As part of a planned outage for Browns Ferry Unit 3, initial drywell leak inspections were performed after shutdown (mode 3). This inspection identified a
weld defect in
Residual Heat Removal (
RHR) piping. The defect was in a one inch test line near manually operated valve 3-74-638B. This is classified as
pressure boundary leakage and the piping is rated as
ASME code class 1. The leak rate was estimated by visual observation at less than 0.25 gpm. Investigation is continuing into the cause of the
weld defect. Unit 1 and 2 remain at full power and are not affected by this event.
This event is reportable within 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> under 10 CFR 50.72(b)(3)(ii)(A) and 10 CFR 50.73(a)(2)(ii)(A) as 'Any event or condition that results in the condition of the nuclear power plant, including its principal safety barriers, being seriously degraded.'
The licensee plans to continue to Mode 4 (Cold Shutdown) as required by Tech Specs for pressure boundary leakage.
The NRC resident inspector has been notified.