IA-87-759, Annotated Slides of NRC 870909 Briefing on Pipe Replacement Project
| ML20236X006 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 09/09/1987 |
| From: | NRC |
| To: | |
| Shared Package | |
| ML20236X002 | List: |
| References | |
| FOIA-87-759 NUDOCS 8712080365 | |
| Download: ML20236X006 (37) | |
Text
, .. , - . e. y. - mawwarauw
'; 0 N-.. ..
?3AC' 30":'0Y f.?0Y C ?0ERi S'.'A'.'10K X '.' 3
??3 33?.'AC3Y3N'.' ?30;3C'.'
m, hfc q 3::s
/ %
C 0 g
m 4t- . _
y
= gr , 4#b ...:..._ -
m m
. e P i :
b/
e I
NUCLEAR REGULATORY COMMISSION STAFF BRIEFING g, g. fy. 7f7
@"@$$'[$a'. SEPTEMBER 9,1987
-. s----__.---a-_w.----. . _ _ - - -._-__..--A.__---_---_a__ ._-----_-__---a---- - - _ - - - _ . - _ _ . _ - - ---________.__--_-_--.a__---------_--_.----__------____--___-______..__-------__--.-.n_ _--.__
n.
?3A?S Uf' 3 ?:?3 E3: ACE: M ' ?30J3CT TODAY'S MEETING PURPOSB TO PROVIDE INFORMATION TO THE NRC STAFF CONCERNING TECHNICAL ISSUES ADDRESSED DURING THE PIPE REPLACEMENT PROJECT AT PEACH BOTTOM- ATOMIC POWER STATION UNIT 3 s
~ ,
- m. .-
1 s
e
.y .
'BA?S UNL" 3 ?IPE REPUCPMEN" PRO." CT .
PlFOSE TO REPLACE-OR CLAD EX!SW.: lGSCC. SUSCEP~. :' E.
MATER'ALS (304SSL 2flD ALLO':' ' 82) m.t '
6 L s ( ; ks .?>[ .h k Ln>
- k A
,w . , p .
,s,c.-
gy., . - . . .
RE4SO/h
40 0F 132-WELDS "lERE CRA.CKED-
- Li.. FED SAFE T.] L!FE -
e ' . 0 t ed
' ~
.st a- C :* * % ).s ' ("s V s c a/- Aln/1/w .
c e.g_., r.. , . 6 e #
- 1 .
l r .-
l__1____._.___ _ _ _ _ _ _ . _ _ _ . _ _ _ _ _ . _ _ . _ _ _ _ , _
- g PBAPS UNIT 3 PIPE REPLACEMENT PROJECT S
AGEhTA TOP!C PRESENT0R PROJECT 0'ERVEN TONY BAZZAN!
DECONTAMINATION.
MARK MILLER ENGINEERING FRAT!K COOK L
i___-_________. _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ _ . _ _ . _ _ _ _ _ _ _ _ _ _ _ _ _
k 4
?3A?S "10' 3 ?Zs E3MC3k3r ?30;3C" A33 ROAC ~~0 3ROJ EC- l UTILIZE AVAILABLE TIME TO MAXIMlZE ADVANCE PLANNING
-* MINIMlZE FUTURE RISK 1
- INCORPORATE LATEST TECHNOLOGY UTILIZE LESSONS LEARNED FROM UNIT 2 AND OTHER
- CONTINGENCY PLANNING i
ADDRESS EVOLVING REGULATORY POSITIONS
{
wse- amm
___-____m___.._ -. _---_..-__ ____m_ __-.___ _____mu
7 3 .
.)
L .
P3APS UNIT 3 ?IPE 33:3:AC3M3N" :330J3C" J; i
JECOUTAM'NK~l0X i
-*- DECONTA!.!!NAT!0N REAGENT QUALIFICATION
- e. DECOMTAM: NATION REAGENT SELECTION
- liATER!ALS REV.EW
- DECONTAM! NATION FLOW PATH SELECTION
,2 _.
- . )
S .T P R N O GAL
.N CEP /
U W NN0 .
_ S5D PAR
_ A BtOl. O T _
P C
(
C E _
J _
O _ V R _ I DR P _
_ RN
.G GE N
T N _ EJ
.O N O _
CR EP E I _
L E
M T _
E A _
C Z T N _
A I E S R
R L N D E T R E
T G
N
~ A E
P A I S -R C E _
N E A )
S E C L
E G E L PJO
.N N U J N E 8 O N R R R I O G RROCI E J .
P . R N _ EPD A C O - G _
W . (
OV A
. E --
E N CE P E _ PR E
J P
- a x P T I S
I C V _
P E _
- 3 J _
R)S O _
GL T N A R
_ NEI .
T P _
A LJE
.R S T S E
I POT N N L R A A O TE N RPW E
I T
L J H A U _
WN8 OG .
U S
A C E
I PIS N JBS
_ SE O , * *
- S _ - D(ED C P _
A _
B _
P _
_ N O R R
_ IN TO G EI
. _ CIN L USE L8 RI I A I VJ 1 B SIO 5 NDR N C O P I C
'[ i. ji
! .t ! .
~
k u J
s 4
, l L
PBAPS UNITL3 PIPE REPLACEMENT PROJECT-- ) ,
I
)
DECONTAMINATION .0 ORGANIZATION c:
I I
l PECO MECHANICAL ENGINEERING DMSION: i POWER PLANT SERVICES SECTION - LEAD RESPONSIBLE ENGINEER - MARK MILLER PROJECT ADVISORS:
J. A. J0NES APPLIED RESEARCH COMPANY DECONTAMINATION VENDOR:
PACIFIC NUCLEAR SERVICES, INC.
CONSULTANT:
i UNITED KINGDOM CENTRAL ELECTRICITY GENERATING BOARD
__.u__________. _ _ - . _ , _m _ ._ _ -
N T m J
- - C E
J O ' "s R "
r P o o
- " \ t X
x_
- k E
E 5 )
L L
E W
Y C R D
A y N E R D L U RT S I
P [ i E NI t
mR E ;
(
R 3 [ .g .
P I
P [
m 3
T [ "A I "
X S r
o n
U R E
S I
[ L I
R S :- $
3 t k M
3
~
U C
W R
m w) L T L c E u W s ;Y R
D Y E L D r I S
R, ru H
, s (t 1 .: i
I A Tt AQ
" RK EE
, j C M ET CA
,lJ E EE RH J -
0 M M ,
O .
^
3 -
P P -
3 C
S E
E j N O
C .'
d I T
A 3 , j ,\J
- A
_ N 3: r,
-(
I M
A E
T
_ N
- - = .
O E
L C 3 3 4 4 E
_ D I '
3 . \
U R .
3 ^
E C E G v N W T
1 T
A t R I
- Ad RX N
EE N
U .
- s P *p A w B
3 i . i
k
. . 4
~ ~
.PBAPS URT 3 ?IPE 3EPLACEMENT PROJECT DECONTAM;NATiOM REAGE;E QU.E'J CATION PEACH BOTTOM UN!i 3 P!PE SA!,iPLES, 304SS
- "A" LOOP SUCT!0M 4" BL!!!D FLA':GE
- 1" PLUG-SAMPLE FRO:.! REC:RCUI'!O': P:P!NG e- REAGENTS ,
- - LOMI-NP-LO!f! @ 90*C
- LOMI-AP-LO!A @ 90*C
- CANDECON-AP-CANDECON @ 90*C
- CANDEC0!! @ 120*C
- PNS C!TROX-AP-CITROX @ 90*C 1
= . . __
PBAPS U' NIT 3 PIPE . REPLACEMENT PROJECT-DECONTAMINATION REAGENT QUAUFICATION t
- RESULTS '
HIGH CHROMlUM/ ZINC 0XIDE INDICATED THE NEED FOR
~
PRE-0XIDATION STEP
-i ALL REAGENTS REMOVED AT LEAST 75% OF ACTMTY ON SAMPLES EXTREMELY LOW AND ACCEPTABLE CORROSION ON ALL OF; -
i THE SAMPLES
___-m.m- . _ _ _ _ _ _ _ . - _ _ _ _ _ _ - - _ . _ _ . -
- yq4 l
.N.; c1.
?3PS UN"'? :3L :31PE'RIPIAC: BIEN'.' :330JEC'? t
{
f DECONTAM!NAT!0N1 REAGENT SEl.ECT!01 lu
,i 1
q e
- l010- .AP-La%' SELECTEn d 7 3
- COMPAT!BLE WTH0!/EUED MATER:ALS; (PER GE/EPR:: TEST PROGRAM)
H'GH ACTMlY RE!.'0\'AL (80 - 90.".)
l SHORTEST APPL! CATION TIME-(ABOUT HALF THAT 07 OTHER COMMERClA!.LY AVAILAB.'.E SOLVE!C
- EXTENS!VE SUCCESSFUL PLANT EXPERENCE-
. 4 3
(MONT! CELLO, DRESDEN 2 & 3,-QUAD CIT!ES 1 & 2, OYSTER CREEK) l l
_-___m_m._ __________...m__.
_ _ _ ___._.______.m.
_ __ _a
F ; -__ :.' (!_t _ .Q'
') :
+ :,, . ,
,,i, L j',y L '., '
bt
- j} ,
- 4 t ..; t.*
' f :P3A?S4UN:" 3 ?IPEEPIAC3 MEN'l PROJECT
+ .
.. I' ,
- Kb '.-g.c i
.n
(..
^i(
',n *
). ! . Q T*' A /"\- f"i 6i!l' - - -- . '!
t.'T 7 L.i.,.1, i . '.
1 l..6
- wA T' .4.
.\..
s i '.' 'm.I' I .. -i s l
i
.. .. .. ..:e s .. o
..i:.- .
.N*[,.,p,.,.w%il'*T^
,m, '
'?
- . 10W-AP-LO SElECTED ^
p Ae. . y .
- . CO U.. . .D.A.~...". "".T. a".
.. ..' r'. .", c'r D U,1.1.A.
. , . . , m , .'..'.'mS -
r
- LR. .Gr '"f DR'i e 6S7 PR. .OGP4. ....) .
.(o. .. j 1. t i a
.- ;j
- - H GH ACP.17Y RU.'.0i'.u. -(80' - 905) J x a h
... q
- S.r.,0R, _S.!. ;. PPL,.C.m. .,.!0n .s u.t.k. (.,30.vi.- . .- u., y o~ o,
- v
- 0. ~n:U n i , s.u. VUr!.u,cpV,r.
.. e
.l . .
p:t..m.ncc
... D..._ ._ ..
,.0 c) 1
- EXTE!,'S!',1~ SUCCESSFU!. PL4!T EXP..R.. ..I
- .(L'.0NT!C..'.LO, r DRESDEN 2 '& 3, QUAD . ~ .
s 1 & .', '
OYSTER CREEK)
. .- 6 o -
. , a
1 w '
PBAPS; UNIT 3 PIPE' REPLACEMENT PROJECT GE COMPONENT MATER!AL REVIEW 0F LOMI-NP-LOMI
- Ai1 WETTED SURFACES REV!EWED:'
- PUMPS- 4
- PIP!NG
.i VALVES'
- RWCU HEAT EXCHANGERS l
CONCLUS!0N:
i l
- NO DELETERIOUS EFFECTS RESULTING FROM L
EXPOSURE TO LOMi-MP-LOMI ARE EXPECTED j l
1 l
_ _ l
e- .
g.
y w.< yo
+ +
.~ 4. PBAPS UNIT!3 PIPE REPLACEMENT PROJECT
)
m u
(, VESSELiiNTERNAL MATERIAL REVIEW-g -
IEFFECTSf 0F LOMI-NP-LOMI LONl VESSEL INTE
'* LOMI, EVEN WITHOUT. DILUTION, DEMONSTRATED NOT-TO HAVE DELETERIOUS EFFECTS ON- ANY. VESSEL-INTERNAL l MATERIAL-
- NP, EVEN WITHOUT DILUTION, DEMONSTRATED NOT 1T0;HAVE DELETERIOUS EFFECTS-ON ANY VESSEL INTERNAL MATERIAL EXCEPT SA-508 LOW ALLOY STEEL (VESSEL N0ZZLES)
INSUFFICIENT TEST DATA'TO CONCLUDE EFFECTS - ON . SA-508 e
.NP NOT TO BE PERFORMED ON 28" RECIRC n- -
SUCTION PlPING WHERE CONTACT WlTH l SA-508 POSSIBLE 1
1
.l l
- + c
. l l ,
- I , , , 1 1
,'l!i1 I l ' ,
' ' ; ' 1 t
'l
-, E M -
, A E _
0 R 5
c .
, 8 1
1 s
1 1 M
~ _
1 8 V _
_ T 1
m 1
Tf R a
_ 2
, , ( M R
4 m, ,.
~
._ Tt 2
o r
, i g >f
.(y/7/[
j
, ' - /
/- - - - - y' i n
i N
>dI OA
~
T 1
' l , N e ' . I r
,Y M
\
4 R
I T5 "A C
' a g .
A T
_, i
$ T, e N .
', } $ V oL
- O My, p A
- _ CV
- r C .
E riI fr,
//, / // J X // ,hyh/ ' /y _
D M
Y E
- p , M R
L rU rC UW T
S
, i 1
] -
U T
f.
R '
SR RD HN Y
S
-
- pA
% t R
J
_ N D
O
]
- L
- j
/ ' . I T
re1
- - "4 2
"8 2
A I
{ s U
$ gJ/'s', ,',R / .
u C RI
., Y C r'@
E xg,,MU L
J i R
i*l
~
/ - F hu C
~
T 2
R
~
^ I s
~-
T i L
~
f /N S
E j , ,; , '
~ C Z
Z //// jy/ #' X //
7: 9 N
"3 1 2 M
l
1
?3A?S UX" 3 ?:?3 33?MC3Bf ?30;3C'.'
-)
'N
- %\'%
SPRAY' WAND.
- _ ~
n
, q. I ky .
]
=i NO22LE
(
. l 4 .
} \
12" EISER #.
h w -__- - _ _
. , j
, e '= ~
e==== emma.
)
__1 ---- j - - -
, 1
-l l
~'.g.
INLY RISER SPRAY WAND INSTALLATION DETAIL i
w e s -- +,um-w-.6
_____.m.__._ _ . _ _ . _ _ _ _ _ . - - - - - _ - - - - -
?3X3S X.L3 :3::P3 R3P:ACEMEN'.' :3R0;EC'.'
'mi
.i JEC0bEAMINAT'ON US;hG SPRAY WANJS-i.
" FILL AND DRA!N" METHOD e APPUCAT!0N T!ME APPROX!MATELY HALFtTHAT OF
" FILL AND DRA!N" METHOD
/?
l
_ _ - _ _ _ - _ = _ _ _ - _ _ _ _ _ _ _ _ - _ _
- - ----- - ---------- - =
2 ...
+
'I
-- i 4
P PBAPS UNIT 13 PIPE REPLACEMENT PROJECT i
DECONTAMINATION
SUMMARY
r i
- - EXPERIENCED ORGANIZATION i
- PLAN TO USE LOMI-NP-LOMI WITH SPRAY WANDS
- *~ CONSERVATIVE APPLICATION METHOD NO DELETERIOUS EFFECTS ON WETTED ' SURFACES / M
- o.
- NP NOT TO BE PERFORMED ON' SUCTION PIPING
- EXPECT AN AVERAGE OVERALL SYSTEM CONTACT DF 0F 7.0 WHICH WILL SAVE SIGNIFICANT MAN-REM
. q I',
?3A?STUT.' 3 ?:?3 33?MC3NM.' ?30;3C'.' '
i s.
7 .
BG NEalhG SCOPE:0F REPLACEMJT DESIGN IMPROVEMENTS CODES AND STANDARDS NON-DESTRUCTIVE EXAM!NAT!0N
^
PRESERV!CE TESTING 10 CFR 50.59 EVALUATION TECHN! CAL SPECIFICATION CHANGES RESTORATION lij-VESSEL IN-SERVICE INSPECTION
___m_____ _ _ . _ - - _m-__. _ _ _ _ _ _ _ = _ _ _ - _ _ _ . - - _ _ _ - _ _ . _ _ _ _ _ _ _ - _ _ _ _ _ _ _ _ _ . _ _ _ _ __.____._-..__.____________m.m__._____ _ _ - _ _ _ _ __ _ . - _ _ _ _ - __ _ _ _ _ _ . _ _ _ _ _ _ _ _ _ ___
'4-
i>
m,
. r L * . REC!RC PIPING LOOPS A & B
- RHR SUPPLY AND RETURN PlPING' INCLUDING PENETRATIONS
- . RWCU PENETRATION AND PlPING TO REGEN HX
- RPV DRAIN REROUTE AND SHIELDING
- N-1, N-2, N-5, AND N-8 SAFE ENDS l
~
'* REPLACE MIRROR WITH FIBERGLASS Bl.ANKET INSULATION l
l 1
- RHR AND CORE SPRAY TORUS STRAINERS l L
i
?3A?S X? 3 ?3 33?MC3Y3N'? ?R0;3CT i
REJSD COV 30VEN~~S I
r P!PE' SUPPORT HARDWARE l
l RECIRCULATION PUMPS AND VALVES 1
l j,
h
- q x
?3A?S UN7.'4 ?:?3 R3?:14CEMEN" :?R0;3C" t DE_ET ONS.
e
- RHR HEAD.. SPRAY SYSTEM-L.
l REClRCULAT!ON PUMP FLOW SPUTTERS-e '
J CROSS tie VALVES
- A!B PIPE WHIP RESTRAINTS l.
l u
?3A?S X" 3 ??3 33?AC3NEN" ?30;3C" ;
J S Gt MROV_g1TS ,
- SEAMLESS 316 NG PIPING
- REMOVE / CLAD ALLOY 182 BUTTER ]1
- USE OF BENT PlPE ELIMINATES 42 WELDS
- IMPROVED CONTROL OF WELD HEAT INPUT l l
1
'>
- ELECTROPOLISHING AND PRE 0XlDATION 1
I L
- REPLACEMENT OF WELDED ATTACHMENTS
. 1
- RWCU.PlPING REDESIGNED TO REDUCE PUMP LOADS
- RPV DRAIN REDESIGNED TO REDUCE RADIATION LEVELS I
t ll
L .
. - PBAPS UNIT 3 PIPE RE?lACEMENT PROJECT REDUCED WELDS-
% *O6
) B E -
. ..... 5 ,, Aff
, .h o k, .
m Q e.,- -
.' o .....
.........:: Qe; .......
g g ,
rm
. D M
-t wo L a b i
i l
I
= - __.
l
. PBAPS UNIT 3 PIPE REPLACEMENT PROJECT CODES AND STAN)ARDS e RECIRC, RHR, CORE SPRAY AND RWCU INSIDE CONTAINMENT-
. DESIGNED, FABRICATED, AND INSTALLED TO
. ASME SECTION lli SUBSECTION NB RPV DRAIN AND RWCU PlPlNG OUTSIDE CONTAINMENT DESIGNED TO ANSI B31.1
~
FABRICATED AND INSTALLED TO ASME SECTION 111. NB AND ND RESPECTIVELY
- . PIPE SUPPORTS
. NEW - ASME SECTION lil SUBSECTION NF
. REUSED - ANSI B31.1 e' -CONTAINMENT PENETRATIONS ASME SECTION lll SUBSECTION NB & NE n.-.--n_. _---- .-__ - - - _ . - .
h L
?3A?S UT.' 3 ?I?3 :13?:lC3N3N" ?:10J3C'.'
N0;\-JES RUC VE .EXAMA"ON
- ASME XI PSI PER 80 EDITION W81 ADDENDA AS DEFINED BY PBAPS SECOND INTERVAL ISI PROGRAM USING IGSCC ACCEPTED TECHNIQUES AND EPRI QUALIFIED INSPECTORS ALLOY 182/82 BUTTER UT UTILlZING REFRACTED L-WAV I
1
____.c______m-.m- _ - _ - _ - - W
L PBAPS UNIT 3 PIPE-REPLACEMENT PROJECT PRESERV!CE TESTING i
- RPV DRAIN, RECIRC, RHR AND RWCU INSIDE DRYWELL-OUTLTO THE OUTER C.I. VALVES WILL BE HYDR 0 TESTED WITH THE.
REACTOR VESSEL PER. ASME XI .
o R'NCU OUTSIDE DRYWELL HYDR 0 TESTED SEPARATELY PE CONTA:NMENT ILRT TO TEST NEW PENETRATIONS
~
PBAPS UNIT 3. PIPE REPLACEMENT PROJECT l
10 CFR 50.59 O!ALUAT!0N ARBliRARY INTERMEDIATE BREAX (A!B) DELEil0N NRC GENER!C LETTER DAED 6/19/87 ALLOWED EUM!NAT 0F AIB RULES FOR OPERAT!NG PLANTS 1
RHR AND CORE SPRAY STRAlNERS NRC GENER!CALLY APPROVED !"SULA!!0N RG 1.82 TRANSPORT ANALYS:S LARGER STRAINER FLOW AREA FLOW SPLrITERS PURPOSE WAS TO REDUCE PUM? !NLET SWIRL GE AND BYRON JACKSON PERFORMED TESTS A.ND ANALYS!
WH CH VERIF!D ACCEPTABL7Y OF DELET!0N UNTT 2 OPERAT!0N CONFIRMS ANALYSIS
o - .
.' (N j - 2 . .. . .
PBAPS UNIT.3 PIPE REPLACEMENT PROJECT 1 4
l-_
10LCFR 50.59 EVALUATION (CONTD.' .
1 BI-STABLE' FLOW - .
-(IEB'86-110) - EXACT CAUSE UNKNOWN BUT SEEMS TO B CAUSED BY HIGH AP IN HEADER TEES COMPARED T0.
.* GE HA3 REVlBED PBAPS AND CONCLUDED PBAPS AP RATIO IS SMALL AND IS ACCEPTABLE-
- UTTLE DIFFERENCE FROM UN!T 2-FINAL VERIFICATION DURING PRE-0P TESTING y
l
= HYDRAUUC ANALYS!S Ti T l GE ANALYZED AND CONCLUDED THE CHANGES FROM UNIT 2- ARE VERY SMALL AND THERE WILL BE NEGUGIBLE FLOW DISTRIBUTION CHANGES
.x .
PBAPS UNIT.31 PIPE REPLACEMENT PROJECT a
v , !
J0. CFR 50.59 Ei'Al UATION. (CONTD. . .) 1 i
HEAD SPRAY i
y{
j
- - NO CREDIT TAKEN IN UFSAR FOR. SAFETY FUNCTION. a
' LORIGlNAL PURPOSE IS ONLY:TO REDUCE HEAD
[ ,
. COOL DOWN TIME.
- - N0:!MPACT ON HEAD VENT li ,
- DELEED BY. OTHER PLANTS CROSS TlE
- NO CREDIT TAKEN FOR ECCS OPERATION
- EQUAL FLOW DISTR!BUT!0N FROM ONE LOOP UNNECESSARY l
1
- CURRENTLY LOCKED CLOSED L
l l;
I = = _ _ _ __=__- . - - _ -
w i
r
- 7. . ... 1 ..
y bh -'- .,
_c ,
- PBAPSLUNIT:3 PIPE? REPLACEMENT PRO
(
n . TECHNICAL SPECIFICATION CHANGESL
,
- SEC. 4.6.E.2 - CROSS TIE VALVES
- ?
TABLEL4.2
-DELETE HEAD! SPRAY LOGIC FUNCTION T 4
- ' TABLE 3.7.1
- DELETE HEAD. SPRAY ISOLATION VALVES
& 3.7.4
. l 1
1 1
n
-1 L i L
p
_---___zu-___------..1--------__ - - - - - - - - - - - - - - - - - - - - - - - - - - ----^------------------------------------------- - - - - - - - - - -
- r; .
I. :; .. .
PBAPS UNIT 3 PIPE REPLACEMENT PROJECT-RESTORATION
- MAIN ATTEMPT IS TO REINSTALL IN ORIGINAL CONFIGURATION
- CHANGES WILL BE EVALUATED ON CASE BY CASE BASIS
- ' ALL MODS WILL BE PERFORMED IN ACCORDANCE WITH ASME XI 1:
L_ >
m
- PBAPSLUNIT:31PIPELREPLACEMENT PROJECT -
J -
ENGINEERING
SUMMARY
~*
1 MATERIAL; UPGRADE FOR RECIRC, RHR, RWCU, & RPV DRAIN!
SAFE END. REPLACEMENT & BUTTER INSPECTION 7
ASME Ill 80 EDITION WINTER 81 ADDENDA
- ~
. DESIGN IMPROVEMENTS
- EXPERIENCED PERSONNEL UTILIZATION OF LATEST TECHNOLOGY AND INDUSTRY EXPERIENCE l>
L
- - 'l COMPREHENSIVE IN-VESSEL INSPECTION PROGRAM l1 r .
.a
n ,
p ..,
p
+
p n- LPBAPS UNIT 3 PIPE REPLACEMENT PROJECT L
IN-VESSEL INSPECTIONS (CONTD. . .)
y INSPECTION. MITIGATION
-COMPONENT PLAN PLAN' JET PUMP SENSING'UNES
. DAMAGE REPAIR N/A- -. REPAIR
. VlBRATION RESONANCE TEST - CLAMPS'AS REQUIRED SHROUD HEAD BOLTS N/A - REPLACE JET PUMP HOLD DOWN N/A - REPLACE-L "Il BEAMS DRY TUBES VISUAL - REPLACE AS REQUIRED STEAM DRYER VISUAL - REPAlR AS REQUIRED CONTROL BLADES VISUAL - BUFFER MAINTENANCE
- MODIFIED BLADES
y, 7 ~, L N i .' % ' .;'
m k l,._
"U' j - ,
l
};;e..
1
. PBAPS UNIT 3 PIPE REPLACEMENT PROJECT-1 IN-VESSE!. !NSPECTIONS.
i 1' INSPECTION MmGATION
. COMPONENT PLAN __
PLAN ACCESS HOLE COVER UT- - - 00hTNGENCY CLAM?~
, - HWC.
\;.
TOPLGU!DE - lH -- REPATR AS' REQUIRED
- r. ;I.
7 4
' CORE SPRAY SPARGER V!SUAL - CONT!NGENCY CLAMP '
CORE' SPRAY lhT.RNAL MSUAL - C0hTNGENCY MATERIA'.
P!?E
'l -
\ \
w & 4,*.e,*ce.
.e- ,
==.s- 4e, e,in-