JAFP-85-0116, Monthly Operating Rept for Jan 1985
| ML20106H226 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 01/31/1985 |
| From: | Jackie Cook, Glovier H POWER AUTHORITY OF THE STATE OF NEW YORK (NEW YORK |
| To: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE) |
| References | |
| JAFP-85-0116, JAFP-85-116, NUDOCS 8502150221 | |
| Download: ML20106H226 (9) | |
Text
.
OPERATING DATA REPORT
)
DOCKET NO. 50-333 DATE Feb. 1985 COMPLETED itY J. Cook TELEPHONE (315)342-3840
,0PERATING STATUS 1.
Unit Name: James A. FitzPatrick
- Notes 2..
Reporting Period:
850101 - 850131 3.
Licensed Thermal Power (MWt): 2436 4
Nameplate Rating (Cross MWe): 883 5.
Design Electrical Rating (tet MWe): 821 6.
Maximum Dependable Capacity (Cross MWe): 830 7.
Maximum Dependable Capacity (Net MWe): ~ BIO 8.
If Changes Occur in Capacity Ratings (Items 3 Through 7) Since Last Report,Give Reasons:
NONE 9.
Power Level To Which Restricted If Any (Net MWe):
NONE 10.
Reasons For Restrictions, If Any:
This Month Yr.-to-Date Cumulative 11.
Ilours in Reporting Period 744 744 83425 12.
Number Of Hours Reactor Was Critical 744 744 60360 13.
Reactor Reserve Shutdown Hours 0
0 0
14.
Ilours Generator On-Line 744 744 58691.3 15.
Unit Reserve Shutdown Hours 0
0 0
16.
Cross Thermal Energy Generated (MWH) 1722696 1722696 124658650 17.
Gross Electrical Energy Generated (MWH) 587920 587920 42868200 18.
Net Electrical Energy Generated (MW11) 568945 568945 40966960 19.
Unit Service Factor 100%
100%
70.4%
20.
Unit Availability Factor 100%
100%
70.4%
21.
Unit Capacity Factor (Uning MDC Net) 94.4%
94.4%
63.9%
22.
Unit Capacity Factor (Using DER Net) 93.1%
93.1%
59.8%
23.
Unit Forced Outage Rate 0%
0%
13.3%
24.
Shutdowns Scheduled Over Next 6 Months (Type, Date, and Duration of Each):
R fueling outage scheduled for February 16, 1985 to last approximately 60 days.
l 25.
If Shut Down At End Of Report Period, Estimated Date of Startup:
26.
Units In Test Status (Prior to Commercial Operation):
Forecast Achieved INITIAL CRITICALITY INITIAI. ELECTRICITY COMMERCIAL OPERATION f$
8502150221 850131 g
PDR ADOCK ObOOO333 i(
R PDR l
AVERAGE DAILY UNIT POWER LEVEL DOCKET NO.
50-333 UNIT FitzPatrick DATE Feb. 1985 COMPLETED BY J. Cook TELEPHONE (315)342-3840 MONTH January 1985 DAY AVERACE DAILY POWER LEVEL DAY AVERAGE DAILY POWER LEVEL (MWe-Net)
(MWe-Net) 1 806 17 804 2
806 IS 797
(
3 804 19 799 4
800 20 805 5
801 21 603 6
g04 22 566 7
803 23 667 8
gos 24 635 9
628 25 719 10 747 26 797 11 7so 27 799 12 773 28 796 13 803 29 795 14 gos 30 792 15 802 31 7p 16 gos
SUMMARY
- The FitzPatrick Plant operated at near full thermal power for this reporting period with two power reductions to repair main condenser tube leaks.
UNITSIIUTDOWNS AND POWER REDUCTIONS DOCKET NO.
50-333 UNIT NAAIE FitzPatrick DATE _
Feb. 1Q85 REPORTMONTII anuary 1985 COAfPLETED BY
_T _ ennte 4
J TELEPilONE r11n u>,oen w.
4 wE c
e
'g,'
93,,
1 5}
E 75y Licensee 5%
$"^.
Cause & Corrective "2
y fpe Event 13 Action to y
g.
3 Gi j Report =
in U Prevent Recurrence oO g
b 1
850109 S
0 H
4 N/A SD COND Reduced power for repair to main condenser tube leaks i
850121 S
0 H
4 N/A SD COND Reduced power for repair to main condenser tube leaks 1
l l
l l
2 3
4 F: Forced Reason: '
Method:
Exhibit G Instrucilons S: Scheduled A Equipment Failure (Explain) 1-Manual for Preparation of Data 841aintenance of Test 2 Manual Scram.
Entry Sheets for Licensee C-Refueling 3 Automatic Scram.
Event Report (LER) File (NUREG-D-Regulatory Restriction 4-Other ( Explain) 0161)
E-Operator Training & Ucense Examination F Administrative 5
G-Operational Error (Explain)
Exhibit I-Same Source li Other (Explain)
e i
l l
NARRATIVE
SUMMARY
OF OPERATING EXPERIENCE JANUARY 1985 The FitzPatrick Plant operated at near full thermal power for this I
reporting period. On 850109 power was reduced to repair main condenser tube leaks in water box Bl.
On 850121 power was again reduced to repair main condenser tube leaks in water box B2.
At the end of this reporting period the plant is operating at approx-imately 76
- E'e.
v.h-1 I
i
'N N\\
s
POWER AUTHORITY OF T11E STATE OF NEW YORK
/
JAMES A. FITZPATRICK NUCLEAR POWER PLANT
/
- j SAFETY RELATED ELECTRICAL & MECHANICAL MAINTENANCE
SUMMARY
JANUARY 1985 WORK REQUEST #
REPAIR DATE SYSTEM COMPONENT #
HOW DFTECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME HOURS 11/28/84 71 22889 VISUAL Missing Panel Replaced fasteners 4
EDG-A,B,C,D Fasteners 11/28/84 24 34261 OPS Burned Out Relay Replaced Relay 3
EOD-1 11/28/84 24 33943 OPS Misadjusted Limit Adjusted Limit Switch 3
EOD-2 Switch 12/02/84 27 23966 OPS Supply Breaker Has Replaced Supply Breaker 12 FW-1 Loose Terminal 12/01/84 07 34240 OPS Incorrectly Wired Rewired 8
PR-46B 12/01/84 27 33414 OPS Cracked Diaphragm Rebuilt Pump 172 P-11B 12/10/84 15 33587 VISUAL Packing Leak Wire Brushed and Lubricated 1
MOV-102 Gland Assembly 12/06/84 24 27878 OPS Bent Linkage Straightened Linkage 3
EOD-1 12/05/84 12 28629 VISUAL Leaking Bonnet Replaced Bonnet Gasket 70 MOV-18 Gasket 01/10/85 08 27970 OPS Leaking Solenoid Replaced solenoid Valve and Air 69 Refuel Bridge Valve and Air Line Line 01/07/85 08 27981 OPS Leaking 011 Replaced Regulator 2
Refuel Bridge Regulator
/
1 i
POWER AUTHORITY OF THE STATE OF NEW YORK JAMES A. FITZPATRICK NUCLEAR POWER PLANT f
i
,/
l SAFETY RELATED ELECTRICAL & MECHANICAL MAINTENANCE
SUMMARY
I JANUARY 1985 WORK REQUEST #
REPAIR DATE SYSTEM COMPONENT #
HOW DETECTED CAUSE OF MALFUNCTION ACTION TAKEN TO PRECLUDE RECURRENCE TIME HOURS 01/10/85 11 28727 VISUAL Worn Packing Replaced Cross Head Seals and 30 P-2B Gaskets Repacked 01/14/85 11 19991 VISUAL Worn Packing Adjusted Packing 4
P-2A 01/04/85 23 27979 ALAR'I Open Auxiliary Replaced Coil 3
MOV-14 Relay Coil l
l l
01/08/85 27 28000 VISUAL Leaking Bonnet Replaced Bonnet Gasket 9
PCV-122B Gasket 01/05/85 13 21559 VISUAL Worn Packing Repacked 12 MOV-131 01/03/85 76 28627 OPS Cracked Battery Replaced Battery Connectors, 75 P-1 Connectors and Cables and Cells Bad Cells 01/09/85 71 28714 VISUAL Corrosion and Weld Cleaned Terminal Posts 2
BAT-3A Residue on Terminal Posts 01/11/85 08 34397 OPS Faulty Proximity Replaced Proximity Switch 6
Refuel Bridge Switch 10/11/84 71 22654 PREVENTIVE Damaged Secondary Replaced Coupler 3
BKR-10520 MAINTENANCE Coupler 10/10/84 71 22653 PREVENTIVE Damaged Secondary Replaced Coupler 3
BKR-10510 MAINTENANCE Coupler a
n A
m a
NEW YORK POWER AUTHORITY - JAMES A. FITZPATRICK NUCLEAR POWER PLANT
~
s MAINTENANCE
SUMMARY
Ji'TAFY 19 5 ACTION TAKEN REPAIR WORK REOUEST NO.
HOW CAUSE OF RESULTS OF
'10 PRECLUDE TIME DATE SYSTEM COMPONENT No.
DETECTED MALFUNCTION FALFUNCTION RECURRENCE HOURS 850108 02-3 028788 JIC Normal Wear Left Hand Valve Repalced Valve, 2.5 LITS-79 Leaks Perf. ISP-77 850109 02-3 028792 OPS UNKNOWN Meter Observed Checked Indicator 1.0 LI-91 Downscale
& Response good 850109 07 028790 JIC Due To Moisture Will Not Reach Ran Machine Again-10.0 TIP "C" In The System Core Top Limit Checked OK 850108 07 027963 OPS Age / Wear Tip Machine Replaced Tip "D" 44.0 hm-131-4D Output Pegged High 841228 07 034307 OPS Age / Wear Recorder Does Not Replaced Switch 0.5 PR-46C Bad Switch Indicate Proper Level 850104 08 023095 JIC Short In New Trolley Can't Vary Replaced Stata-Trol 8.0 REFUEL BRIDGE Control Box Motor Speed 850107 08 027967 OPS UNKNOWN Refuel Grapple Lifted Off Holding 12.0 GRAP-26 Hoist Won't Raise Pin 850102 08 034328 OPS Motor Control Box Bridge-Will Not Go Replaced Bad Motor 150.0 REFUEL BRIDGE Worn Out North-South Control Box 850104 11 029126 JIC Indicator Loc. Ind. Found Replaced Ind., Perf, 2.0 LI-46 Component Worn Out Of Tolerance ISP-82 Out 850113 13 034429 OPS Age / Wear Output of Inverter Replaced Topaz 8.0 E/S-152 Is Dead Inverter 850109 17 027952 OPS Loose Ink Pen Erratic "A" Cleaned, Calibrated, 8.0 RR-433 In Holder Recorder Readings And Changed Pen
NEW YORK POWER AUTIIORITY - JAMES A. FITZPATRICK NUCLEAR POWER PLANT MAINTENANCE
SUMMARY
JANUARY 1985 l
l ACTION TAKEN REPAIR l
WORK RE01'EST NO.
I!OW CAUSE OF RESULTS OF 10 PRECLUDE TIME DATE SYSTEM C0"PONENT NO.
DETECTED MALFt'NCTION MALFUNCTION RECURRENCE I!OURS 841227 20 027872 OPS Wiring Error Chart Recorder Repaired Wiring Error 7.0 FR-528 Does Not Advance In Motor 841221 27 034303 NRC Loose Point 15 Reads Disconnected and 6.0 i
RTD-101C Connection Wrong Temp.
Reconnected 850104 27 027947 OPS Instrument Drift 0 Analyzer Performed ISP-31 8.0 9
OAZ-101A,101B Discrepancy-A&B 850103 93 034300 OPS UNKNOWN When Paralleling Within Tolerance,No 8.0 EDG-P&D Gen. 'D' Lags
'B' Problems When Tested 9
l 1
4
Jemte A. Fit:Pctrick Nuclist Powse Plznt PO. Boa 41 Lycoming. New York 13093 315 342.3840 Harold A.Glovier Resident Manager
- > NewYorkPower c
tv Authority February 8, 1985 JAFP 85-0116 Director, Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission Washington, D.C. 20555 ATTENTION:
DOCUMENT CONTROL DESK
REFERENCE:
DOCKET NO. 50-333
Dear Sir:
Enclosed please find the J. A. FitzPatrick Operating Status Report for the month of January, 1985. Refueling information remains the same as previously submitted.
If there are any questions concerninF this report, please contact John Cook at (315) 342-3840, Ext. 439.
I 6:t TEh?
^
HAGhJ
- mac' cc:
Internal Distribution Enclosures l
l I
J