ENS 52335
ENS Event | |
---|---|
15:42 Oct 26, 2016 | |
Title | Containment Sump Suction Valve Opened During Containment Spray Pump Testing |
Event Description | On October 26, 2016, the Harris Nuclear Plant was in Mode 6 with core reload complete, the reactor head removed, and reactor cavity water level greater than 23 feet. The refueling water storage tank (RWST) was less than 23.4% level as expected for the refueling conditions.
During surveillance testing to adjust the eductor flow throttle position, the containment spray pump was started in recirculation mode with the discharge valve shut. With RWST level less than 23.4%, logic was satisfied to actuate Engineered Safety Features Actuation System (ESFAS) Functional Unit 8, containment spray switchover to containment sump. The containment sump suction valve opened in accordance with the design, however the action was unexpected by the operators. Therefore, operators secured the containment spray pump and shut the containment sump suction valve. ESFAS Functional Unit 2, Containment Spray, was not actuated and water did not flow through the containment spray nozzles. This event is reported as a specified system actuation in accordance with 10 CFR 50.72(b)(3)(iv)(A) due to the opening of the containment sump suction valve. This event did not impact the health and safety of the public. The licensee has notified the NRC Resident Inspector. |
Where | |
---|---|
Harris ![]() North Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+120.95 h5.04 days <br />0.72 weeks <br />0.166 months <br />) | |
Opened: | Chuck Yarley 16:39 Oct 31, 2016 |
NRC Officer: | Bethany Cecere |
Last Updated: | Oct 31, 2016 |
52335 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 52335\u003C/a\u003E - \u003Ca href=\"/Harris\" title=\"Harris\"\u003EHarris\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EContainment Sump Suction Valve Opened During Containment Spray Pump Testing\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 52335 - Harris\n","link":"","lat":35.63344166666667,"lon":-78.95586666666667,"icon":"/w/images/7/75/Duke_Energy_icon.png"}],"imageoverlays":null} | |
WEEKMONTHYEARENS 561902022-10-31T00:57:00031 October 2022 00:57:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation - Auxiliary Feedwater System Actuation ENS 561892022-10-30T10:53:00030 October 2022 10:53:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Auxiliary Feedwater System Actuation ENS 560752022-08-28T07:29:00028 August 2022 07:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 558682022-04-29T08:05:00029 April 2022 08:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip and Auxiliary Feedwater System Actuation ENS 533182018-04-07T08:51:0007 April 2018 08:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Actuation of Auxiliary Feedwater System (Afw) ENS 523352016-10-26T15:42:00026 October 2016 15:42:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Containment Sump Suction Valve Opened During Containment Spray Pump Testing ENS 522912016-10-08T17:28:0008 October 2016 17:28:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Unusual Event Declared Due to Loss of Offsite Power ENS 522892016-10-08T05:50:0008 October 2016 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unplanned Reactor Trip and Safety Injection Due to Turbine Control Valve Transient ENS 497422014-01-18T15:16:00018 January 2014 15:16:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Alert Declared Due to Fire in 480V Bus ENS 463962010-11-05T05:04:0005 November 2010 05:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of an Emergency Diesel Generator Following Inadvertent De-Energization of Safety Bus ENS 444232008-08-19T13:05:00019 August 2008 13:05:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Rod Control System Malfunctioned ENS 436762007-09-29T02:32:00029 September 2007 02:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of a Startup Transformer ENS 428482006-09-19T14:00:00019 September 2006 14:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Generator Lockout Signal ENS 416542005-05-01T04:21:0001 May 2005 04:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Condensate Pump ENS 411792004-11-07T21:35:0007 November 2004 21:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation "a" Auxiliary Feedwater (Afw) Pump Manually Started Due to Decreasing Steam Generator Water Level. ENS 411292004-10-18T11:41:00018 October 2004 11:41:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Emergency Diesel Start ENS 407302004-05-06T16:52:0006 May 2004 16:52:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip and Actuation of Auxiliary Feedwater System ENS 400842003-08-17T19:51:00017 August 2003 19:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of "a" Condensate Pump. 2022-08-28T07:29:00 | |