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GJ(agra Pow Comruiny 333 Piedrnont Avenuo Atlanta. Getngia 30308
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, Vephone 404 526 3195 o
Ma,hng Acktrm 40 inntr+n Center Parkway Post Offce Don 1295 H,rminghani Alatrima 35201 Telephore 205 808 %81 I'4! 5(4/NMVD (W Clf(? $ yFft.'II)
W. G. Hairston, all Sen.or Vce Presnient neear orieraxins November 7, 1990 4
Docket No.
50-424 U. S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, D. C.
20555 Gentlemen:
V0GTLE ELECTRIC GENERATING PLANT LICENSEE EVENT REPORI PERSONNEL ERROR LEADS TO A TECHNICAL SPECIFICATION VIOLATION In accordance with 10 CFR 50.73, Georgia Power Company hereby submits the enclosed report related to an event which was discovered on October 8,.1990.
Sincerely, w.k.. % 4 x H. G. Hairston, III WGH,III/NJS/gm Enclo::dre:
LER 50-424/1990-020 xc: Egpraia Power Company Mr. C. K. McCoy Mr. W. B. Shiaman Mr. P. D. Rusiton Mr. R. M. Odom NORMS 1
j 1
U. S Nuclear Reaulatory Commission Mr. S. D. Ebneter, Regional Administrator Mr. D. S. Hood, Licensing Project Manager, NRR Mr. B. R. Bonser, Senior Resident Inspector, Vogtle l
l 9011150127 901107
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grm366 U.5. NVGLEAR REGULAIDRV GOMM15510N LICENSEE EVENT REPORT (LER)
FACILITY H.Mi (1)
DOGLEI huMBER (Z) r,cr (T)
VOCITE ELECIRIC GDERATING PIANT - UNIT 1 05000424 L
e, l 3 IJ1LL (4) pIR50HNEl. ERROR IJJ)S *11) A TECINICAL SPECIF1 CATION VIO1ATION EVEh! DA1E (5)
LER huMBER (6)
ALPORI DATE (7)
OTHER fACILillES lhv0LVED (6)
MON 1H DAY TEAR YEAR SED WUM ALV MON 1H DAV YEAR FACILl1Y NAMES DOCLEI hUMBER($)
05000 08 08 90 90 020 00 11 07 90 05000 I I II I
II "I
I #
OPfRATING MODE (9) 1 20.402(b) 20.405(c) 50.73(a)(2)(lv)
LEVEL 100 20.405(e)(1)(1) 50.36(c)(1) 50.73(a)(2)(v) 73.71(b) 73.71(c)
POWER
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20.405(e)(1)(ii) 50.36(c)(2) 50.73(a)(2)(vil)
OTHER (specify in
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20.405(e)(1)(lii)
T 50.73(a)(2)(1)
[ 50.73(a)(2)(vill)(A)
Abstract below) 20.405(e)(1)(lv) 50.73(a)(2)(ll) 50.73(a)(2)(vill)(B)
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PD.405(e)(1)(v)
$0.73(a)(2)(Ill)
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50.73(a)(2)(x)
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LICEhSEE CONIACI f0R THl$ LER (li)
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TELEPH0ht NUMBER AREA CODE R. M. ODG4. NUCIIAR SAFEIY AND COMPLIANCE 404 826 3201 COMPLETE oNE LihE FOR EACH FAILURE DESCRIBED IN THl$ REPORT (13)
NVFAC=
R PORT CAU2E DYSTEM COMPONENT MAwUFAC-R P0Ri
CAUSE
SYSTEM COMPONENT M[Up(g 7UR wppg
$UPPLEMENTAL REPOR1 EXPECIED (14)
MON 1H DAY YEAR EXPECTED l"E] NO SUBMISSION Dt.iE (1$)
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YES(If yes, complete EXPECTED SUBMIS$10N DATE) l ABt1RACT (16)
On 8 8-90, an electrician was performing monthly preventive maintenance (PM) on battery bank 1CD1B in the 125 volt DC Class 1E electrical system.
Several parameters on each battery cell aere measured and recorded on the " Battery Maintenance Data Sheet" attached to the PM work order.
The PM was completed and signed-off as approved by the electrician's foreman.
l On 10-8-90, the system engineer was reviewing the above mentioned work order and identified that the measured voltage of cell #35 was recorded as 2.12 volts.
Technical Specification (TS) Table 4.8 2 requires the float voltage for each connected cell to be greater than or equal to 2.13 volts.
Therefore, a violation of TS occurred when the voltage parameter had not been verified to be restored in the required time frame and the TS action statement was not implemented. Upon identification by the system engineer, the Shift Supervisor was advised of this condition and was informed that the float voltage of the battery cell involved had been found to be acceptable during two subsequent PM's on 8-29 90 and 10 2-90.
The cause of this event was a personnel error on the part of the electrician and the maintenance foreman. Although the voltage acceptance criteria identified in the TS was not met, the electrician and foremar' erroneously approved the measurements. These individuals have been counseled regarding the importance of attention to detail.
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$1 8/31/88 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FAClllTY NAMI (1)
DOCKL1 NUMBlR (?)
L(R NUMBER (b)
PAG [ (3) 1[AR 5[Q hbM "V
VOCTLE ELE &iRIC CENERATING PINff UNIT 1 05000424 90 020 00 2
or 3
I T[K1 A.
REQUIREMENT FOR REPOR1 This report is required per 10 CFR 50.73 (a)(2)(1) because the unit operated in a condition outside of Technical Specification (TS) requirements. A Limiting Condition for Operation (LCO) actica statement was not completed within the allowable time when a component (a battery cell) was outside of its operability requirements.
B.
UNIT STATUS AT TIME OF EVENT At the time of the occurrence of this event on 8 8 90, Unit I was operating in Mode 1 (Power Operation) at 100% of rated thermal power.
Other than that described herein, there was no inoperabic equipment which contributed to the occurrence of this event.
C.
DESCRIPTION OF EVENT
On 8 8 90, an ciectrician was performing monthly preventive maintenance (PH) on battery bank 1CD1B in the 125 volt DC Class 1E electrical system per procedure 27915 C, "Ceneral Battery Haintenance".
Several parameters on each battery cell were measured and recorded on the " Battery Maintenance Data Sheet" attached to ths PM work order.
The PM was completed and signed off as approved by the electrician and foreman.
On 10 8-90, the system engineer was reviewing the above mentioned work order and identified that the measured voltage of cell #35 was recorded as 2.12 volts. Table 4.8-2 of the TS requires the float volta &c for each connected cell to be greater than or equal to 2.13 volts. This table also allows float voltages betwoon 2.10 volts and 2.13 volts provided ths.t this parameter is restored to its 2.13 volt lower limit in 7 days. Otherwise, the TS 3.8.2.1 action statement applies as follows:
"With less than the above minimum required D. C. electrical sources OPERABLE restore the inoperable D. C electrical sources to OPERABLE stacus within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> or be in at least il0T STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and in COLD SilUTDOWN within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
Therefore, a violation of TS occurred on 8-15 90 when the voltage parameter I
had not been verified to be restored within 7 days and the TS 3,8.2,1 action statement was not impicmented. Upon identification by the system engineer on 10-8 90, the Shift Supervisor was advised of this condition and was informed that the float voltage of the battery cell involved had been found
.to be acceptable during two subsequent PM's on 8 29-90 and 10 2 90.
D.
CAUSE OF EVENT
The cause of th;d event was a cognitive personnel error on the part of the cicctrician and maintenance foreman. Although the voltage acceptance criteria identified in the TS and in the PM procedure was not met, they erroneously approved the measurements. This error was not the result of-any unusual characteristics of the work location.
[8W,*#***
$$5ROL 50$15 I 58 8/31/88 LICENSEE EVENT REPORT (LER) TEXT CONTINUATION FACILITY NAME (1)
DOCKET huMBER (2)
LER NUMBER (5)
PAGE (3)
)[AR SEQ hum EEV VX.TLE EIICIRIC CINERATINC PIAVT UNIT 1 05000424 90 020 00 3
or 3
TEXI E.
ANALYSIS OF EVENT
Hessurements taken, both prior to the 8-8 90 event and again on 8-29-90 and 10 2-90, indicated acceptable cell voltage values.
Furthermore, due to the amount of data which must be transcribed during these monthly surveillances, we believe that the unaccepts.ble float voltage recorded on 8 8 90 was the result of a transcription error and not a real problem with float voltage.
Finally, the other three battery banks in the system remained operable during the period of time involved.
Based on these considerations, there was no adverse effect on plant safety or public health and safety as a result of this event.
F.
CORRECTIVE ACTIONS
1.
The Georgia Power Company electrician and foreman involved have been counseled regarding the importance of attention to detail, 2.
A memo has been sent to other appropriate personnel describing this event and the need for adequate reviews.
3 ~. Battery cell #35 has been designated a pilot cell, which requires more L
frequent (weekly) testing. This will allow future problems with cell
- 35 to be identified sooner.
4.
A review of the various surveillances and PMs which are required for the batteries is in progress in an effort to eliminate duplication and simplify data recording. This review will be completed and incorporated into procedures by 1-31-91.
C.
ADDITIONAL INFORMATION
1.
Failed Components:
None 1
2.
Previous Similar Events
LER 50 424/1989-019, dated 1-2 90.
Corrective actions from this LER included personnel counseling and procedure enhancement.
3.
Energy Industry Identification System Code:
125 volt DC Class 1E Electrical System - EJ
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| 05000424/LER-1990-001-02, :on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch Adjusted |
- on 900124,reactor Tripped When MSIV Failed to Reopen Automatically at 10% Closed Position,As Designed & Indicator Illuminated & Position Indication Lost.Caused by Failed Fuses.Fuses Replaced & Switch Adjusted
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000425/LER-1990-001-03, :Surveillances Performed on 900103 & 0201 Failed to Meet Requirements of Tech Specs 4.6.1.1.a.Caused by Personnel Misled to Believe That Only 2 of 41 Items Verified.Sts Revised |
- Surveillances Performed on 900103 & 0201 Failed to Meet Requirements of Tech Specs 4.6.1.1.a.Caused by Personnel Misled to Believe That Only 2 of 41 Items Verified.Sts Revised
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-001, :on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure Carefully |
- on 900103,misleading Task Sheet Leads to Inadequate Tech Spec Surveillances Found.Caused by Deficient Technical Review of Rev to Sts.Personnel Involved Counseled Re Importance of Reviewing Procedure Carefully
| 10 CFR 50.73(a)(2)(i) | | 05000424/LER-1990-002-02, :on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing Performed |
- on 900215,discovered That Train C Auxiliary Feedwater Sys Actuation Relay K266 Improperly Tested.On 900216,discovered That Automatic Diesel Generator Electrical Trip Not Tested.Testing Performed
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-002-03, :on 900320,generator Primary Differential Relay Energized,Causing Generator,Turbine & Reactor Trips & Fault Which Tripped Reserve Auxiliary Transformers a & B.Caused by Incorrect Tap Settings.Settings Corrected |
- on 900320,generator Primary Differential Relay Energized,Causing Generator,Turbine & Reactor Trips & Fault Which Tripped Reserve Auxiliary Transformers a & B.Caused by Incorrect Tap Settings.Settings Corrected
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000424/LER-1990-003-01, :on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps Replaced |
- on 900223,discovered 16 Transformer Core Clamp Bolts Missing on Seismically Qualified Switchgear. Caused by Installation Error During Const Phase of Plant. Missing Clamps Replaced
| 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-003, S-01:on 900425,engineering Supervisor Observed Unsecured & Unattended Safeguards Cabinet in Engineering Support Dept Ofc Area.Caused by Cognitive Personnel Error. Engineer Counseled | S-01:on 900425,engineering Supervisor Observed Unsecured & Unattended Safeguards Cabinet in Engineering Support Dept Ofc Area.Caused by Cognitive Personnel Error. Engineer Counseled | | | 05000424/LER-1990-004-01, :on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2 |
- on 900301,failure to Comply W/Tech Spec 3.0.4 Occurred on Entry Into Mode 6.Caused by Cognitive Personnel Error.Util Complied W/Action Requirements for Tech Spec 3.9.2
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-004-02, :on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs |
- on 900411,power Range Calorimetric Channel Calibr Not Performed.Caused by Cognitive Personnel Error. Unit Shift Supervisor Counseled Re Importance of Complying W/Tech Specs
| 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-005, :on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator Counseled |
- on 900314,observed That Indicator Lights for Actuation Handswitches for Trains a & B of Fuel Handling Bldg Showed Actuation Occurred.Caused by Personnel Error. Operator Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000425/LER-1990-005-02, :on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card Replaced |
- on 900427 & 29,computer Point FO-424A Discovered to Be Reading Lower than Control Board Indications.Caused by Intermittent Failure of Computer. Computer Input Card Replaced
| | | 05000425/LER-1990-006-01, :on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate Action |
- on 900501,data Processing Module Was Taken to Purge Which Rendered Both Monitors 2RE-2562C & 2RE-2562A Inoperable.Caused by Personnel Error.Memo Issued to Chemistry Dept Personnel Re Appropriate Action
| 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-007, S-00:on 900829,safeguards Info Container Observed Unsecured & Unattended in Document File Room.Caused by Safeguards Info Coordinator Failure to Secure Container Before Going to Lunch.Coordinator Counseled & Reprimanded | S-00:on 900829,safeguards Info Container Observed Unsecured & Unattended in Document File Room.Caused by Safeguards Info Coordinator Failure to Secure Container Before Going to Lunch.Coordinator Counseled & Reprimanded | | | 05000425/LER-1990-007-02, :on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV Tested |
- on 900506,control Room Operators Received Trouble Alarms Indicating Closure of MSIV 2HV-30264 & Steam Generator 3 Low Level Water Level.Caused by Relay Failure. Failed Relay Replaced & MSIV Tested
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000425/LER-1990-008-02, :on 900628,indication Received in Control Room That MSIV 2HV-3026A Was Closing.Caused by Failure of O-ring Which Seals Connection of Nonpump Side Manifold Assembly to Boss on Actuator cylinder.O-ring Replaced |
- on 900628,indication Received in Control Room That MSIV 2HV-3026A Was Closing.Caused by Failure of O-ring Which Seals Connection of Nonpump Side Manifold Assembly to Boss on Actuator cylinder.O-ring Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000424/LER-1990-008, S-00:on 901011,eleven Documents Found Unattended & Unsecured in Folder on Desk Being Moved.Caused by Cognitive Personnel Error.Safeguards Documents Returned to Their Approved Storage Container | S-00:on 901011,eleven Documents Found Unattended & Unsecured in Folder on Desk Being Moved.Caused by Cognitive Personnel Error.Safeguards Documents Returned to Their Approved Storage Container | 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(1) 10 CFR 50.73(a)(1)(v) | | 05000425/LER-1990-009-02, :on 900630,manual Reactor Trip Initiated Due to Delays in Synchronization to Grid.Caused by Cognitive Personnel Error by Shift Superintendent.Personnel Counseled & Operating Procedure Revised |
- on 900630,manual Reactor Trip Initiated Due to Delays in Synchronization to Grid.Caused by Cognitive Personnel Error by Shift Superintendent.Personnel Counseled & Operating Procedure Revised
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000424/LER-1990-009, :on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation Signal |
- on 900413,inadvertent Feedwater Isolation Occurred.Caused by Procedural Inadequacy.Procedure Revised to Have Input Error Inhibit Switch Placed in Normal First & Reinstate Block on Feedwater Isolation Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000425/LER-1990-010-02, :on 900702,observed That Unit 2 Process & Effluent Radiation Monitoring Sys Computer Screen Displayed Active Limiting Condition for Operation Against 2RE-2562C. Caused by Personnel Error.Personnel Counseled |
- on 900702,observed That Unit 2 Process & Effluent Radiation Monitoring Sys Computer Screen Displayed Active Limiting Condition for Operation Against 2RE-2562C. Caused by Personnel Error.Personnel Counseled
| 10 CFR 50.73(a)(2)(i) | | 05000424/LER-1990-010, :on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals Counseled |
- on 900418,oncoming Shift Supervisor Found That Containment Level C Temp Improperly Recorded.Caused by Data Being Recorded & Reviewed from Malfunctioning Indication.Individuals Counseled
| 10 CFR 50.73(a)(2)(1) | | 05000425/LER-1990-011-02, :on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for Analysis |
- on 900830,containment Ventilation Isolation Occurred.Caused by Failure of Random Access Memory (RAM) Circuit Board in Data Processing Module.Failed RAM Board Replaced & Returned to Vendor for Analysis
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000424/LER-1990-011, :on 900425,reactor Manually Tripped Due to Inadvertent Closure of Main Feed Regulating Valve.Caused by Mispositioning of Local Control Levers.Local Control Levers Removed |
- on 900425,reactor Manually Tripped Due to Inadvertent Closure of Main Feed Regulating Valve.Caused by Mispositioning of Local Control Levers.Local Control Levers Removed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000424/LER-1990-012, :on 900529,discovered That Sequencer Delay Times Not Taken Into Account During Summation Procedure for Control Room Emergency Filtration Sys.Caused by Inadequate Procedure Review.Procedures Changed |
- on 900529,discovered That Sequencer Delay Times Not Taken Into Account During Summation Procedure for Control Room Emergency Filtration Sys.Caused by Inadequate Procedure Review.Procedures Changed
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-012-02, :on 900916,shift Supervisor Inadvertently Issued Mode 5 Clearance to Remove Train a & B Containment Spray Sys Pumps from Svc for Maint |
- on 900916,shift Supervisor Inadvertently Issued Mode 5 Clearance to Remove Train a & B Containment Spray Sys Pumps from Svc for Maint
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(1) | | 05000425/LER-1990-013-02, :on 900926,removing Power to Plant Vent Monitor Led to Tech Spec Violation |
- on 900926,removing Power to Plant Vent Monitor Led to Tech Spec Violation
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000424/LER-1990-013, :on 900601,discovered That Containment Air Lock Leakage Surveillance Exceeded 6-month Test Interval,Per Tech Spec 4.6.1.3.b.Caused by Personnel Error.Plant Surveillance Tracking Program Revised |
- on 900601,discovered That Containment Air Lock Leakage Surveillance Exceeded 6-month Test Interval,Per Tech Spec 4.6.1.3.b.Caused by Personnel Error.Plant Surveillance Tracking Program Revised
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-014-02, :on 900927 & 1001,unmonitored Liquid Release Occurred Due to Failure to Restore Steam Generator Blowdown Effluent Line Radiation Monitor 2RE-0021 to Svc After Being Isolated & Valved Out |
- on 900927 & 1001,unmonitored Liquid Release Occurred Due to Failure to Restore Steam Generator Blowdown Effluent Line Radiation Monitor 2RE-0021 to Svc After Being Isolated & Valved Out
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-015, :on 900712,calibr Requirements Not Applied to Computer Points Used for Obtaining Final Feedwater Temp Input Valves.Caused by Cognitive Personnel Error.Precision Heat Balance Procedure to Be Revised |
- on 900712,calibr Requirements Not Applied to Computer Points Used for Obtaining Final Feedwater Temp Input Valves.Caused by Cognitive Personnel Error.Precision Heat Balance Procedure to Be Revised
| 10 CFR 50.73(a)(2)(i) | | 05000425/LER-1990-015-02, :on 901026,missed Procedure Step Results in Inadvertent Operation of ESF Components |
- on 901026,missed Procedure Step Results in Inadvertent Operation of ESF Components
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(1) | | 05000425/LER-1990-016-02, :on 901108,personnel Error Led to Auxiliary Feedwater Sys Actuation |
- on 901108,personnel Error Led to Auxiliary Feedwater Sys Actuation
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(s)(2) | | 05000424/LER-1990-016, :on 900723,determined That Failed 4,160/480- Volt non-1E Transformer Led to Main Feed Pump Trip & Reactor Trip.Caused by Internal Fault in 1NB01 Transformer.Failed Transformer Replaced |
- on 900723,determined That Failed 4,160/480- Volt non-1E Transformer Led to Main Feed Pump Trip & Reactor Trip.Caused by Internal Fault in 1NB01 Transformer.Failed Transformer Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000425/LER-1990-017-02, :on 901110,LCO 3.0.3 Entered Due to Inoperable Step Demand Counters for Control Bank D |
- on 901110,LCO 3.0.3 Entered Due to Inoperable Step Demand Counters for Control Bank D
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-017, :on 900305,sys Engineer Found That Certain Electrical Circuits Not Identified for Testing During Performance of Procedure.Caused by Inadequate ESFAS Test Procedure.Procedure 00404-C Revised |
- on 900305,sys Engineer Found That Certain Electrical Circuits Not Identified for Testing During Performance of Procedure.Caused by Inadequate ESFAS Test Procedure.Procedure 00404-C Revised
| 10 CFR 50.73(a)(2)(i) | | 05000424/LER-1990-018-01, :on 900907,discovered That Surveillance Required by Tech Spec 4.0.5 & ASME Section XI Inadequately Performed.Caused by Procedure Inadequacy.Procedure Corrected & Operability of Check Valve Reverified |
- on 900907,discovered That Surveillance Required by Tech Spec 4.0.5 & ASME Section XI Inadequately Performed.Caused by Procedure Inadequacy.Procedure Corrected & Operability of Check Valve Reverified
| 10 CFR 50.73(a)(2)(i) | | 05000424/LER-1990-019-01, :900314,engineer Discovered Condition Which Would Allow Inservice Insps of Containment Isolation Valves to Be Performed Following Completion of ASME Section XI Local Leak Rate Testing |
- 900314,engineer Discovered Condition Which Would Allow Inservice Insps of Containment Isolation Valves to Be Performed Following Completion of ASME Section XI Local Leak Rate Testing
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(1) | | 05000424/LER-1990-020-01, :on 900808,personnel Error Led to Tech Spec Violation |
- on 900808,personnel Error Led to Tech Spec Violation
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-021-01, :Between 901202-03,special Condition Surveillance Not Performed When Rod Position Deviation Monitor Inoperable.Caused by Personnel Error.Future Training on Proteus Computer Planned |
- Between 901202-03,special Condition Surveillance Not Performed When Rod Position Deviation Monitor Inoperable.Caused by Personnel Error.Future Training on Proteus Computer Planned
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(1) 10 CFR 50.73(e)(2)(iv) | | 05000424/LER-1990-021, :on 901202,special Condition Surveillance Not Performed When Rod Position Deviation Monitor Inoperable. Caused Personnel Error.Personnel Under Went Positive Discipline Re Compliance W/Procedures |
- on 901202,special Condition Surveillance Not Performed When Rod Position Deviation Monitor Inoperable. Caused Personnel Error.Personnel Under Went Positive Discipline Re Compliance W/Procedures
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) | | 05000424/LER-1990-022-01, :on 901212,auditor Found Possible Discrepancy in Calculation for Determining Filter Unit Electrical Heater Power Dissipation.Caused by Architect/Engineer.Request for Tech Spec Change Submitted |
- on 901212,auditor Found Possible Discrepancy in Calculation for Determining Filter Unit Electrical Heater Power Dissipation.Caused by Architect/Engineer.Request for Tech Spec Change Submitted
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(x) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(1) 10 CFR 50.73(e)(2)(v) 10 CFR 50.73(h)(2) | | 05000424/LER-1990-023-01, :on 901218,4160/480 Volt non-1E Transformer Experienced Internal Fault.Cause Indeterminate.Failed Transformer Replaced & Further Study of Possible Factors Which May Have Led to Failure in Progress |
- on 901218,4160/480 Volt non-1E Transformer Experienced Internal Fault.Cause Indeterminate.Failed Transformer Replaced & Further Study of Possible Factors Which May Have Led to Failure in Progress
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(1) 10 CFR 50.73(s)(2) | | 05000424/LER-1990-024-01, :on 900807,Unit 2 Containment Isolation Valves Associated W/Train a Closed & Unit 1 Valves Opened for Testing.Caused by Procedural Inadequacy.Procedures Revised & Procedure Coordinator Informed |
- on 900807,Unit 2 Containment Isolation Valves Associated W/Train a Closed & Unit 1 Valves Opened for Testing.Caused by Procedural Inadequacy.Procedures Revised & Procedure Coordinator Informed
| 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) |
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