ENS 48644
ENS Event | |
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19:08 Jan 2, 2013 | |
Title | Inadvertent Actuation of Safety Injection, Containment Cooling and Containment Isolation Signals |
Event Description | At 1308 hours0.0151 days <br />0.363 hours <br />0.00216 weeks <br />4.97694e-4 months <br /> [CST] on January 2, 2013, Arkansas Nuclear One Unit 2 (ANO-2) experienced an inadvertent safety injection actuation signal (SIAS), containment cooling actuation signal (CCAS) and containment isolation actuation signal (CIAS) during matrix testing on 'C' channel plant protective system (PPS). All components actuated as designed for the stated actuation signals.
After verification that the actuation signal was not valid the high pressure safety injection (HPSI) pumps and low pressure safety injection (LPSI) pumps were secured and their hand switches placed in pull-to-lock as directed by the abnormal operating procedure for inadvertent SIAS at 1312 hours0.0152 days <br />0.364 hours <br />0.00217 weeks <br />4.99216e-4 months <br />. The HPSI and LPSI pumps were the restored to normal standby condition and available for automatic operation at 1352 hours0.0156 days <br />0.376 hours <br />0.00224 weeks <br />5.14436e-4 months <br />. The unit did down power to approximately 87% power when all three coolant charging pumps ran with suction aligned to the boric acid makeup tanks. The unit currently remains in mode 1. SIAS, CCAS, and CIAS have been reset. The cause of the inadvertent actuation signals is under investigation. The NRC Resident Inspector has been informed. Unit 2 entered Technical Specification 3.0.3 for approximately 40 minutes while the LPSI and HPSI pumps were in pull-to-lock. |
Where | |
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Arkansas Nuclear Arkansas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
LER: | 05000368/LER-2013-001 |
Time - Person (Reporting Time:+-0.43 h-0.0179 days <br />-0.00256 weeks <br />-5.89014e-4 months <br />) | |
Opened: | Donald Walls 18:42 Jan 2, 2013 |
NRC Officer: | Howie Crouch |
Last Updated: | Jan 2, 2013 |
48644 - NRC Website
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Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (87 %) |