ML030770577
| ML030770577 | |
| Person / Time | |
|---|---|
| Site: | Cook |
| Issue date: | 03/14/2003 |
| From: | Greenlee S Indiana Michigan Power Co |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| AEP:NRC:2691-28 | |
| Download: ML030770577 (8) | |
Text
Indiana Michigan Power Company 500 Circle Drive Buchanan, MI 49107 1395 INDIA NA MICHIGAN POWER March 14,2003 AEP:NRC:2691-28 Docket Nos.
50-315 50-316 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Mail Stop O-P1-17 Washington, DC 20555-0001 Donald C. Cook Nuclear Plant Units 1 and 2 MONTHLY OPERATING REPORT Pursuant to the requirements of Donald C. Cook Nuclear Plant Unit 1 and Unit 2 Technical Specification 6.9.1.8, the attached Monthly Operating Report for February 2003 is submitted.
Sincerely, Scot A. Greenlee Director, Nuclear Technical Services BWO/jen Attachments
U. S. Nuclear Regulatory Commission Page 2 c: ANI Nuclear Engineering Department A. C. Bakken, III L. Brandon - Department of Health M. J. Finissi G. T. Gaffney - Canton S. A. Greenlee S. Hamming - Department of Labor RAF Harris INPO Records Center B. Lewis - McGraw-Hill Companies D. H. Malin K. L. Matheny B. A. McIntyre NRC Project Manager - NRR NRC Region III NRC Resident Inspector D. W. Paul - Columbus J. E. Pollock W. H. Schalk AEP:NRC:2691-28
N.R.C. OPERATING DATA REPORT DOCKET NO.
50-315 DATE 3/5/03 COMPLETED BY RAF Harris TELEPHONE 269-465-5901 OPERATING STATUS
- 1. Unit Name D.C. Cook Unit 1 Notes:
- 2. Reporting Period Feb-03
- 3. Licensed Thermal Power (MWt) 3304
- 4. Name Plate Rating (Gross MWe) 1152
- 5. Design Electrical Rating (Net MWe) 1020
- 6. Maximum Dependable Capacity(GROSS MWe) 1056
- 7. Maximum Dependable Capacity (Net MWe) 1000
- 8. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since Last Report Give Reasons
- 9. Power Level To Which Restricted. If Any (Net MWe)
- 10. Reasons For Restrictions.
This Mo.
Yr. to Date
- 11. Hours in Reporting Period 672.0 1416.0
- 12. No. of Hrs. Reactor Was Critical 595.0 951.2
- 13. Reactor Reserve Shutdown Hours 0.0 0.0
- 14. Hours Generator on Line 573.4 929.6
- 15. Unit Reserve Shutdown Hours 0.0 0.0
- 16. Gross Therm. Energy Gen. (MWH) 1851712.3 3017344.5
- 17. Gross Elect. Energy Gen. (MWH) 597760.0 979450.0
- 18. Net Elect. Energy Gen. (MWH) 577591.8 946750.5
- 19. Unit Service Factor 85.3 65.6
- 20. Unit Availability Factor 85.3 65.6
- 21. Unit Capacity Factor (MDC Net) 86.0 66.9
- 22. Unit Capacity Factor (DER Net) 84.3 65.5
- 23. Unit Forced Outage Rate 14.7 34.4
- 24. Shutdowns Scheduled over Next Six Months (Type,Dateand Duration):
Cumm.
246864.0 168299.8 463.0 165618.5 321.0 493286419.1 160221880.0 154221947.0 67.6 67.6 63.9 62.7 19.3
- 25. If Shut Down At End of Report Period, Est'd Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO.
UNIT DATE COMPLETED BY TELEPHONE 50-315 ONE 05-Mar-03 RAF Harris 269-465-5901 MONTH Feb-03 AVERAGE DAILY POWER LEVEL DAY 0
0 0
0 362 886 1026 1036 1040 1037 1037 1040 1037 1047 1047 1031 AVERAGE DAILY POWER LEVEL 2/17/03 2/18/03 2/19/03 2/20/03 2/21/03 2/22/03 2/23/03 2/24/03 2/25/03 2/26/03 2/27/03 2/28/03 1040 1034 1041 1041 1037 1039 1038 1019 1042 1040 1044 1028 DAY 2/1/03 2/2/03 2/3/03 2/4/03 2/5/03 2/6/03 2/7/03 2/8/03 2/9/03 2/10/03 2/11/03 2/12/03 2/13/03 2/14/03 2/15/03 2/16/03
DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE PAGE 50-315 D.C. Cook Unit 1 March 7, 2003 B. O'Rourke 269-465-5901 1 of 1 UNIT SHUTDOWNS AND POWER REDUCTIONS - February 2003 METHOD OF SHUTTING LICENSEE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO.
DATE TYPE1 HOURS REASON 2 REACTOR 3 REPORT NO.
CODE4 CODE5 TO PREVENT RECURRENCE 347 030115 F
77.0 A
3 315/2003-001 EL XFMR The unit was shutdown due to a fault and subsequent fire in the Unit 1 main transformer. The cause of the fault is under investigation. The main transformer has been replaced. Actions to prevent recurrence will be identified once the cause of the transformer fault is known.
t" AD KMIN:KlT, 1 TYPE:
F: Forced S: Scheduled 2 REASON:
A: Equipment Failure (Explain)
B: Maintenance or Test C: Refueling D: Regulatory Restriction E: Operator Training and License Examination F: Administrative G: Operational Error (Explain)
H: Other (Explain) 3 METHOD:
1: Manual 2: Manual Scram 3: Automatic Scram 4: Other (Explain)
Exhibit G - Instructions for preparation of data entry sheets for Licensee Event Report (LER) File (NUREG 0161)
Exhibit I: Same Source
N.R.C. OPERATING DATA REPORT DOCKET NO.
50-316 DATE 315/03 COMPLETED BY RAF Harris TELEPHONE 269-465-5901 OPERATING STATUS
- 1. Unit Name D.C. Cook Unit 2 Notes:
- 2. Reporting Period Feb-03
- 3. Licensed Thermal Power (MWt) 3411
- 4. Name Plate Rating (Gross MWe) 1133
- 5. Design Electrical Rating (Net MWe) 1090
- 6. Maximum Dependable Capacity(GROSS MWe) 1100
- 7. Maximum Dependable Capacity (Net MWe) 1060
- 8. If Changes Occur in Capacity Ratings (Items no. 3 through 7) Since Last Report Give Reasons
- 9. Power Level To Which Restricted. If Any (Net MWe)
- 10. Reasons For Restrictions.
This Mo.
- 11. Hours in Reporting Period 672.0
- 12. No. of Hrs. Reactor Was Critical 475.4
- 13. Reactor Reserve Shutdown Hours 0.0
- 14. Hours Generator on Line 450.8
- 15. Unit Reserve Shutdown Hours 0.0
- 16. Gross Therm. Energy Gen. (MWH) 1493985.3
- 17. Gross Elect. Energy Gen. (MWH) 493750.0
- 18. Net Elect. Energy Gen. (MWH) 478279.9
- 19. Unit Service Factor 67.1
- 20. Unit Availability Factor 67.1
- 21. Unit Capacity Factor (MDC Net) 67.1
- 22. Unit Capacity Factor (DER Net) 65.3
- 23. Unit Forced Outage Rate 32.9
- 24. Shutdowns Scheduled over Next Six Months (Type,Date,and Duration):
RpfiiPlinn noifqnti Qrhrfli Ipd fnr Myv 9(0.'A r.to Date 1416.0 1140.6 0.0 1105.1 0.0 3678943.6 1216840.0 1178905.8 78.0 78.0 78.5 76.4 22.0
- 25. If Shut Down At End of Report Period, Est'ed Date of Startup:
- 26. Units in Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAL ELECTRICITY COMMERCIAL OPERATION Cumin.
221010.0 142708.7 0.0 138845.6 0.0 434902640.9 140990540.0 135931645.1 63.5 63.5 59.2 57.6 23.8
AVERAGE DAILY POWER LEVEL (MWe-Net)
DOCKET NO.
UNIT DATE COMPLETED BY TELEPHONE 50-316 TWO 5-Mar-03 RAF Harris 269-465-5901 MONTH Feb-03 AVERAGE DAILY POWER LEVEL 1102 1099 1099 1096 960 0
0 0
0 0
0 0
0 0
367 977 DAY 2/17/03 2/18/03 2/19/03 2/20/03 2/21/03 2/22/03 2/23/03 2/24/03 2/25/03 2/26/03 2/27/03 2/28/03 AVERAGE DAILY POWER LEVEL 1105 1099 1103 1100 1106 1099 1110 1089 1112 1101 1105 1100 DAY 2/1/03 2/2/03 2/3/03 2/4103 2/5/03 2/6/03 2/7/03 2/8/03 2/9/03 2/10/03 2/11/03 2/12/03 2/13/03 2/14/03 2/15/03 2/16/03
DOCKET NO.
UNIT NAME DATE COMPLETED BY TELEPHONE PAGE 50-316 D.C. Cook Unit 2 March 7, 2003 B. O'Rourke 269-465-5901 1 of 1 UNIT SHUTDOWNS AND POWER REDUCTIONS - February 2003 METHOD OF SHUTTING LICENSEE DURATION DOWN EVENT SYSTEM COMPONENT CAUSE AND CORRECTIVE ACTION NO.
DATE TYPE1 HOURS REASON2 REACTOR3 REPORT NO.
CODE' CODE5 TO PREVENT RECURRENCE 210 030205 F
196.6 A
3 316/2003-002 SJ JX Unit 2 turbine/reactor trip from 100% due to a dual failure of the 24 VDC power supplies in control group 3. The cause of the power supply failure is under investigation. The power supplies have been replaced and the unit was returned to service. Actions to prevent recurrence will be identified once the cause of the failure is known.
211 030214 F
0.0 A
4 n/a n/a n/a The Unit 2 turbine was manually tripped due to a high-high level in the moisture separator drain Tank (MSDT). The MSDT alternate level control valve was repaired and the generator was synchronized to the grid on February 15,2003 at 0302 hours0.0035 days <br />0.0839 hours <br />4.993386e-4 weeks <br />1.14911e-4 months <br />. The cause of the valve failure is under Investigation.
- 4.
- 5=5bM 3
uuI -
L
- sJ1r'J*
In I:
n 1 TYPE:
F: Forced S: Scheduled 2 REASON:
A: Equipment Failure (Explain)
B: Maintenance or Test C: Refueling D: Regulatory Restriction E: Operator Training and License Examination F: Administrative G: Operational Error (Explain)
H: Other (Explain) 3 METHOD:
1: Manual 2: Manual Scram 3: Automatic Scram 4: Other (Explain) 4 SYSTEM:
Exhibit G - Instructions for preparation of data entry sheets for Licensee Event Report (LER) File (NUREG 0161)
Exhibit I: Same Source