ML030070208
| ML030070208 | |
| Person / Time | |
|---|---|
| Site: | Crystal River |
| Issue date: | 04/03/2002 |
| From: | - No Known Affiliation |
| To: | Office of Nuclear Reactor Regulation |
| References | |
| FOIA/PA-2003-0059 | |
| Download: ML030070208 (1) | |
Text
For Information Only.
CR3 Crystal River Nuclear Facility Summary Report - NCRs Initiated Since 3127102 Sorted by Origination Date, Ar Number, Priority Selection Cnteria. AR Type = NCR and AR Status not = Canceled with Attribute of 1A POTL OPER/REPORT AR#
Originator AR Subject Orig. Date AR Status Priority Potential Oper/Report NCR Owner 00058555 PAUL GILMAN WBSB-2 QUICK CONNECTS WILL NOT 20020401 APPROVED 2
N CR3 MAINTENANCE ENGAGE UNIT EVALUATOR GROUP WHILE PERFORMING STEP 4.1.5 OF PT-160A, THE CHEMISTRY TECH WAS UNABLE TO ENGAGE THE WSSB-2 QUICK CONNECTS.
THIS EQIP MENT IS REQUIRED TO MEET NUREG 0737 AND REGULATORY GUIDE 1. 97 COMMITMENTS FOR PASS.
W/R 44398 WRITTEN.
00058558 AUGUST DOWLING NAS C-SC-02-01, SS-307 ON ADMIN HOLD 20020401 APPROVED 5
N CR3 SECURITY UNIT EXCESSIVE TIME GROUP DURING NAB C-SC-02-01,A FINDING RESULTED DUE TO SECURITY PR OCEDURE SS-307 BEING ON HOLD SINCE JULY 24, 2001.
SS-307 W AS REPLACED WITH A SERIES OF CSP-NGGC'S PROCEDURES.
SS-307 NEEDS TO BE CANCELLED.
00058559 DANIEL JOPUNG RWH-36
& 73 DO NOT MEET CODE REQUIREMENTS BUT ARE OPERABLE 20020401 COMPLETE 2
N CR3 ENIiINEEHINLi N
CR3 ENGINEERI*NG DESIGN UNIT EVAL GROUP CALCULATIONS M-74-0009 RWH-36 AND RWH-73 AND DETERMINED THE Y ARE OPERABLE ONLY.
THIS CALCULATION WAS DEVELOPED AS PAR T OF THE LARGE BORE PIPING PROGRAM.
THE IDENTIFICATION OF SUPPORTS THAT ARE NOT FULLY QUALIFIED TO THE CR-3 LICENSING BASES WAS AN EXPECTED RESULT OF THE PROGRAM.
THE OPERABIL IT:Y DETERMINATION WAS IN ACCORDANCE WITH MDG-002, WHICH IS BASED ON GL 91-18, AND IEBIS 79-02 AND 79-14.
THE LBPP DEV ELOPED DR-JCO 97-0048 WHICH PROVIDED A GENERIC ASSESSMENT 0 F ANTICIPATED SUPPORT NON-CONFORMANCES.
00058572 ANTHONY WASHINGTON PRESSURISER LEVEL CONTROL NOT RESPONDING ADEQUATELY.
20020401 APPROVED Z
N
iwIJ AFTER MAKING A HYDROGEN ADDITION TO THE MUT THE PRESSURISER LEVEL FELL TO 209 & THE MUT LEVEL INCREASED ACCORDINGLY WH ILE IN AUTO WITH SETPOINT AT220.
ONCE THE LEVEL RECOVERED I T WAS CONTROLING LOW AT 214.
THE RO ADUSTED SETPOINT UP AND THEN HAD TO ADJUST THE SETPOINT BACK TO THE ORIGINAL 220 SETPOINT TO HAVE MUV-31 CONTROL LEVEL AT 220.
00058575 GUY MCCALLUM HEALTHY SEA TURTLES RESCUED FROM BAR RACKS 20020401 APPROVED I
Y CR3 E&RC HADIATIUN Y
CR3 E&RC RADIATION CONTROL UNIT EVAL GRP A LIVE HEALTHY TURTLE WAS RESCUED FROM THE INTAKE BAR RACKS SITE SECURITY NOTIFIED THE CONTROL ROOM OF THE RESCUE AT 1940 ON 4/01/02.
THE TURTLE HAS BEEN TRANSPORTED TO THE M ARICULTURE CENTER FOR IDENTIFICATION.
2 2UPDATE: 2AN ADDITI ONAL TURTLE HAS BEEN RESCUED FROM THE BAR RACKS.
SITE SECU RITY NOTIFIED THE CONTROL ROOM OF THE RESCUE OF THE SECOND TURTLE AT 2120 ON 4/01/02.
THE TURTLE HAS BEEN TRANSPORTE D TO THE MARICULTURE CENTER FOR IDENTIFICATION.
Run Date/Trme:
4/3/02 4:07:29 AM Report Name: RpLATNCRslntLast7a_CR3, Created from SrceThlAT_NCRsindtLast7a UNITEVAL Page 11 of 13 N
20020401 APPROVED 2