ENS 49120
ENS Event | |
---|---|
19:22 Jun 15, 2013 | |
Title | Division 1 and 2 Emergency Diesel Generators Power Buses After Momentary Offsite Power Loss |
Event Description | Columbia Generating Station is shutdown for a refueling outage and is currently in Mode 4. At 1222 PDT June 15, 2013, the 115 kV offsite power to the backup transformer relayed off and then came back on. Both Division 1 and Division 2 4.16 kV critical switchgear buses were powered from the backup transformer at the time of the loss of backup power.
Upon detection of under voltage conditions, Emergency Diesel Generators 1 and 2 started and powered the Division 1 and Division 2 4.16 kV critical switchgear buses after approximately 5 seconds. The temporary loss of power to the Division 1 and Division 2 4.16 kV critical switchgear buses also resulted in the closure of containment isolation valves in the Reactor Water Cleanup System, Equipment Drain System and the Floor Drain System. Shutdown cooling had previously been secured in preparation of performing the reactor pressure vessel hydro test. Investigation into the cause of the temporary loss of the 115 kV offsite power is on-going. The Division 1 and Division 2 4.16 kV critical switchgear buses are currently being powered from the 230 kV offsite power through the startup transformer. There were no radiological releases as a result of this event." The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Columbia Generating Station Washington (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000397/LER-2013-005 |
Time - Person (Reporting Time:+-0.73 h-0.0304 days <br />-0.00435 weeks <br />-9.99954e-4 months <br />) | |
Opened: | Bruce Hugo 18:38 Jun 15, 2013 |
NRC Officer: | Pete Snyder |
Last Updated: | Jun 15, 2013 |
49120 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 49120\u003C/a\u003E - \u003Ca href=\"/Columbia\" title=\"Columbia\"\u003EColumbia\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EDivision 1 and 2 Emergency Diesel Generators Power Buses After Momentary Offsite Power Loss\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 49120 - Columbia\n","link":"","lat":46.55068333333333,"lon":-119.488975,"icon":"/w/images/7/7c/Energy_Northwest_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 559382022-06-13T16:23:00013 June 2022 16:23:00
[Table view]10 CFR 50.72(b)(3)(iv)(A), System Actuation Partial Loss of Power to RPS During Maintenance ENS 529182017-08-20T23:05:00020 August 2017 23:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to a Rise in Main Condenser Back Pressure ENS 524422016-12-18T19:24:00018 December 2016 19:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Scram Due to Load Reject from Substation ENS 510862015-05-22T07:14:00022 May 2015 07:14:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Start Due to Actuation of Undervoltage Circuitry ENS 491202013-06-15T19:22:00015 June 2013 19:22:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Division 1 and 2 Emergency Diesel Generators Power Buses After Momentary Offsite Power Loss ENS 452452009-08-05T14:50:0005 August 2009 14:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Toxic Gas from a Switchgear Fire in the Turbine Building ENS 417902005-06-23T20:46:00023 June 2005 20:46:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit Experienced an Automatic Reactor Scram Due to a Loss of Feedwater Flow ENS 417792005-06-15T21:00:00015 June 2005 21:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Turbine Throttle Valve Closure 2022-06-13T16:23:00 | |