ENS 44273
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ENS Event | |
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05:56 Jun 6, 2008 | |
Title | Reactor Trip Due to Low Cooling Flow to Main Generator Rectifier |
Event Description | During the performance of stator water low flow testing a turbine trip and subsequent Reactor trip occurred on low cooling flow to the main generator rectifier. An Automatic Emergency Feedwater actuation signal occurred on low steam generator level due to unit trip. This is an expected actuation for a turbine/reactor trip from 100% power. The Engineered Safety Function Actuation operated as designed.
On the Unit trip, the main feedwater pumps exhibited large rpm oscillations. Operators tripped one of the non-safety related main feed pumps, and placed the second in manual which stabilized the main feedwater system. When conditions allowed, operators placed the operating main feed pump in automatic control. All rods fully inserted successfully. All emergency systems operated as required. No PORV's or Safety valves lifted during this event. Auxiliary Feedwater system is available, but not in use at this time. RCPs are in operation transferring decay heat to steam generators. Main steam is being directed to main condenser via bypass. The licensee notified the NRC Resident Inspector. |
Where | |
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San Onofre California (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-1.13 h-0.0471 days <br />-0.00673 weeks <br />-0.00155 months <br />) | |
Opened: | Lou Bosch 04:48 Jun 6, 2008 |
NRC Officer: | John Knoke |
Last Updated: | Jun 6, 2008 |
44273 - NRC Website
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Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (97 %) |
After | Hot Standby (0 %) |
San Onofre with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 476282012-02-01T01:30:0001 February 2012 01:30:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to a Primary to Secondary Leak Greater than 30 Gal/Hr ENS 472522011-09-08T22:38:0008 September 2011 22:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Grid Disturbance ENS 463462010-10-19T22:15:00019 October 2010 22:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Specified System Actuation ENS 453472009-09-13T19:43:00013 September 2009 19:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Following Turbine Trip for Loss of Condenser Vacuum ENS 442732008-06-06T05:56:0006 June 2008 05:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Low Cooling Flow to Main Generator Rectifier ENS 439282008-01-23T22:15:00023 January 2008 22:15:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation One of Two Main Feedwater Pumps Trip ENS 434352007-06-21T05:50:00021 June 2007 05:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Failed Instrument Air Header Leads to Manual Reactor Trip ENS 413682005-02-03T20:27:0003 February 2005 20:27:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Unit Auxiliary Transformer Trip ENS 412092004-11-19T16:07:00019 November 2004 16:07:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Turbine Trip on Main Generator Trip ENS 407912004-06-04T11:45:0004 June 2004 11:45:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip Due to Intake Structure Seaweed Fouling ENS 406642004-04-10T18:50:00010 April 2004 18:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Both Main Feedwater Pumps 2012-02-01T01:30:00 | |
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