ML020440131

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December 2001 Monthly Operating Report for Nine Mile Point, Unit 2
ML020440131
Person / Time
Site: Nine Mile Point Constellation icon.png
Issue date: 01/11/2002
From: Peckham M
Constellation Nuclear
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
NMP2L 2045
Download: ML020440131 (4)


Text

P.O. Box 63 Lycoming, New York 13093 Constellation Nuclear Nine Mile Point Nuclear Station A Member of the Constellation Energy Group January 11, 2002 NMP2L 2045 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555 RE:

Nine Mile Point Unit 2 Docket No. 50-410 NPF-69 Monthly Operating Report for December 2001 Gentlemen:

Submitted herewith is the Operating Data Report, the Unit Shutdowns, and Summary of Operating Experience for December 2001.

Very truly yours, Unit 2 Plant General Manager MFP/cld Attachments cc:

Mr. H. J. Miller, NRC Regional Administrator, Region I Mr. G. K. Hunegs, NRC Senior Resident Inspector Records Management

Subject:

NIAGARA MOHAWK POWER CORPORATION NINE MILE POINT NUCLEAR STATION UNIT #2

SUMMARY

OF OPERATING EXPERIENCE Nine Mile Point Unit Two operated with a capacity factor (MDC) of 77.21% and an availability factor of 78.24% for the month of December 2001.

On December 2nd at 1449 hours0.0168 days <br />0.403 hours <br />0.0024 weeks <br />5.513445e-4 months <br />, Unit 2 was manually scrammed from approximately 75% power following an electrical fault and trip of the "A" reactor feedwater pump. The reactor was brought critical at 1132 hours0.0131 days <br />0.314 hours <br />0.00187 weeks <br />4.30726e-4 months <br /> on December 5h and the main turbine was placed in service at 1922 hours0.0222 days <br />0.534 hours <br />0.00318 weeks <br />7.31321e-4 months <br /> on December 6t. Full power operation was achieved by 2048 hours0.0237 days <br />0.569 hours <br />0.00339 weeks <br />7.79264e-4 months <br /> on December 7h. A planned power reduction to approximately 80% power was performed starting at 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> on December 8" to perform a rod pattern adjustment related to plant startup. Full power operation was again resumed by 0843 hours0.00976 days <br />0.234 hours <br />0.00139 weeks <br />3.207615e-4 months <br /> the same day.

On December 15th at 2046 hours0.0237 days <br />0.568 hours <br />0.00338 weeks <br />7.78503e-4 months <br />, Unit 2 was manually scrammed from approximately 60% power following indication of increased reactor coolant leakage of 5.87 gpm. A plant shutdown because of the increased leakage was in progress at the time of the manual scram. The source of the leakage was failed packing of 2RCS*MOV18A. The reactor was brought critical at 1958 hours0.0227 days <br />0.544 hours <br />0.00324 weeks <br />7.45019e-4 months <br /> on December 17tb and the main turbine was placed in service at 1007 hours0.0117 days <br />0.28 hours <br />0.00167 weeks <br />3.831635e-4 months <br /> on December 18h. Full power operation was achieved by 1135 hours0.0131 days <br />0.315 hours <br />0.00188 weeks <br />4.318675e-4 months <br /> on December 19k". A planned power reduction to approximately 82% power was performed starting at 1900 hours0.022 days <br />0.528 hours <br />0.00314 weeks <br />7.2295e-4 months <br /> on December 19'h to perform a rod pattern adjustment related to plant startup. Full power was again resumed by 0109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> on December 20, 2001 There were no challenges to the safety relief valves during this reporting period.

Reason:

A-Equipment Failure (Explain)

B-Maintenance or Test C-Refueling D-Regulatory Restriction E-Operator Training & License Exam F-Administrative G-Operational Error (Explain)

H-Other (Explain)

UNIT SHUTDOWNS APPENDIX B REPORTING PERIOD - December 2001 Prepared by: T. McMahon DOCKET NO: 50-410 UNIT NAME: NMP#2 DATE: 20020108 TELEPHONE: (315) 349-4045 Method:

1-Manual 2-Manual Trip/Scram 3-Automatic Trip/Scram 4-Continuation 5-Other (Explain)

Duration Method of Cause & Corrective Actions No.

Date Type (Hours)

Reasons Shutting Down' Comments F:Forced S: Scheduled 01-06 011202 F

100.55 A

2 Feedpump "A" motor windings failure. Inspection of "B" & "C" motor windings. "A" motor sent for rewinding.

01-07 011215 F

61.35 A

2 Failed packing of valve 2RCS*MOV18A caused high coolant leakage. Valve was repacked.

OPERATING DATA REPORT DOCKET NO.: 50-410 DATE: 20020108 PREPARED BY: T. McMahon TELEPHONE: (315) 349-4045 OPERATING STATUS

1.

2.

Unit Name:

Reporting Period:

Design Electrical Rating (MWe)

Maximum Dependable Capacity (Net MWe):

3. Number of Hours Reactor was Critical
4. Hours Generator On-Line
5. Reactor Reserve Shutdown Hours
6. Net Electrical Energy Gen. (MWH)

This Month 628.1 582.1 0.0 643,249.2 Nine Mile Point Unit #2 December 2001 1143.3 1119.8 Yr-to-Date 8,105.9 7,966.5 0.0 8,858,846.7 Cumulative 95,203.2 92,381.0 0.0 96,058,332.7