrating event reports (OE 126 18 and OE 10468) wvere issued to address nitrogen introduction into the RCS during thesc tests. The reports concluded that the nitrogen came out of solution from the water that was injected during the test. Whcn the test is performed with fuel in the core, the risk to RHR pump operability for shutdown cooling may represent a safety concerni.

In response to tle recent operating reports, Westinghouse has examined the likelihood of nitrogen release and entrainment into the RIR suction piping and has concluded that perforning this test in MODE 6 with the reactor vcssel head removecl loes not pose a significant risk to RHR ptmp operability for shutdown cooling with fuel in the core.

Adrlitinnil infnrmqtinn if rrniiiired. may he nhtainri from the originator. Telephone (412) 374-4139.

Originator: S. R. Swianter, I-l. A. Sepp, .anager Systems and Equipment Engineering Rcgulatory & Licensing Engineering Official rccord electronically approved in ED-IS 2000

NSAL-02-6 Page 2 of 3 ISSUE DESCRIPTION The NRC requires plants to verify safetv injection accuimlulzator discharge cieck valve operability by either valve disassembly or full flow testing. Many plants verify the operabilitv of the check valves b a low presstire blowdoli test designed to stroke the check valves to the full open position. WVstinghouse has provided en-ineering reports and safety evaluations for several plants in the developmenlt of such tests.

Two operating event reports (OE 261S and OE1046S) werc issued by INPO to address nitrogen introduction into the RCS dLuring these tests. Both plants concluded that the nitrogen came out of solution from the water that was injected during the test. Nitrogen rclease into the RCS by this mcclanism was not considered in any of the engineering and safety evaluations performed by Westinghouse.

TECHNICAL EVALUATION Westinghouse has evaluated the potential impact on RI-R operability of nitrogen being released into the RCS during a low pressure ( 25 psig) blowdown test performed in Mode 6 with the reactor vessel head removed and the reactor cavity flooded. The cvaluation assumed that sufficient timc was allowed for the nitrogen content in the water to come into equilibrium at the test pressure. The Westinghouse evaluation used test and system parameters for a reference plant. Although parameters would be plant specific, conditions are expected to be similar for other affected plants. The Westinghouse evaluation determined that there are four lines of cefense which protect the nitrogeni from advcrsely impacting the RTIR system. Thcse lines of defense are described below along witl the results and conclusions of the evaluation.

The first linc of defense is the fact that most of the nitrogen wlhich enters the reactor vesscl will be transported into the reactor cavity as opposed to entering the RCS hot leg. Each safety injection accumulator discharges into a separate reactor coolant system cold leg. The flow then enters the reactor vessel downcomer and flotvs upward through the vessel. The vast majority of nitrogcl released from solution is expected to flow up through the reactor vessel and into the reactor cavity during the test. This is due to the fact that the nitrogen is distributed throughout the cntire reactor vessel flow stream. Therefore, most of the flov is from the reactor vessel into the rcactor cavity since the accumulator flow rate is typically greater than the RHR flow rate. Only the flow supplied to the RHR puilip enters the hot leg, the remainder of the flov enters the reactor cavity.

The naximun nitrogcn cntrained in the vessel flow rate after mixing witli the RHRS flow (3000 gpm) is 11%

by volume. This is higher than the recommended limits (3%) ptblished in NUREG/CR-2792. However, only a small fraction of this has the potential for entering the RCS hot leg.

The second line of defcnse is the fact that not all of thc nitrogcn cntrainect in the vater wvhich enters the RCS liot leg will enter the RIlR intake pipe. The RI-IR intake pipc is typically located several feet down stream of the hot leg inlet. In adclition, the RIR intake is located on the lower half of the hot leg. As the water flows in the hot eg toward the RHR intake pipe, the nitrogen bubbles will rise to the top of the hot leg. The ability of the flow stream to transport bubblcs wvhich collect at the top of the hot leg is predicted by the flow strcam Froude numllber. The Froude number provides an indication of the magnitude of the inertial force relative to the gravitational forcc in the flow stream. Thc flow characteristics (Frolde No. much less than I) of the hot leg are such that nitrogen will collect in the top of the hot leg ancl not bc carried along vith the flow stream.

The flov velocity in the hot leg is less than 2 ftsec vith onlv thc R[-IR putmp operating (riot a Rcactor CeoŽ!:an! PI, pl). T trq,,.c"nt tl' nf o I, flrn t t,r ,,,1 P tmt t! l, Rt-rQ intaIa i Q.'vi'r I sec,ns Therefore, only nitrogen bubblcs which are very small (diamctcr < 0.014 inch) have the potential to be carried into the RHR intake. Bubbles of larger sizc will have adequate time to rise to the upper half of the hot leg and collect at the top of the hot lcg. Thus the hot leg acts as a buffer to collect nitrogeni bubbles which enter the hot leg and excludes them from entering the RI-IR intakc. Therefore, the percent volume of nitrogcn cntrained in the fluid will be reduced as the fluid travels downii the hot leg. In addition, the hot leg vents to the

NSAL- 02-6 Page 3of3 stean gencrator and reactor vessel. The RIR intatke is from the lower half of the hot cg. Therefore, the hot lecg cannot be filcdl with nitrogen, suchI that it is forced into the RHR intake. This prevents any large bubbles ot nitrogen from being drawn into the RH R intakc.

The third line of defense is the fact that the lot lea limits the size of the bubble which can enter the RHR intake to a very small size. This significantly reduces the potential adverse impact on the RHR purmp. Very small bubbles will be transported with the ovv stream and would tend to cushiion the flow rather than starve, or bind the flow throughl the RHR pump.

The fourth line of defense is the fact that the flow characteristics (Froude No. > 1) of the RHR intake flow rate (3000 gpm) are such that any nitrogen bubbles entrained in the intake flow rate will be carried along with the flow stream and will not collect at local high points. This eliminates the potential for any entrained air to have an adversc effect on the pump or system.

SAFETY SIGNIFICANCE A potential safcty concern may exist if the nitrogen released into the RCS during a low pressure blowdown test limits RHR pump operability so as to affect shutdovn cooling required while fuel is in the core. The above evaluation concludes that RHR pump operability villi not be affected by the nitrogen entrained in the accumulator discharge water. Therefore, the ability of the RHR pumps to provide shutdown cooling will not be affected.

NRC AWARENESS The NRC has not been made aware of this issuc.

RECOMMENDED ACTIONS This NSAL is applicable to plants which verify operability of the safety injection accumulator check valves by a low pressure blow down test perfonned in MODE 6 with the reactor vessel head removed with fuel in the reactor core. Affected plants should review their tcst proccedlures and configuration and cvaluate the impact on shutdown corc cooling irnposed by the test.

This document is available via the Internet at svvw.rIe.westinghouse.com. This site is a free service of Westinghouse Electric Co. but requires specific access through a firewall. Requests for access should be made to kleinwdri vestin"Iiouse.com.

joc.lrt~ !C~ZS~O4 KIZ 8s I 2 j CE 0TJ 0 . 4 02 1 no".

_T ,,, ,  !

I ITgrM-0 GGW .

CAWrtr, I--

nt FSw^ I Iio SIL3

.l 0 .5550 O!0"I 5I I 5 0.

PAOI . MrG O01IN@0'. 50 F. = .

_ -rl

~~~~~~;;

wt ctscso PM

  • f17

_ _,1 r^.Es,;Zvl 1bs- > 1 zv s s _

I' CAD CW,O w.="V . R c W ,il .I . 0 S 0 0

  • .o. 2075 0.

, o. is, rt, S0.O=. 10st3oL @0r @0,1 0..

MA5 555(. A w0t.5A5.S 1 sszJ l 'C,. 5am El" ,W. I PACIFIC PUMPS DIVISIbN DRESSER IDUSTRIES. INC.

PUMP ASSEMBLY rt V . I P45 WOI i. -I0

. 5C0- P45250 . I.

I I I I S I . I w

,^.}%.., " _ _,;n Bq-1 3- 'IjL 1, . jAIR146(1, 10 410S 30