05000296/FIN-2016001-08
From kanterella
(Redirected from 5000296/FIN-2016001-08)
Jump to navigation
Jump to search
Finding | |
---|---|
Title | Licensee-Identified Violation |
Description | Licensee Event Report (LER) 05000296/2014-003-00 Primary Containment Isolation Valve Inoperable for Longer Than Allowed by Technical Specifications 10 CFR 50, Appendix B, Criterion 5 required, in part, that activities affecting quality be implemented in accordance with documented procedures and drawings. Contrary to the above, between March 7, 2014 and June 6, 2014, relay 3-RLY-074-10A-K98A was wired incorrectly as discussed in LER 05000296/2014-003-00. The licensee corrected the wiring and entered the issue into the licensee's corrective action program as CR 892500. Inspectors screened the violation using IMC 0609, Appendix G, Attachment 1, Exhibit 3 Mitigating Systems Screening Questions, dated May 9, 2014. Because the finding degraded a functional auto-isolation of RHR on low reactor water level, a Phase 2 screening was required. Using attachment 3, Phase 2 Significance Determination Process Template for BWR During Shutdown, dated February 28, 2005, inspectors completed Worksheet 1 for Loss of Inventory in Plant Operating State 1 (Head On) and determined the risk was approximately 1e-7/yr, which was less than the 1e-6/yr threshold for a greater than Green finding. The dominant core damage sequence was the failure to isolate a reactor coolant leak and subsequent failure by operators to open vent paths (e.g. a safety relief valve) to control RCS pressure to enable continued low pressure injection. In the evaluation, no operator recovery credit was given for leak isolation, but credit was given for the redundant isolation valve that was operable which could have satisfied the automatic isolation function. The Regional Senior Reactor Analyst performed a detailed risk review of the finding. The risk review considered both the outage related risk, and the risk associated with a trip from power that would have the plant in shutdown cooling during the recovery. A screening analysis using bounding assumptions and the risk models ISLRHR event tree was performed. The dominant cutsets involved failure of the redundant valve to operate, and operator actions to recover. Because of the short exposure time during the shutdown periods, the redundant valve with the automatic action available, and the availability of operator recovery, the Finding was determined to be Green. This violation is being treated as an NCV consistent with Section 2.3.2 of the Enforcement Policy. |
Site: | Browns Ferry |
---|---|
Report | IR 05000296/2016001 Section 4OA7 |
Date counted | Mar 31, 2016 (2016Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | A Blamey A Nielsen A Ruh C Fontana D Dumbacher R Kellner R Powell R Williams S Sanchez T Stephen |
Violation of: | 10 CFR 50 Appendix B Criterion V |
INPO aspect | |
' | |
Finding - Browns Ferry - IR 05000296/2016001 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|---|
Finding List (Browns Ferry) @ 2016Q1
Self-Identified List (Browns Ferry)
| ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||