At approximately
1814 hours0.021 days <br />0.504 hours <br />0.003 weeks <br />6.90227e-4 months <br /> (EST) on January 17, 2012, H. B. Robinson Steam Electric Plant (HBRSEP), Unit No. 2, personnel confirmed that the Station Battery Performance Capacity Test (Five Year Interval), for station battery 'B' was not completed within its required periodicity plus
grace period. Based upon this information, plant Operations personnel declared the 'B' battery
inoperable and entered the required action for Improved Technical Specifications (
ITS) 3.8.4, Condition 'A', which requires that the
DC electrical power subsystem be restored to
operable status in
2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. At
2014 hours0.0233 days <br />0.559 hours <br />0.00333 weeks <br />7.66327e-4 months <br /> (EST), Operations personnel entered the required action for
ITS 3.8.4, Condition 'B' due to required actions and associated completion time for Condition 'A' not met. Condition 'B' requires the unit to be in Mode 3 within
6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> AND be in Mode 5 within
36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.
This report is being made in accordance with 10 CFR 50.72(b)(2)(i) based on the initiation of a plant shutdown required by the Technical Specifications. Following the shutdown, the unit will commence a refueling outage that was originally scheduled to begin at 0000 hours0 days <br />0 hours <br />0 weeks <br />0 months <br /> (EST) on January 21, 2012.
The licensee informed the NRC Resident Inspector.