JAFP-04-0035, February 2004 Monthly Operating Report for James a FitzPatrick
| ML040780357 | |
| Person / Time | |
|---|---|
| Site: | FitzPatrick |
| Issue date: | 03/10/2004 |
| From: | Ted Sullivan Entergy Nuclear Northeast, Entergy Nuclear Operations |
| To: | Document Control Desk, Office of Nuclear Reactor Regulation |
| References | |
| JAFP-04-0035 | |
| Download: ML040780357 (3) | |
Text
Entergy Entergy Nuclear Northeast Entergy Nuclear Operations, Inc.
James A. Fitzpatrick NPP P.O. Box 110 Lycoming, NY 13093 Tel 315 349 6024 Fax 315 349 6480 March 10, 2004 JAFP-04-0035 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Mail Station O-Pl-17 Washington, DC 20555 T.A. Sullivan Site Vice President -JAF
SUBJECT:
James A. FitzPatrick Nuclear Power Plant Docket No. 50-333 February 2004 Monthly Operating Report
Dear Sir:
Enclosed is the Monthly Operating Report (MOR) for the James A. FitzPatrick Nuclear Power Plant for the month of February 2004.
MOR data has been prepared and formatted using the INPO Consolidated Data Entry (CDE) submittal process.
Should you have any questions concerning this report, please direct them to Mr. Mick Baker, Thermal Performance Engineer, at (315) 349-6181.
Very truly yours, TAS:MB:dr Enclosure 7:S7 6 A.
cc:
Regional Administrator U.S. Nuclear Regulatory Commission 475 Allendale Road King of Prussia, PA 19406 Office of the Resident Inspector James A. FitzPatrick Nuclear Power Plant U.S. Nuclear Regulatory Commission P.O. Box 136 Lycoming, NY 13093 Mr. Guy Vissing, Project Manager
-Project Directorate I Division of Licensing Project Management U.S. Nuclear Regulatory Commission Mail stop OWFN 8C2 Washington, DC 20555 Mr. R. Toole ENN BWR SRC Operations Subcommittee Chairman 605 West Homer Street Ebensburg, PA 15931 Mr. Paul Eddy Public Service Commission Office of Electricity and the Environment 3 Empire Plaza Albany, NY 12223 JENG JAFP Files RMS (JAF)
OPERATING DATA REPORT DOCKET NO.
UNIT NAME 1
DATE I
COMPLETED BY I
TELEPHONE I
REPORTING PERIOD:
50-333 itzPatc B
1ake Ma-rchrr M420 a F Bfak e-r 731) 34TZW8 February 2004
- 1. Design Electrical Rating
- 2.
Maximum Dependable Capacity (MWe-Net) 816.00 813.00 3.
4.
5.
6.
Number of Hours the Reactor was Critical Number of Hours Generator On-line Reserve Shutdown Hours Net Electrical Energy Generated (MWHrs)
This Month 696.00 648.67 0.00 511,118.00 Yr-to-Date Cumulative 1,440.00 191,344.50 1,392.67 185,963.87 0.00 0.00 1,137,738.00 139.043,502.00 UNIT SHUTDOWNS Type Method of F: Forced Duration Shutting Cause & Corrective Action S: Scheduled (Hours)
Down 2 Comments 2004-01 02/16/2004 F
47.33 B
5
SUMMARY
- Commenced downpower to remove circulating water pumps from service in order to combat lowering screenwell intake water levels caused by environmental conditions (frazil ice formation on intake bar racks). While at reduced power, the "A' reactor feed pump seal failed. The main turbine was taken offline to remove steam from the system and allow pump seal replacement The main turbine was put back on line when seal repairs were complete, and power ascension commenced. The reactor remained critical throughout the evolution.
I 2
Reason:
A Equipment Failure (Explain)
B -Maintenance or Test C
Refueling D
Regulatory Restriction E
Operator Training & License Examination F
Administration G
Operational Error (Explain)
H Other (Explain)
Method:
I Manual 2
Manual Trip/Scram 3
Automatic Trip/Scram 4
Continuation 5
Other (Explain)
Page 1 of 1