05000456/FIN-2018003-02
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Finding | |
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Title | Minor Violation |
Description | All Braidwood Station EDG governors were replaced during the late 1990s. During design testing, the licensee noted that the historical EDG frequency response had changed slightly due to installation of new electronic governors. Prior to these governor replacements, EDG frequency was always above 57 hertz (Hz) during load sequencing. However, with the newly installed electronic governors, 1A and 2A EDG frequency was observed to dip below the 57 Hz under frequency relay setpoint following start of the 1A and 2A motor-driven AF pumps. (Note that because the 1B and 2B AF pumps are diesel-driven, there is no corresponding impact on the 1B or 2B EDGs.) As a result, an external 2-second time delay, provided by an Agastat time delay relay, was incorporated into the under frequency trip logic for the 1A and 2A EDGs to provide an additional margin for frequency recovery following motor-driven AF pump load starts. The Braidwood governor modification was installed in 1998, with the external time delay added to the 1A and 2A EDGs as part of the design changes to prevent inadvertent actuations of the under frequency logic.During the licensees investigation into the issue discussed in the subject LER, it was identified that the external Agastat time delay was installed incorrectly on the 1A EDG. Specifically, the original trip logic wiring had not been properly removed, which permitted the actuation of the under frequency trip after the original 0.5 second internal time delay through the bypassing of the additional 2.0 second external time delay. The wiring error was introduced during the original modification installation in October 1998. Screening: The inspectors determined that the error was of minor safety significance. Absent the mechanical binding of the manual fuel trip lever and associated linkage, as discussed in NCV 05000456/201800301 in this report, the 1A EDG had performed reliably and satisfactorily during surveillance testing prior to the Unit 1 refueling outage testing in April of 2018. Additionally, the inspectors determined that the error, having occurred some 20 years ago, was not indicative of current licensee performance.Violation: This failure to comply with the requirements of 10 CFR Part 50, Appendix B, Criterion III , Design Control, constitutes a minor violation that is not subject to enforcement action in accordance with the NRCs Enforcement Policy. |
Site: | Braidwood |
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Report | IR 05000456/2018003 Section 4OA3 |
Date counted | Sep 30, 2018 (2018Q3) |
Type: | Violation: Severity level Minor |
cornerstone | No Cornerstone |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | D Kimble D Betancourt R Baker K Barclay J Cassidy T Go K Pusateri M Porfirio E Duncan |
Violation of: | 10 CFR 50 Appendix B 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Braidwood - IR 05000456/2018003 | |||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Braidwood) @ 2018Q3
Self-Identified List (Braidwood)
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