ENS 41183
ENS Event | |
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14:14 Sep 15, 2004 | |
Title | Invalid Actuation of Containment Vent Isolation Valve |
Event Description | The following information is provided as a 60 day telephone notification to NRC under 10 CFR 50.73(a)(1) in lieu of submitting a written LER to report a condition that resulted in an invalid actuation of the WBN [Watts Bar Nuclear] Train A Containment Vent Isolation signal. NUREG1022 Revision 2 identifies the Information that needs to be reported as discussed below.
(a) The specific train(s) and system(s) that were actuated. On September 15, 2004, at 0914 EDT, a Train A Containment Vent Isolation (CVI) signal was received when the A Train Containment Purge Radiation Monitor momentarily spiked above the High Radiation Trip set-point. The B Train Containment Purge system was in operation at the time of the CVI signal and automatically shutdown as designed. (b) Whether each train actuation was complete or partial. The actuation was considered complete. The CVI signal for Train A automatically isolated the containment ventilation system as designed. The A Train Containment Purge Radiation Monitor was removed from service and considered inoperable due to no supporting indication of actual radiation by redundant radiation monitors or recorded trend data. (c) Whether or not the system started and functioned successfully. Train A Containment Vent Isolation signal automatically actuated and functioned successfully. The CVI signal was not in response to an actual plant condition. Maintenance on the Train A Containment Purge Radiation Monitor, revealed a loose connection in the detector cable. The radiation monitor was repaired and returned to service and the containment ventilation air cleanup unit was also returned to service." The NRC Resident Inspector was notified of this by the licensee. |
Where | |
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Watts Bar Tennessee (NRC Region 2) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1318.63 h54.943 days <br />7.849 weeks <br />1.806 months <br />) | |
Opened: | Rickey Stockton 13:52 Nov 9, 2004 |
NRC Officer: | John Mackinnon |
Last Updated: | Nov 9, 2004 |
41183 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 573362024-08-02T01:27:0002 August 2024 01:27:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-DAY Notification of Invalid Specified System Actuation ENS 573242024-07-22T16:48:00022 July 2024 16:48:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Notification of Invalid Specified System Actuation ENS 570772024-02-16T02:24:00016 February 2024 02:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Emergency Diesel Generators ENS 562742022-11-24T21:21:00024 November 2022 21:21:00 10 CFR 50.73(a)(1), Submit an LER 60-DAY Optional Telephonic Notification of Invalid Actuation of Containment Ventilation Isolation Valves ENS 548702020-07-23T13:56:00023 July 2020 13:56:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for Two Invalid Containment Ventilation Isolation Actuations ENS 542202019-07-26T14:03:00026 July 2019 14:03:00 10 CFR 50.73(a)(1), Submit an LER Invalid Containment Ventilation Isolation Actuation ENS 538402018-12-02T05:28:0002 December 2018 05:28:00 10 CFR 50.73(a)(1), Submit an LER Invalid Containment Ventilation Isolation Actuation ENS 527902017-04-28T09:00:00028 April 2017 09:00:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Auxiliary Feedwater Actuation ENS 525392016-12-15T18:32:00015 December 2016 18:32:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Telephonic Notification for an Invalid Containment Ventilation Isolation Actuation ENS 520012016-04-14T18:06:00014 April 2016 18:06:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for an Invalid Containment Vent Isolation Actuation ENS 511522015-04-15T16:07:00015 April 2015 16:07:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuations of the Containment Ventilation Isolation System ENS 510792015-03-17T17:06:00017 March 2015 17:06:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Auxiliary Feedwater System During Electrical Testing ENS 501332014-04-16T05:48:00016 April 2014 05:48:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification for Inadvertent Fast Start of Diesel Generator During Testing ENS 482042012-06-19T03:49:00019 June 2012 03:49:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Ventilation Isolation ENS 441602008-02-23T04:00:00023 February 2008 04:00:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Verbal Notification of Invalid Specified System Actuation ENS 411832004-09-15T14:14:00015 September 2004 14:14:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Vent Isolation Valve 2024-08-02T01:27:00 | |