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Category:INVESTIGATION REPORTS
MONTHYEARIR 05000133/19730011973-02-0202 February 1973 Inquiry Rept 50-0133/73-01Q:on 730126,concentrated Liquid Radwaste Storage Tank 2 Overflowed Due to Partially Open Inlet Valve.Caused by Plugged Sump Drain in Tank Vault, Resulting in Leakage Ground Instrument Line Penetrations 1973-02-02
[Table view] Category:TEXT-INSPECTION & AUDIT & I&E CIRCULARS
MONTHYEARIR 05000133/19990021999-09-29029 September 1999 Insp Rept 50-133/99-02 on 990915.No Violations Noted.Major Areas Inspected:Licensee Physical Security Program IR 05000133/19990011999-04-0808 April 1999 Insp Rept 50-133/99-01 on 990222-25 & 0308.No Violations Identified.Major Areas Inspected:Decommissioning Performance,Status,Organization,Maint & Cost controls,self- Assessments,Audits & Corrective Actions IR 05000133/19980041998-11-20020 November 1998 Insp Rept 50-133/98-04 on 980901-03,1012-17 & 20-22.No Violations Noted.Major Areas Inspected:Review Work Activities Associated with Removal of 250 Ft Tall Ventilation Stack IR 05000133/19980031998-05-22022 May 1998 Insp Rept 50-133/98-03 on 980427-30.No Violations Noted. Major Areas Inspected:Decommissioning Performance & Status, Organization,Mgt & Cost Controls & Radioactive Waste Treatment,Effluents & Environ Monitoring IR 05000133/19980021998-05-14014 May 1998 Insp Rept 50-133/98-02 on 980414-15.No Violations Noted. Major Areas Inspected:Licensee Physical Security Program Including Review of Alarm Stations,Physical Barriers, Detection Aids,Assessment Aids & Mgt Effectiveness IR 05000133/19980011998-02-27027 February 1998 Insp Rept 50-133/98-01 on 980126-29.No Violations Noted. Major Areas Inspected:Organization,Mgt & Cost Controls, Safety Reviews,Design Changes & Mods,Sf Pool Safety,Cold Weather Preparations & Decommissioning Performance Review ML20217D6381997-10-0101 October 1997 NOV from Insp on 970513-0911.Violation Noted:Process Water Monitor Was Set to Alarm at 300,000 Counts Per Minute IR 05000133/19970021997-10-0101 October 1997 Insp Rept 50-133/97-02 on 970513-0911.Violations Noted.Major Areas Inspected:Organization,Mgt & Cost Controls,Employee Concern Program,Decommissioning projects,10CFR50.59 SE Program,Annual Environ Rept Reviews & Maint & Surveillance PNO-IV-97-050, on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA1997-09-12012 September 1997 PNO-IV-97-050:on 970911,completed Repair of Reactor Caisson Leak by Reducing in-leakage to Less than Ten Gallons/Day. Informed State of CA IR 05000133/19930021993-08-26026 August 1993 Insp Rept 50-133/93-02 on 930817-20.No Violations Noted. Major Areas Inspected:Radwaste Mgt,Environ Protection,Ep, Shipping & Transportation & Occupational Exposures IR 05000133/19930031993-08-26026 August 1993 Insp Rept 50-133/93-03 on 930817.No Violations or Deviations Noted.Major Areas Inspected:Licensee Employee Concerns Program PNO-V-92-017, on 920605,earthquake W/Richter Magnitude of 5.0 Occurred.Plant Walkdowns Performed & No Problems Noted1992-06-0505 June 1992 PNO-V-92-017:on 920605,earthquake W/Richter Magnitude of 5.0 Occurred.Plant Walkdowns Performed & No Problems Noted IR 05000133/19900021990-07-13013 July 1990 Insp Rept 50-133/90-02 on 900618-21.No Violations or Deviations Noted.Major Areas Inspected:Licensee Activities During Safstor,Including Licensee Action on Open Items, Followup on NRC IE Info Notices & Emergency Preparedness PNO-V-89-057, on 890921,earthquake of 5.1 Magnitude Occurred 45 Miles Southwest of Facility.Facility Shut Down Since Jul 1976 & Reactor Vessel Defueled.Licensee Conducted Insp of Facility & No Damage Identified1989-09-21021 September 1989 PNO-V-89-057:on 890921,earthquake of 5.1 Magnitude Occurred 45 Miles Southwest of Facility.Facility Shut Down Since Jul 1976 & Reactor Vessel Defueled.Licensee Conducted Insp of Facility & No Damage Identified ML20246D2951989-08-11011 August 1989 Insp Rept 50-133/89-02 on 890717-20.Violations Noted.Major Areas Inspected:Actions Taken on Licensee Reported Items, Organization & Mgt Controls,Operator Training,Shipping & Transportation & Fire Protection Program ML20246D2911989-08-0808 August 1989 Notice of Violation from Insp on 890717-20.Violation Noted: Failure to Conspicuously Post High Radiation Area,Per Tech Spec Requirement IR 05000133/19880011988-09-15015 September 1988 Insp Rept 50-133/88-01 on 880829-0902.No Violations or Deviations Noted.Major Areas Inspected:Operator Training, in-office Review of Semiannual Radioactive Effluent Release Rept,Training & Qualifications & Followup on LERs IR 05000133/19870061988-01-12012 January 1988 Insp Rept 50-133/87-06 on 871215-18.No Violations Noted. Major Areas Inspected:Actions on Previous Insp Findings, Mgt Organization & Controls,Radwaste Mgt,Transportation, Followup on IE Info Notices & Followup on LER IR 05000133/19870051987-10-19019 October 1987 Insp Rept 50-133/87-05 on 870928-1001.No Violations or Deviations Noted.Major Areas Inspected:Actions on Previous Insp Findings,Radiological Confirmatory Measurements, Radiological Environ Monitoring & Review of Licensee Repts IR 05000133/19870031987-07-23023 July 1987 Partially Withheld Matl Control & Accounting Safeguards Insp Rept 50-133/87-03 on 870714-16 (Ref 10CFR2.790).No Violations or Deviations Noted.Major Areas Inspected:Matl Control & Accounting Reactors & Mgt Meetings ML20235D1921987-06-23023 June 1987 Notice of Violation from Insp on 870602-05.Violation Noted: Failure to Remove Stack Effluent Sample for Lab Analysis within 200 H Limit IR 05000133/19870021987-06-19019 June 1987 Insp Rept 50-133/87-02 on 870602-05.Major Areas Inspected: Actions on Previous Findings,Fire Protection,Operator & Plant Radiation Protection Training & Qualification, Procedures,Operational Safety & Surveillance Procedures IR 05000133/19860031986-12-0808 December 1986 Insp Rept 50-133/86-03 on 861117-21.No Violations or Deviations Noted.Major Areas Inspected:Activities Associated W/Decommissioning,Including Actions on Previous Insp Findings & Radiation Protection Organization & Mgt IR 05000133/19860021986-06-19019 June 1986 Insp Rept 50-133/86-02 on 860602-06.No Violation or Deviation Noted.Major Areas Inspected:Activities Associated W/Safe Storage Decommissioning,Including Operator Training, Liquid Effluents & Fire Protection IR 05000133/19860011986-03-11011 March 1986 Insp Rept 50-133/86-01 on 860219-21.No Violations or Deviations Noted.Major Areas Inspected:Activities Associated W/Decommissioning Process,Including Radiation Protection Training & Qualification & ALARA Program IR 05000133/19850041985-09-24024 September 1985 Insp Rept 50-133/85-04 on 850826-30 & 0918-22.No Violations or Deviations Noted.Major Areas Inspected:Processing, Solidification & Classification of Radwaste & Transportation Activities Associated W/Decommissioning Process ML20127N6671985-06-12012 June 1985 Notice of Violation from Insp on 850513-16 ML20127N6801985-06-11011 June 1985 Insp Rept 50-133/85-02 on 850513-16.Violations Noted:Failure to Follow Fuel Handling Procedures,Failure to Control Access to High Radiation Areas & Failure to Make Records of Required Radiation Surveys IR 05000133/19820021982-07-0101 July 1982 IE Safeguards Insp Rept 50-133/82-02 on 820621-24.No Noncompliance Noted.Major Areas Inspected:Security Plan & Procedures,Security Organization & Program Audit Records, & Locks & Keys.Details Withheld (Ref 10CFR73.21) ML20244A5941979-04-26026 April 1979 PNO-79-67AG:summary of Info Re Nuclear Incident as of 790426.Describes Plant Status & Environ Status.Highest Incore Temp Reading Is 311 F ML20244A5881979-04-25025 April 1979 PNO-79-67AF:summary of Info Re Nuclear Incident as of 790425.Describes Plant Status & Environ Status.Highest Thermocouple reading:312 F ML20151X7871977-07-28028 July 1977 PNO-77-135:on 770722,leakage of Visible Quantities of Chromate Into Outfall Canal Was Identified.Licensee Determined Source of Leakage to Be Concentrates from Radioactive Waste Evaporator ML20249B1911976-03-18018 March 1976 PNO-76-045:on 760317,reactor Was Shutdown Due to Abnormal Increase in Coolant Leakage Which Had Risen to 11.8 Gph.Insp of Piping Inside Drywell Disclosed Crack.Soft Patch Was Applied to Secure Leakage ML20236U7781975-08-0404 August 1975 PN-75-064:an Earthquake Registering 5.7 on Richter Scale at Univ of California,Berkeley & 6.4 at California Institute of Technology,Pasadena,Occurred in Vicinity of Oroville,Ca on 750801 IR 05000133/19730011973-02-0202 February 1973 Inquiry Rept 50-0133/73-01Q:on 730126,concentrated Liquid Radwaste Storage Tank 2 Overflowed Due to Partially Open Inlet Valve.Caused by Plugged Sump Drain in Tank Vault, Resulting in Leakage Ground Instrument Line Penetrations 1999-09-29
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R0fInqu'iry Report No'.i050-0133/73-01Q Pacific Gas &. Electric Compan Humboldt: Bay Unit No. 3L License No..~DPR-7l BWR,;240.Hwt UNPLANNED RELEASE OF RADIOACTIVE LIQUID' EFFLUENT
- Prepardd by:. yv a M d / 72
,j[.m.A.'D. Johnson,ReactorInc,pector
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Date
' Date and Manner AEC was Informed A' representative of Pacific Gas and Electric Company notified
' D.' Johnson by telephone on January 26, 197 Description of Particular Event or Circumt.tance ?
!The No. 2 concentrated radioactive liquid waste storage tank overflowed'
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as a . result of . the . inlet valve being partially open. Apparently the
' sump drain in the tank vault was plo;;ged, and as a result, the solution ,
rose to a level of approximately 2 font and began to leak through the
. caulked annulus around one of the inntrument line penetrations.- It then flowed :to an outside sump which drained into the outfall cana This sump can also be valved to drain to the radwaste building ~ sum From the maximum time that the Icakane could have occurred and the maximum estimated Icakage rate,.the licensee estimated that a maximum quantity of 20 gallons had been released over a period of approximately six hours. The concentr.ytion of radioactivity in the liquid was measured to be 3.5 x'10 uC/ml. The total quantity of activity released was therefore estimated to have been approximately 3 mci (an amount
approximately equal to that contained in a routine laundry waste tank ' discharge) ~. Action by Licensee
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The inlet valve to the storage tank ens fully closed. The licennce in
.l investigating ~the cause of the plugging in the vault drain to the radwaste j
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building' sump'to determine the necennary corrective action to preclude l
.a recurrence. The licensec does not plan to submit a written report to
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'the Directorate of Licensing since the' event does not fall within the l type.of. occurrences required to be reported to the AE The~1icensee plans to rerort the event to the State of California pursuant to the company's agreement with the State of California North Coastal Regional' Water Control Boar + poNra8 P00R BRIBIRM
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UNITED ST ATES '
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& M% ATOMIC ENERGY COMMISSION penECTOR ATE Ofr REGULATORY OPEH ATlONS
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l DIRECTORATE OF REGULATOP.Y OPERATIONS BULLETIN 72-3
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Pacific Gas and Electric Company Docket No. 050-0133 77 Beale Street'
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Attention: Mr. Frederick T. Searls ,
Vice President and General Counsel Gentlemen:
- We recently received information relating to the malfunction of electric
' type valve operators at two reactors. The valve operators were identified as Limitorque Models SMB-00 and SMB-000 which are used extensively in safety related systems at a number of PWR and BWR reactor facilitie Subsequent investigation identified a specific production group of these modeln which' vere manufactured between 1969 and mid-1971. The specific deficiencies are described as follows:
N Plant A Testing of valves and valve or.rators used in safety related systems at thin facility disclosed ten valves that failed to close following a " valve full open operation" test. The cause of failure was attributed to malfunction of the valve operator torq2e switch due to a lack of proper clearance between the moving parts o? the torque switch unit and the inability of the
" torque switch torsion spring" to return the electrical contacts to a closed position following operation of the valve. The weak torsion spring is considered a common mede of failure. Approximately 150 valves ranging up to eight inches in afee were equipped with valve operators having the faulty switche .
Plant B During a reactor starte , the inboard steam supply valve of the reactor core isolatien coolant (RCIC) system failed in the open position. Several attempts were made unsu cessfully to close the valv The failure was
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attributed to an interp.1 torsion spring in the valve operator torque switch
. which normally resets the electrical contacts. The valve operator in .
question is similar to the units which failed at Plant '
Two additional facilities have recently experienced similar failures since those repopted at plants A and s4 i
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' DEC 6 1912'
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Pacific Gas and Electric C .
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It,is requested.that you determine whether valve operators of the described make, model and vintage are installed or scheduled to be installed in your facilit If your findings show that valves installed or scheduled to be installed are equipped with the described valve operators,.please inform this office within thirty days,'in writing,.of the number of. valves equipped with the valve operators, the systems in which the subject valves are installed
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.- ., - or scheduled to be installed, a description of corrective actions taken or
' . . . planned, and the scheduled completion date of your corrective action Should you have any question concerning this matter we will be pleased to
- discuss them with yo .
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Sincerely,
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R. W. Smith
' Director
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cc: Warren Raymond, Humboldt Bay Nuclear Power Station
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