ENS 45603
ENS Event | |
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05:10 Jan 2, 2010 | |
Title | Diesel Generator Auto Start Due to Failed Line Arrestor in Switchyard |
Event Description | This report is being made under 10CFR50.72(b)(3)(iv)(A), 'Any event or condition that results in valid actuation of any of the systems listed in Paragraph (b)(3)(iv)(B) of this section' due to an auto start of the 'A' Standby Diesel Generator.
The auto start of the 'A' Standby Diesel Generator occurred on a valid bus undervoltage condition caused by a momentary fault on the 161 kV Vinton line. Switchyard inspection revealed a failed 161 kV line arrestor [on] one of the phases of the Vinton line. The 'A' Standby Diesel Generator supply breaker was not required to close onto its respective essential bus as it remained powered from its normal power supply, 1X003 Start-up Transformer, during and after the event. Offsite power remained fully operable during and following the event. The 'A' Standby Diesel Generator has been returned to the standby/readiness condition. As designed, the 'A' Emergency Service Water systems auto started when the 'A' Standby Diesel Generator started. The Emergency Service Water systems have been returned to the standby/readiness condition. The 'B' Well Water Pump tripped as a result of the electrical transient. The 'A' Well Water pump and 'B' Emergency Service Water pump were manually started by operators in accordance with Abnormal Operating Procedure 408, Well Water System Abnormal Operation. The in-service Reactor Water Cleanup pump tripped which removed RWCU from service. The RWCU system has been returned to service. The in-service Spent Fuel Pool Cooling pump tripped as a result of the electrical transient. Spent Fuel Pool Cooling has been returned to service. Spent fuel pool temperature rose 0.7 [degrees] F while the pump was out of service. All ECCS systems were available before the event and have remained available following the event. The licensee is not in any Technical Specification LCO's as a result of this event. The in-service Spent Fuel Pool Cooling pump was OOS for approximately 58 minutes. The NRC Resident Inspector has been notified. |
Where | |
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Duane Arnold ![]() Iowa (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000331/LER-2010-001 Regarding Emergency Diesel Generator Start Due to Failed Arrester in Switchyard |
Time - Person (Reporting Time:+-0.97 h-0.0404 days <br />-0.00577 weeks <br />-0.00133 months <br />) | |
Opened: | Stephen Speirs 04:12 Jan 2, 2010 |
NRC Officer: | Joe O'Hara |
Last Updated: | Jan 2, 2010 |
45603 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 540122019-04-20T10:07:00020 April 2019 10:07:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Both Reactor Feed Pumps Trip Causing Manual Reactor Scram and Eccs Injection ENS 536762018-10-19T05:00:00019 October 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Automatic Reactor Trip Due to Feedwater Regulating Valve Failing Closed ENS 514842015-10-20T23:00:00020 October 2015 23:00:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Diesel Generators Started After Transmission Line Lightning Strikes ENS 502462014-07-01T00:13:0001 July 2014 00:13:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto-Start of Standby Diesel Generators Due to a Grid Disturbance ENS 471432011-08-11T16:38:00011 August 2011 16:38:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Primary Containment Isolations ENS 456032010-01-02T05:10:0002 January 2010 05:10:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Diesel Generator Auto Start Due to Failed Line Arrestor in Switchyard ENS 454212009-10-08T19:20:0008 October 2009 19:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram During Testing ENS 451542009-06-23T22:04:00023 June 2009 22:04:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Auto Start of Emergency Diesel Generators Due to Offsite Voltage Transient ENS 449652009-04-03T05:28:0003 April 2009 05:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Increasing Reactor Water Level During Calibration ENS 448212009-02-02T00:00:0002 February 2009 00:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Condenser Cooling ENS 438172007-12-01T20:35:0001 December 2007 20:35:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Edg Starts on 161 Kv Line Transient ENS 432712007-04-02T16:25:0002 April 2007 16:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Lowering Reactor Vessel Water Level ENS 432472007-03-19T00:40:00019 March 2007 00:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Coolant Chemistry Concerns ENS 432102007-03-03T05:32:0003 March 2007 05:32:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Signal Due to High Discharge Volume Level ENS 431852007-02-24T23:56:00024 February 2007 23:56:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Normal Electrical Lineup Due to Grid Instability from Adverse Weather Conditions ENS 429662006-11-06T07:10:0006 November 2006 07:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram During Turbine Testing ENS 403532003-11-25T21:22:00025 November 2003 21:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram Due to Degrading Condenser Vacuum During Power Ascension ENS 403012003-11-07T07:34:0007 November 2003 07:34:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Scram at Duane Arnold Due to Hi Coolant Conductivity 2019-04-20T10:07:00 | |