ENS 42084
ENS Event | |
---|---|
22:05 Aug 31, 2005 | |
Title | Invalid Actuation of an Emergency Diesel Generator |
Event Description | This telephone notification to report an invalid actuation is provided in accordance with 10 CFR 50.73(a)(1), which states, 'In the case of an invalid actuation reported under Sec. 50.73(a)(2)(iv), other than actuation of the reactor protection system (RPS) when the reactor is critical, the licensee may, at its option, provide a telephone notification to the NRC Operations Center within 60 days after discovery of the event instead of submitting a written LER.' The specific reporting requirement in 10 CFR 50.73(a)(2)(iv)(A), states, 'Any event or condition that resulted in manual or automatic actuation of any of the systems listed in paragraph (a)(2)(iv)(B).' For this report, the affected system was the emergency AC electrical power systems as listed in 10 CFR 50.73(a)(2)(iv)(B)(8). Specifically, the Train A emergency diesel generator (EDG) automatically started due to an invalid system actuation.
On August 31, 2005, at approximately 1805 hours0.0209 days <br />0.501 hours <br />0.00298 weeks <br />6.868025e-4 months <br /> (EDT), with H. B. Robinson Steam Electric Plant (HBRSEP), Unit No. 2, operating in MODE 1 at approximately 100% power, the Train A EDG automatically started from the standby condition. The EDG did not automatically connect to the associated emergency bus (E-1), because no E-1 bus undervoltage (UV) signal was present. The automatic start was caused by a failed solenoid-operated valve (SOV) in the air start system for the EDG (valve number DA-23A). The SOV failed-open, which is the designed failure-mode condition for this valve. This admitted air to the EDG air-start distributor, which started the Train A EDG. No additional failures or abnormalities were noted. The Train A EDG successfully started and achieved the required speed and voltage, but as stated previously, the EDG did not load because no UV signal was present on the associated bus. The Train B EDG remained operable during this event. Also, the EDGs each have two starting SOVs that are in parallel in the starting air system. A start signal or a loss of power to either valve is sufficient to start the associated EDG. The failed SOV was replaced. The Train A EDG was tested after replacement of the SOV and returned to service at 1016 hours0.0118 days <br />0.282 hours <br />0.00168 weeks <br />3.86588e-4 months <br /> on September 1, 2005. The invalid EDG start was entered into the corrective action program for HBRSEP, Unit No. 2. The investigation of this event has been completed. The results of the investigation determined that the EDG start was caused by a short-circuit failure of the coil for the SOV. Additional corrective actions for this condition, beyond replacement of the failed SOV, are in progress and are being tracked via the corrective action program. The licensee notified the NRC Resident Inspector. |
Where | |
---|---|
Robinson South Carolina (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1355.57 h56.482 days <br />8.069 weeks <br />1.857 months <br />) | |
Opened: | Curtis Castell 09:39 Oct 27, 2005 |
NRC Officer: | Bill Huffman |
Last Updated: | Oct 27, 2005 |
42084 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 42084\u003C/a\u003E - \u003Ca href=\"/Robinson\" title=\"Robinson\"\u003ERobinson\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EInvalid Actuation of an Emergency Diesel Generator\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 42084 - Robinson\n","link":"","lat":34.40111111111111,"lon":-80.15933333333334,"icon":"/w/images/7/75/Duke_Energy_icon.png"}],"imageoverlays":null} | |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 550792020-12-01T14:46:0001 December 2020 14:46:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Optional Telephonic Notification of an Invalid Specified System Actuation ENS 461272010-05-25T17:14:00025 May 2010 17:14:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Report for Inadvertent Safety Injection System Actuation ENS 434502007-05-02T03:39:0002 May 2007 03:39:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation ENS 420842005-08-31T22:05:00031 August 2005 22:05:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of an Emergency Diesel Generator 2020-12-01T14:46:00 | |