IR 05000903/2011001

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Notice of Violation from Insp on 850903-1101
ML20138R853
Person / Time
Site: Braidwood, 05000903  Constellation icon.png
Issue date: 11/14/1985
From: Little W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML20138R852 List:
References
50-456-85-45, 50-457-85-44, NUDOCS 8511190143
Download: ML20138R853 (2)


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Appendix NOTICE OF VIOLATION Comonwealth Edison Company Docket No. 50-456

Docket No. 50-457 As a result of the inspection conducted on September 3 through November 1, 1985, and in accordance with the General Policy and Procedures for NRC Enforcement

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Actions, (10 CFR Part 2, Appendix C), the following violation was identified:

10 CFR 50, Appendix B, Criterion XVI, Corrective Actions, as implemented by the Commonwealth Edison Quality Assurance Manual, requires that measures be established to assure that conditions adverse to quality are promptly identified and correcte Contrary to the above, corrective actions were inadequate or not implemented for

the following NRC identified issues
Corrective actions (instruction to contractors), in response to NRC concerns over protecting systems and components from intrusion of foreign matter, such as dust and moisture, were insufficient and resulted in exposure of the internals of reactor protection electrical components in the auxiliary electrical room and control room panels to deposition of significant dust from nearby ongoing nasonry work. Previous corrective actions addressed specific examples identified by the inspectors, but was apparently narrow in scope and not applied to other systems and areas.

l On or about September 19, 1985, the inspectors identified the following deficiencies to the licensee:

1) Numerous damaged flexible electrical cable conduits were observed

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during a plant tour. The damaged conduits exposed the cable insulation to cuts and gashes from the sharp edges of the conduit and also forced the cable to support the condui ) An accumulation of oil was found inside the bearing thermocouple junction box for centrifugal charging pump 1CV01PA. This caused the thermocouple cable insulation to be imersed in oil and resulted in potential degradation of the insulation. In addition this oil represented a fire hazard to the pum As of October 28, 1985, no corrective action had been taken to correct these conditions or identify and correct their cause.

l This is a Severity Level IV violation (Supplement II).

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Pursuant to the provisions of 10 CFR 2.201, you are required to submit to this l office within thirty days of the date of this Notice a written statement or l explanation in reply, including for each violation: (1) corrective action taken l and the results achieved; (2) corrective action to be taken to avoid further violations; and (3) the date when full compliance will be achieve g5 M 56 Pg ADOCK pp G

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Appendix 2 Consideration may be given to extending your response time for good cause show k D

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