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Category:CORRESPONDENCE-LETTERS
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217N2321999-10-15015 October 1999 Requests NRC Approval to Use Alternative to Requirements of 10CFR50.55a(f)(4)(ii).Licensee Requests Extension to Specified Schedule for Implementing Updates to IST Program ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes PY-CEI-NRR-2438, Informs That DBNPS & PNPP Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl1999-10-14014 October 1999 Informs That DBNPS & PNPP Staffs Have Modified or Withdrawn Several of Positions Proposed within Re Request for Approval of Qap.Revised Positions Encl ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20216J6701999-09-24024 September 1999 Forwards Post Examination Documentation for Written Operator Initial License Examination Administered at Davis-Besse Nuclear Power Station on 990920.Without Encls ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20216E5961999-09-0707 September 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1,safety Features Actuation Sys Instrumentation & Associated Bases 3/4.3.1 & 3/4.3.2,reactor Protection Sys & Safety Sys Instrumentation ML20211K6611999-08-30030 August 1999 Forwards Copies of Operator License Renewal Applications for Individuals Listed.Operators Have Successfully Completed Appropriate Operator Requalification Training Program at Dbnps.Without Encls ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211K6681999-08-30030 August 1999 Forwards Copies of Certified Personal Qualification Statement - Licensee (NRC Form 398) for Operator Candidates Listed Below.Without Encls ML20211H0201999-08-25025 August 1999 Forwards semi-annual FFD Rept for 990101-0630 for DBNPS, Unit 1,IAW 10CFR26.71(d) ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211G3911999-08-20020 August 1999 Forwards Update to Estimated Info for Licensing Action Requests Through 010930,re Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates PY-CEI-NRR-2411, Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl1999-08-19019 August 1999 Informs That Firstenergy Nuclear Operating Co Has Developed Corporate QA Program Manual for Davis-Besse Nuclear Power Station & Perry Nuclear Power Plant,As Discussed on 990318 Between Util & Nrc.Revised USAR Pages,Encl ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20211J9201999-08-13013 August 1999 Urges NRC to Find Funds for Stockpiling Radiation Pills for Residents Living Near Plant ML20210T1061999-08-12012 August 1999 Forwards Preliminary NRC Forms 398 & 396 for Listed Candidates,Per Operator License Exam Scheduled for Week of 990913.Encl Withheld ML20210S6071999-08-11011 August 1999 Provides Final Response to NRC RAI Re GL 98-01, Y2K Readiness of Computer Systems at Npps ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210G5521999-07-28028 July 1999 Provides Addl Response to 980923 OL Licensing Exam Rept 50-346/98-301 Re OL Exam Administered in Aug 1998.Results of Root Cause Investigation & Corrective Actions,Discussed ML20210H0491999-07-28028 July 1999 Forwards Application for Amend to License NPF-3,revising TS 3/4.7.5.1, Ultimate Heat Sink, to Allow Plant Operation in Modes 1-4 with Water Temp Less than or Equal to 90 F ML20210G3831999-07-27027 July 1999 Forwards Application for Amend to NPF-3,changing TSs 6.4, Training, 6.5.2.8, Audits, 6.10, Record Retention, 6.14, Process Control Program & 6.15, Odcm ML20210G5151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs for Implementation of 10CFR50,App J,Option B for Type B & C Containment Leakage Rate Testing ML20210G4391999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising Tech Specs 3/4.3.2.1, Safety Features Actuation Sys Instrumentation, & Associated Bases 3/4.3.1 & 3/4.3.2, Reactor Protection Sys & Safety Sys Instrumentation ML20210G7151999-07-26026 July 1999 Forwards Application for Amend to License NPF-3,revising TSs 3/4.3.3.1, Radiation Monitoring Instrumentation, 3/4.3.3.2, Instrument - Incore Detectors & 3/4.3.3.9, Instrumentation - Waste Gas Sys Oxygen Monitor ML20211P3071999-07-26026 July 1999 Forwards Final Rept for 990504 Biennial Radiological Emergency Preparedness Exercise for David-Besse Power Station.No Deficiencies Identified for Any Jurisdiction During Exercise ML20210G3211999-07-26026 July 1999 Forwards Written OL Exam & Supporting Matl for Exam to Be Administered at DBNPS During Week of 990913.Listed Encls Withheld from Public Disclosure Until After Exam Complete ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure 05000346/LER-1998-001-01, Forwards LER 98-001-01,which Provides Addl Info Re 980407 Occurrence.Changes Are Marked with Rev Bar in Margin.List of Util Commitments,Encl1999-07-13013 July 1999 Forwards LER 98-001-01,which Provides Addl Info Re 980407 Occurrence.Changes Are Marked with Rev Bar in Margin.List of Util Commitments,Encl ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20209C3981999-07-0101 July 1999 Responds to NRC Re Violations Noted in Insp Rept 50-346/98-21.Corrective Actions:Developed Rev to Boric Acid Control Program & Work Process Guideline on Plant Leakage ML20209B5821999-06-24024 June 1999 Provides Justification for Rev to Completion Date for One of Insp follow-up Items Cited in Insp Rept 50-346/98-03, Designated as Inspector follow-up Item 50-346/97-201-10 ML20196G1251999-06-23023 June 1999 Responds to NRC RAI Re GL 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants ML20196E5321999-06-17017 June 1999 Forwards Addl Info Re Relief Request RR-A16 to Support NRC Approval of Relief Request ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves PY-CEI-NRR-2377, Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 11999-06-16016 June 1999 Forwards Master Decommissioning Trust Agreements Revised After 1990 for Ohio Edison Co,Cleveland Electric Illuminating Co,Toledo Edison Co & Pennsylvania Power Co Re Bvnps,Units 1 & 2,DBNPS,Unit 1 & Perry Unit 1 ML20195F9071999-06-10010 June 1999 Forwards Application for Amend to NPF-3,changing Tech Specs 3/4.6.4.4, Hydrogen Purge Sys, TS 3/4.6.5.1, Shield Bldg Emergency Ventilation Sys & TS 3/4.7.6.1, Crevs ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20195F8851999-06-0707 June 1999 Withdraws 950929 License Amend Application,Proposing Mod to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20207G0621999-06-0404 June 1999 Forwards Insp Rept 50-346/98-21 on 980901-1201 & 990425-0513.Violations Identified & Licensee Being Provided Opportunity to Either Respond to Violations within 30 Days or Inform NRC That LER Rept Already Contain Info Requested ML20207F4231999-06-0202 June 1999 Forwards Rev 1 to DBNPS Emergency Preparedness Evaluated Exercise Manual 990504, IAW 10CFR50.4.NRC Evaluated Exercise Has Been Rescheduled for 991208,since NRC Did Not Evaluate 990504 Exercise ML20207E2521999-05-28028 May 1999 Forwards Rev 18,App A,Change 1 to Davis-Besse Nuclear Power Station,Unit 1,industrial Security Plan IAW Provisions of 10CFR50.54(p).Encl Withheld,Per 10CFR73.21 1999-09-07
[Table view] Category:NRC TO UTILITY
MONTHYEARML20058H6411990-11-0909 November 1990 Forwards Final SALP Rept 50-346/90-01 Covering Mar 1989 to June 1990 ML20058E7141990-10-30030 October 1990 Forwards Exam Forms & Answer Keys,Grading Results & Individual Answer Sheets for Each Applicant ML20058D6771990-10-25025 October 1990 Forwards Exemption Request for Reactor Operators Selected for NRC Requalification Exam ML20058F4811990-10-24024 October 1990 Forwards Safety Insp Rept 50-346/90-16 on 900814-1009.No Violations Noted ML20062C6811990-10-18018 October 1990 Forwards Safeguards Insp Rept 50-346/90-19 on 900924-28.No Violations Noted ML20059N6661990-10-0909 October 1990 Forwards Correction to SER Re Request for Relief from ASME Boiler & Pressure Vessel Code,Section XI Requirements.W/O Encl ML20059M2101990-09-25025 September 1990 Forwards Info Re Generic Fundamentals Exam Section of Operator Licensing Written Exams to Be Administered on 901010,including Map of Area Where Exams Will Be Taken, Preliminary Instructions for Exam & Equation Sheet ML20059L6041990-09-14014 September 1990 Confirms 901002 Meeting at Plant Site to Present Initial SALP 8 Rept for Facility ML20059J2511990-09-13013 September 1990 Forwards Safety Insp Rept 50-346/90-17 on 900827-31.No Violations Noted ML20059G1431990-09-0404 September 1990 Forwards Safety Insp Rept 50-346/90-15 on 900701-0813. Violation Noted But Not Cited.Util Implemented Corrective Actions as Result of Violation & Will Be Examined During Future NRC Insps ML20056B2701990-08-20020 August 1990 Forwards Safety Evaluation Granting 900710 Request for Relief from ASME Code for Class 3 Piping in Svc Water Sys. Request Granted Until Next Scheduled Outage Exceeding 30 Days But No Later than Dec 1991 ML20059A6821990-08-13013 August 1990 Forwards Safety Insp Rept 50-346/90-09 on 900417-0717. Violations Noted But Not Cited.Util Will Be Notified by Separate Correspondence of NRC Decision Re Enforcement Action Based on Findings of Insp ML20059A6721990-08-10010 August 1990 Forwards Safety Insp Rept 50-346/90-13 on 900605-30 & 0709. Violation Noted But Not Cited ML20059A6631990-08-10010 August 1990 Forwards Enforcement Conference Rept 50-346/90-14 on 900601 & 900717 Telcon Re Violations Noted in Insp Repts 50-346/90-09 & 50-346/90-12 ML20059A7161990-08-0808 August 1990 Provides Comments on 900105 Response to Generic Ltr 89-10 Re safety-related motor-operated Valve Testing & Surveillance. Util Should Provide Description of Methodology for Periodic Verification of motor-operated Valve Switch Settings ML20058M6141990-08-0707 August 1990 Forwards Sample Registration Ltr for 901010 Generic Fundamentals Section of Written Operator Licensing Exam. Registration Ltr Listing Names of Candidates Taking Exam Should Be Submitted to Region 30 Days Prior to Exam Date ML20055J2761990-07-24024 July 1990 Confirms 900731 Meeting in Region III Ofc to Discuss Util Response to Violation Re Instrumented Insp Techniques ML20055G6621990-07-20020 July 1990 Forwards Safety Insp Rept 50-346/90-10 on 900430-0518.No Violations Noted ML20055G3051990-07-13013 July 1990 Confirms 900718 Tour of Plant & Mgt Meeting to Discuss Sixth Refueling Outage & Other Items of Mutual Interest ML20055F2231990-07-0606 July 1990 Ack Receipt of Containing Scope & Objectives for 1990 Emergency Plan Exercise Scheduled on 900919 ML20055D3181990-06-29029 June 1990 Advises of Safety & Performance Improvement Program Implementation Audit Scheduled for Wk of 900716-20.Selected Samples of Technical Recommendations Encl ML20055D9781990-06-29029 June 1990 Advises That 900614 Changes to QA Program Meet 10CFR50,App B Requirements & Acceptable.Nrc Should Be Notified of Changes to QA Commitments Existing in Docketed Correspondence Outside QA Program Description ML20059M8631990-06-13013 June 1990 Forwards NRC Performance Indicators for First Quarter 1990. W/O Encl ML20043F3521990-06-0404 June 1990 Advises That 900406 Rev 8 to Physical Security Plan Consistent W/Provisions of 10CFR50.54(p) & Acceptable ML20043B4131990-05-24024 May 1990 Forwards Safety Insp Rept 50-346/90-06 on 900409-12 & 0514-16.No Violations Noted ML20042G7621990-05-0909 May 1990 Provides Info Re Generic Fundamentals Exam Section of Operator Licensing Written Exam to Be Administered on 900606.Map of Area Including Time & Location Where Exams Will Be Administered Also Encl ML20034A8851990-04-18018 April 1990 Advises That Util 900213 Response to NRC Bulletin 89-003 Re Potential Loss of Shutdown Margin During Refueling Operations Acceptable,Based on Confirmation That Listed Actions to Address Bulletin Performed ML20034A4461990-04-11011 April 1990 Forwards Insp Rept 50-346/90-08 on 900328-29 & Notice of Violation ML20012D9361990-03-22022 March 1990 Confirms Mgt Meeting on 900328 in Region III to Discuss Results of Interfacing Sys LOCA Insp During Period from 891030-1109 ML20033F4161990-03-15015 March 1990 Forwards Environ Assessment & Finding of No Significant Impact Re Util 870112 & 890731 Requests for Nine Exemptions from 10CFR50,App R Requirements Re Fixed Fire Suppression Sys,Alternate Shutdown Capability & Emergency Lighting ML20012C6021990-03-0808 March 1990 Advises That 900129 Rev 10 to QA Program Description,Updated SAR Chapter 17.2,Rev 0 Consistent w/10CFR50,App B & Acceptable ML20011F0051990-02-13013 February 1990 Forwards Safety Insp Rept 50-346/89-27 on 900108-12.No Violations Noted ML20006D5391990-02-0202 February 1990 Forwards Safety Evaluation Supporting Util 900115 Request for Approval of Revised Reactor Capsule Withdrawal & Insertion Schedule ML20006B0021990-01-24024 January 1990 Grants Discretionary Enforcement for Tech Spec 3.3.1.1 Re Plant Operation W/One or Four flux-delta flux-flow Instruments in Channel 2 of Reactor Protection Sys Declared Inoperable.Discretion in Effect Until 900201 ML19354E7121990-01-23023 January 1990 Forwards Safety Insp Rept 50-346/89-26 on 891107-900102 & Notice of Violation.Attachment to Rept Withheld (Ref 10CFR73.21) IR 05000346/19890231990-01-20020 January 1990 Ack Receipt of Informing NRC of Steps Taken to Correct Noncompliance Noted in Insp Rept 50-346/89-23. Justification of Request for Consolidation of Two Violations Not Found ML20006A1481990-01-17017 January 1990 Advises That 891027 Individual Plant Exams Approach, Methodology & Schedule Re Response to Generic Ltr 88-20, Acceptable ML20005E7301990-01-0303 January 1990 Advises of Evaluation of Requalification Program & Licensed Personnel at Plant Scheduled for Wk of 900514.Approved Items Listed in Encl Requested 60 Days Prior to Exam Date IR 05000346/19890211989-12-29029 December 1989 Forwards Releasable Portions of Encl 3 to Insp Rept 50-346/89-21, Investigation of Acoustic Leak Monitoring for NRC Region III ML20005D9661989-12-27027 December 1989 Requests Submittal of Addl Info to Support 890801 Request for License Amend to Revise 18-month Surveillance Interval for Insp & Operability Testing of Reactor Vessel Internal Vent Valves ML19354D6701989-12-22022 December 1989 Forwards Interfacing Sys LOCA Insp Rept 50-346/89-201 on 891030-1109.Weakness in DHR Sys Design & Surveillance Deficiencies Noted.Areas of Human Factors & Performance Which Could Affect man-machine Interface Reviewed ML20005G3621989-12-18018 December 1989 Forwards Revised NRC Forms 396 & 398 Re Certification of Medical Exam by Facility Licensee & Personal Qualification statement-licensee,respectively,reflecting Changes of Operator Licensing Process IR 05000346/19890221989-12-13013 December 1989 Forwards Incomplete Insp Rept 50-346/89-22 on 890914-1106 & Notice of Violation.Violation Re Domestic Water Sys Lines Outside Design Basis,Identified in Insp Rept 50-346/86-12, Remains as Is ML19353A9911989-11-30030 November 1989 Forwards Safeguards Insp Rept 50-346/89-25 on 891031-1107 & Notice of Violation.Notice of Violation Withheld (Ref 10CFR73.21) ML20248D8211989-09-29029 September 1989 Forwards Safety Evaluation Accepting Util 890228 & 0630 Proposed plant-specific Designs to Comply w/10CFR50.62 ATWS Rule Requirements.Proposed Date of May 1990 for Implementing ATWS Mods Also Acceptable ML20248C5691989-09-27027 September 1989 Forwards Amend 6 to Indemnity Agreement B-79,reflecting Changes in 10CFR140, Financial Protection Requirements & Indemnity Agreements, Effective 890701 ML20248A4711989-09-25025 September 1989 Requests Submission of Update Rept or Replacement Pages to Updated FSAR Submitted on 890721 to Appropriate Regional Ofc,Per 10CFR50.4(b)(6).Review of Updated QA Program Description,Section 17.2 Will Require More than 60 Days ML20247H9201989-09-0707 September 1989 Responds to Requesting Emergency Notification Sys Phone at Plant.Proposed Method for Recording Would Involve Emergency Notification Sys Phones Located in Control Room, Technical Support Ctr,Emergency Control Ctr & Inspector Ofc ML20247B4361989-09-0505 September 1989 Forwards Safety Insp Rept 50-346/89-18 on 890807-11.No Violations Noted ML20246L6571989-08-30030 August 1989 Responds to Re Annual Requalification Exam Grading Results.Based on Reviews & Consultations W/Nrc, Remedial Training,Consistent W/Identified Weaknesses, Provided & Intent of Requalification Program Met 1990-09-04
[Table view] Category:OUTGOING CORRESPONDENCE
MONTHYEARML20217P2061999-10-26026 October 1999 Forwards for First Energy Nuclear Operating Co Insp Rept 50-346/99-17 on 990928-1001.Insp Was Exam of Activities Conducted Under License Re Implementation of Physical Security Program.No Violations Identified ML20217N3851999-10-20020 October 1999 Forwards RAI Re Licensee 990521 Request for License Amend to Allow Irradiated Fuel to Be Stored in Cask Pit at Davis-Besse,Unit 1.Response Requested within 60 Days from Receipt of Ltr ML20217G9201999-10-14014 October 1999 Discusses Utils Request for Approval of Quality Assurance Program Changes ML20217F8371999-10-0808 October 1999 Forwards Insp Rept 50-346/99-10 on 990802-0913.One Violation Occurred Being Treated as NCV ML20212L0691999-09-30030 September 1999 Forwards,For Review & Comment,Copy of Preliminary ASP Analysis of Operational Condition Discovered at Unit 1 on 981014,as Reported in LER 346/98-011 ML20217A5641999-09-30030 September 1999 Informs of Completion of mid-cycle PPR of Davis-Besse on 990901.Informs That NRC Plans to Conduct Addl Insps to Address Questions Raised by Issues Re Operator Errors & Failure to Commit to JOG Topical Rept on MOV Verification ML20212D3501999-09-21021 September 1999 Forward Copy of Final Accident Sequence Precursor Analysis of Operational Event at Plant,Unit 1 on 980624,reported in LER 346/98-006 ML20211P3001999-09-0707 September 1999 Forwards FEMA Transmitting FEMA Evaluation Rept for 990504 Emergency Preparedness Exercise at Davis-Besse Nuclear Power Plant.No Deficiencies Identified.One Area Requiring C/A & Two Planning Issues Identified ML20211K0951999-08-30030 August 1999 Forwards Request for Addl Info Re Fire & Seismic Analyses of IPEEE for Davis-Besse Nuclear Power Station,Unit 1. Response Requested within 60 Days ML20211D1171999-08-20020 August 1999 Forwards Insp Rept 50-346/99-09 on 990623-0802.Violations Identified & Being Treated as Noncited Violations ML20211B0161999-08-13013 August 1999 Forwards SE Accepting Evaluation of Second 10-year Interval Inservice Insp Program Request for Relief Numbers RR-A16, RR-A17 & RR-B9 for Plant,Unit 1 ML20210P8051999-08-0909 August 1999 Forwards Insp Rept 50-346/99-15 on 990712-16.No Violations Noted.However,Several Deficiencies Were Identified with Implementation of Remp,Which Collectively Indicated Need for Improved Oversight of Program ML20210H6101999-07-30030 July 1999 Informs That Region III Received Rev 21 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Revision Was Submitted Under Provisions of 10CFR50.54(q) in Apr 1999 ML20210C4381999-07-20020 July 1999 Forwards Insp Rept 50-346/99-08 on 990513-0622.Unidentified RCS Leak Approached TS Limit of 1 Gallon Per Minute Prior to Recently Completed Maint Outage.Three Violations of NRC Requirements Identified & Being Treated as NCVs ML20209G3681999-07-15015 July 1999 Advises That Info Submitted in & 990519 Affidavit Re Design & Licensing Rept,Davis-Besse,Unit 1 Cask Pit Rack Installation Project,Holtec Intl, HI-981933,marked Proprietary,Will Be Withheld from Public Disclosure ML20207H6401999-07-0909 July 1999 Discusses Closure of TAC MA0540 Re Util Responses to RAI on GL 92-01,rev 1,suppl 1, Rv Structural Integrity. Staff Has Revised Info in Rvid & Releasing It as Rvid Version 2 ML20209D1341999-07-0808 July 1999 Forwards Notice of Withdrawal of Application for Amend to Operating License.Proposed Change Would Have Modified Facility TSs Pertaining to Allowable as-found Pressure Lift Setting Tolerance of Two Pressurizer Code Safety Valves ML20195K2751999-06-16016 June 1999 Forwards Safety Evaluation Re GL 95-07, Pressure Locking & Thermal Binding of Safety-Related Power-Operated Gate Valves ML20207G0751999-06-0707 June 1999 Forwards Insp Rept 50-346/99-04 on 990323-0513.Violations Occurred & Being Treated as non-cited Violations,Consistent with App C of Enforcement Policy ML20207G0621999-06-0404 June 1999 Forwards Insp Rept 50-346/98-21 on 980901-1201 & 990425-0513.Violations Identified & Licensee Being Provided Opportunity to Either Respond to Violations within 30 Days or Inform NRC That LER Rept Already Contain Info Requested ML20207B8161999-05-25025 May 1999 Confirms Discussion Between Members of Staffs to Have Mgt Meeting on 990608 in Oak Harbor,Oh to Discuss Recent Performance at Davis-Besse as Described in Plant Performance Review ML20207B3141999-05-24024 May 1999 Informs That in September 1998,Region III Received Revision 20 to Various Portions of Davis-Besse Nuclear Power Station Emergency Plan.Rev Submitted Under Provisions of 10CFR50.54(q) ML20206T0881999-05-18018 May 1999 Confirms 990517 Telcon Between Lindsey & M Bielby Re Arrangements Made for Administration of Licensing Exam at Facility for Week of 990913 ML20206N5311999-05-11011 May 1999 Informs That NRC Office of Nuclear Reactor Regulation Reorganized Effective 990328.As Part of Reorganization,Div of Licensing Project Mgt Created.Aj Mendiola Will Be Section Chief for Davis-Besse Npp.Organization Chart Encl ML20206H2291999-05-0707 May 1999 Forwards Proposed Change to Plant,Unit 1,TS Bases Section 2.2.1, Limiting Safety Sys Settings - Reactor Protection Sys Instrumentation Setpoints - Rc Pressure - Low,High & Pressure Temp ML20206B8171999-04-27027 April 1999 Forwards Insp Rept 50-346/99-05 on 990405-09.No Violations Noted.Purpose of Insp Was to Examine on-line Maint Risk Assessment Program Recently Implemented in Response to Maint Work Control Weaknesses ML20205G5681999-03-26026 March 1999 Advises of Completion of Plant Performance Review on 990202 to Develop Integrated Understanding of Safety Performance. Overall Performance of Plant Acceptable.Plant Issues Matrix & Insp Plan Encl ML20205B8961999-03-25025 March 1999 Forwards Insp Rept 50-326/99-201 on 990223-25.No Violations Noted.Various Aspects of Reactor Operations,Maint, Engineering Programs & Security Were Inspected ML20207G1701999-03-0505 March 1999 Forwards Insp Rept 50-346/99-01 on 990102-0212.No Violations Noted ML20207D4351999-02-25025 February 1999 Forwards Insp Rept 50-346/99-02 on 990202-05.No Violations Noted.Examples of Deficiencies with Station Procedures, Similar to Those Identified Through Staff self-assessments & in Previous NRC Insps,Were Noted ML20203F2541999-02-10010 February 1999 Informs That Beginning 990216,DE Hills Will Be Chief of Operations Branch Which Includes Operator Licensing Function ML20202A6841999-01-22022 January 1999 Forwards Amend 4 to License R-116 & Safety Evaluation.Amend Provides Surveillance Requirement Applicable to Shutdown Conditions,Air Effluent Release Limits Consistent with Current 10CFR20 & Clarifying,Editorial Changes ML20206S0811999-01-22022 January 1999 Forwards Insp Rept 50-346/98-18 on 981110-990102.No Violations Identified.Conduct of Activities at Davis-Besse Generally Characterized by Conservative Plant Operations, & Effective Engineering Involvement in Plant Issues ML20199H5821999-01-20020 January 1999 Forwards SE Re Ampacity Derating Issues Due to Application of Thermo-Lag Fire Barrier Matl at Plant ML20198E6821998-12-17017 December 1998 Forwards Insp Rept 50-346/98-20 on 981116-20.No Violations Noted.Implementation of Licensed Operator Requalification Program Was Generally Characterized by Safety Conscious Operations & Sound Evaluation of Operator Performance ML20198C9881998-12-15015 December 1998 Informs That as Part of NRC PRA Implementation Plan, Commission Assigned Two SRAs to Each Regional Ofc.Sras Will Routinely Assess Licensee Event Repts,Plant Event,Insp Findings & EAs from Risk Perspective ML20198B5391998-12-0909 December 1998 Forwards Insp Rept 50-346/98-17 on 980918-1109 & NOV Re Inadequate Maint Work Order Used by Electrician During Removal of Primary Water Storage Tank Temp Indicator ML20196H4411998-12-0303 December 1998 Confirms Plans to Hold Meeting on 981216 in Lisle,Il,To Discuss Recent Performance at Davis-Besse & Actions Being Implemented by Licensee ML20196G1621998-12-0303 December 1998 Submits Response to Request for TS Interpretation Re Surveillance Interval Extension Allowances ML20198B1511998-12-0202 December 1998 Forwards Insp Activity Plan for Next 6 Months & Plant Issues Matrix.Infor Provided to Minimize Resource Impact on Staff & to Allow for Scheduling Conflicts & Personnel Availability to Be Resolved in Advance of Inspector Arrival Onsite ML20196J5111998-12-0101 December 1998 Fowards Year 2000 Readiness Audit Rept,Which Documents Results of NRR Audit Conducted at Facility from 981027-29 ML20196D4371998-11-25025 November 1998 Discusses Concerns Re Announced Asset Transfer Between Firstenergy Corp & Duquesne Light Co ML20196C6491998-11-20020 November 1998 Forwards Insp Rept 50-346/98-19 on 981014-23.No Violations Noted.Inspectors Reviewed Circumstances Surrounding Events Leading Up to & Following Reactor Trip IR 05000346/19983011998-11-0909 November 1998 Ack Receipt of Informing NRC of Steps Taken to Correct Violations Noted in Insp Rept 50-346/98-301OL Issued on 980923.Effectiveness of C/A Will Be Reviewed Following Submittal of Root Cause Investigation Results ML20155J1471998-11-0303 November 1998 Informs That on 981007,NRC Administered GFE Section of Written Operator Licensing Exam to Employees of Facility. Exam Answer Key for Forms a & B,Grading Results & Individual Answer Sheets Encl.Without Encl ML20155B6641998-10-28028 October 1998 Forwards Safety Evaluation Re Request for Reduction in Commitment Changes in QA Program Matl Receipt Insp Process ML20154Q6711998-10-16016 October 1998 Forwards Insp Rept 50-346/98-15 on 980914-18.No Violations Noted.Emergency Preparedness Program Effectively Implemented During 980624 Tornado Event & Station Personnel Responded Well to Event ML20154Q5891998-10-14014 October 1998 Forwards Insp Rept 50-346/98-14 on 980808-0918.No Violations Noted.Online Safety Equipment Outages Were Performed Well & IAW Established Procedures ML20154H0241998-10-0606 October 1998 Discusses Arrangements Made During 980924 Telcon for Insp of Licensed Operator Requalification Program at Davis Besse Nuclear Power Station During Wk of 981116 ML20154D1801998-09-30030 September 1998 Forwards Insp Rept 50-346/98-16 on 980831-0904.No Violations Noted 1999-09-07
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UNITED STATES
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NUCLEAR REGULATORY COMMISSION
WASHINGTON, D. C. 20555 s.....s P
Docket No. 8.0-346 DEC 13 W License No. NPF-3 EA 85-107 Toledo Edison Company ATTN: Mr. John P. Williamson Chairman and Chief Executive Officer Edison Plaza 300 Madison Avenue Toledo, OH 43652 Gentlemen:
This refers to the report of the NRC Team sent to Davis-Besse by the NRC Executive Director for Operations as a result of the loss of main and auxiliary feedwater event on June 9,1985 and the inspections conducted by the Region III staff during the period March 26 - September 9,1985 of activities authorized by NRC Operating License No. NPF-3 for the Davis-Besse Nuclear Power Station.
As a result of these efforts, violations of NRC requirements were identified.
The results of the inquiry by the NRC Team were published in July 1985 in NUREG-1154, " Loss of Main and Auxiliary Feedwater Event at the Davis-Besse Plant on June 9, 1985." This June 9, 1985 loss of feedwater event at the Davis-Besse facility is significant because a safety system designed to prevent or mitigate a serious safety event did not perform its intended safety function when actually called upon to work. By the time the event ended (approximately 30 minutes after it began), there had been 12 malfunctions of major components or subsystems.
Item I described in the enclosed Notice of Violation and Proposed Imposition of Civil Penalties involves two violations which resulted in the failure of a major safety system to perform its intended safety function when it was actually called upon to verk on June 9, 1985. The violations described in Item I resulted from the failure of your staff to identify that torque switch bypass settings for certain safety-related motor-operated valves were improper and that the auxiliary feedwater pump turbines would not operate properly with steam supplied through the crossover steam piping.
Both of these conditions prevented the auxiliary feedwater system from performirg its intended safety function when actually called upon. to work.
Item II described in the Notice includes six separate violations involving failures in your maintenance, testing, training, analysis, and corrective action programs which led to the June 9, 1985 event.
Some of these failures resulted from inadequate preoperational and surveillance test procedures, inadequate maintenance procedures, and your failure to follow those procedures that were adequate.
CERTIFIED MAIL RETURN RECEIPT REQUESTED 8512200056 851213 PDR ADOCK 05000346 G
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Toledo Edison Company
Item III described in the Notice involve generic problems related to maintenance and troubleshooting identified separately from the June 9 event.
Item III includes a violation of a Technical Specification Limiting Condition for Operation caused by improper wiring of an auxiliary feedwater flow rate instrument.
This condition existed from April 13 to June 2, 1985. The other violation involves an example of a failure to follow procedures and an inadequate procedure for performing safety-related activities.
Item IV described in the Notice involves violations related to your failure to verify that hanger installations were carried out in conformance with design drawings. When substantial defects were identified by your Davis-Besse site staff during March and April 1985 in the Auxiliary Feedwater Pump Turbine Steam Supply hangers, your staff used sketches instead of nonconformance reports as required to report these deficiencies and failed to adequately assess individual and collective hanger failures to ensure adequate evaluation of the root cause of the problem.
In addition, your failure to report to the NRC within 30 days the total extent of degradation of the piping system after you became aware of these failures is also described.
The NRC Team concluded that "the underlying cause of the loss of main and auxiliary feedwater event of June 9,1985 was the licensee's lack of attention to detail in the care of plant equipment. The licensee has a history of performing troubleshooting, maintenance and testing of equipment, and of evaluating operating experience related to equipment in a superficial manner and, as a result, the root causes of the problems are not always found and corrected." The NRC Team further stated that, " Engineering design and analysis effort to address equipment problems has frequently either not been utilized or has not been effective."
Over the past two years, the NRC has directed considerable time and resources toward improving the regulatcry performance at the Davis-Besse facility. This increased attention by the NRC staff was initiated as a direct result of prior poor performance by Toledo Edison Company concerning activities at Davis-Besse.
Your poor performance resulted in the issuance of a Category 3 rating for Maintenance activities in the Systematic Assessment of License Performance (SALP) period.
Frequent management meetings were also held to discuss and emphasize the need for improved regulatory performance. This included three separate meetings between senior NRC management and the Chief Executive Officer of Toledo Edison Company during the seven month period preceding the event.
In addition, the NRC took escalated enforcement action in November 1984 for violations related to a breakdown in Toledo Edison Company's management control system. That enforcement action resulted in the proposal of a $90,000 civil penalty. Another $100,000 civil penalty was proposed in July 1985 for violations involving the licensee's failure to properly control plant activities, effectively communicate, identify root causes of problems, and take adequate corrective actions - based on issues which took place prior to the June 9, 1985 event.
Although the Toledo Edison Company has initiated corrective actions for the specific findings referenced above, and has continued working on a Performance Enhancement Program, the equipment failures that occurred during the Jurie 9,
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Toledo Edison Company
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1985 event and the violations identified in the attached Notice indicate that its corrective actions were ineffective in precluding this event. These problems apparently stemmed from a long history of ineffective and inadequate
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management attention and direction over the operation and maintenance of the i
Davis-Besse facility.
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The NRC staff acknowledges that since the June 9, 1985 event, the licensee has
taken significant initiatives to correct the problems identified in the Notice
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of Violation. However, to emphasize the seriousness with which the NRC views the occurrence of these violations and to ensure that the Toledo Edison Company I
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maintains an effective and aggressive management system to prevent such violations
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and their adverse corsequences to public health and safety, the NRC is proposing extraordinary enforcement actions. Accordingly, I have decided, after consultation
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with the Commission, to issue the enclosed Notice of Violation and Proposed
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Imposition.of Civil Penalties in the amount of Nine Hundred Thousand Dollars
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($900,000) for the violations set forth in the enclosed Notice. These violations
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have been categorized in accordance with the " General Statement of Policy and
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Procedures for NRC Enforcement Actions," 10 CFR Part 2, Appendix C (1985).
The two violations-described in Item I and the six violations in Item II have l
been categorized collectively as a Severity Level.I problem because they resulted in the failure of the auxiliary feedwater system to perform its intended safety function when actually called upon to work on June 9, 1985. The base civil
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l penalty for a Severity Level I violation is $100,000. However, as the NRC
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intends to apply its full enforcement authority as a result of this serious breakdown in management controls, the statutory limit of $100,000 per violation
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-is being proposed for these eight violations.
The two violations in Item III have been categorized as a Severity Level III problem. The base civil penalty for a Severity Level III violation or problem
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of-$50,000 is being proposed. The violations in Item IV have been categorized t
as a Severity Level III problem and the base civil penalty of $50,000 is also j:
being proposed.
You are required to respond to the enclosed Notice, and you should follow the instructions specified therein when preparing your response.
Your response
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should specifically address the corrective actions you will take or have
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taken to increase management attention and direction over the operation and 4'
maintenance of the Davis-Besse facility.
You may reference previous correspondence in your response.
Your reply to this letter and the results
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of future inspections will be considered in determining whether further enforcement action is warranted.
In accordance with 2.790 of the NRC's " Rules of Practice," Part 2, Title 10, Code of Federal Regulations, a copy of this letter and its enclosure will be i
'placed in the NRC Public Document Room.
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Toledo Edison Company-4-The responses directed 'by this letter and the enclosed Notice are not subject to the clearance procedure of the Office of Management and Budget, as required by the Paperwork Reduction Act of 1980, PL 96-511.
Sincerely,
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Wr J mes M. Tay1
, Director ffice of Inspection and Enforcement Enclosure:
Notice of Violation and Proposed Imposition of Civil Penalties cc w/ enclosure:
L. Storz, Plant Manager
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