3F1004-01, September 2004 Monthly Operating Report for Crystal River Unit 3

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September 2004 Monthly Operating Report for Crystal River Unit 3
ML042920047
Person / Time
Site: Crystal River Duke Energy icon.png
Issue date: 10/13/2004
From: Franke J
Progress Energy Florida
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
3F1004-01, ITS 5.7.1.2
Download: ML042920047 (3)


Text

Progress Energy Crystal River Nuclear Plant Docket No. 50-302 Operating license No. DPR-72 Ref: ITS 5.7.1.2 October 13, 2004 3F1004-01 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555-0001

Subject:

Crystal River Unit 3 - September 2004 Monthly Operating Report

Dear Sir:

Florida Power Corporation, doing business as Progress Energy Florida, Inc., hereby submits the Crystal River Unit 3 (CR-3) September 2004 Monthly Operating Report in accordance with CR-3 Improved Technical Specification 5.7.1.2.

If you have any questions regarding this submittal, please contact Mr. Sid Powell, Supervisor, Licensing and Regulatory Programs at (352) 563-4883.

Si Plant General Manager JAF/ff Attachment xc: Regional Administrator, Region II Senior Resident Inspector NRR Project Manager Progress Energy Florida, Inc.

Crystal River Nuclear Plant 15760 W. Power Line Street Crystal River, FL34428 I--F& a

APPENDIX A OPERATING DATA REPORT DOCKET NO. 50-302 UNIT NAME FLCRP-3 DATE October 1 2004 COMPLETED BY J.E. Lane TELEPHONE (352) 795-6486 x3698' REPORTING PERIOD (Month/Year): September 2004 MONTH YEAR TO DATE CUMULATIVE DESIGN ELECTRICAL RATING (MWe-Net) 860 2 MAXIMUM DEPENDABLE CAPACITY (MWe-Net) 838 3 NUMBER OF HOURS REACTOR WAS CRITICAL 598.8 6,404.0 172,475.3 4 NUMBER OF HOURS THE GENERATOR WAS ON LINE 592.7 6,376.0 170,103.6 5 UNIT RESERVE SHUTDOWN HOURS 0.0 0.0 0.0 6 NET ELECTRICAL ENERGY GENERATED (MWH) 497,578 5,416,706 133,265,707

p APPENDIX B UNIT SHUTDOWNS DOCKET NO. 50-302 UNIT NAME FLCRP-3 DATE October 1, 2004 COMPLETED BY J.E. Lane TELEPHONE (352) 795-6486 x3698 REPORTING PERIOD: September 2004 No. Date Type Duration Reason Method of Cause / Corrective Actions F: Forced (Hours) (1) Shutting S: Scheduled Down (2) Comments 2004-03 09/06/2004 F 127.35 H 3 Switchyard breaker flashover during Hurricane Frances led to an automatic reactor trip.

SUMMARY

Crystal River Unit 3 experienced an automatic reactor trip during Hurricane Frances due to a flashover on a switchyard breaker. Salt spray caused the flashover to occur on the breaker which in turn caused protective relaying to strip the bus which powered the Startup Transformer. All plant non-safety buses were lost as a result. Prior to the breaker flashover, the other power feed to the Startup Transformer had been lost in the storm when an insulator located off-site failed on the 230KV Brookridge transmission line.

(1) Reason: (2) Method:

A-EQUIPMENT FAILURE (Explain) 1-MANUAL B-MAINTENANCE OR TEST 2-MANUAL TRIP / SCRAM C-REFUELING 3-AUTO TRIP / SCRAM D-REGULATORY RESTRICTION 4-CONTINUATION E-OPERATOR TRAINING / LICENSE EXAMINATION 5-OTHER (Explain)

F-ADMINISTRATIVE G-OPERATIONAL ERROR (Explain)

H-OTHER (Explain)