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Category:Letter
MONTHYEARCNL-24-082, Central Emergency Control Center Emergency Plan Implementing Procedure Revision2024-12-17017 December 2024 Central Emergency Control Center Emergency Plan Implementing Procedure Revision CNL-24-009, Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations2024-12-17017 December 2024 Brown Ferry Nuclear Plant, Units 1, 2 & 3; Sequoyah Nuclear Plant, Units 1 & 2 and Watts Bar Plant, Units 1 & 2 - Triennial Decommission Funding Plans for Independent Spent Fuel Storage Installations IR 05000390/20243012024-12-16016 December 2024 NRC Operator License Examination Report 05000390/2024301 and 05000391/2024301 ML24352A0092024-12-16016 December 2024 Investigation Summary, Office of Investigations Case Number 2-2023-007 ML24346A3982024-12-16016 December 2024 NRC Examination Results Summary Examination Report 05000390/2024301 and 05000391/2024301 CNL-24-072, Request for Alternative to Extend First Containment Inservice Inspection Interval2024-12-12012 December 2024 Request for Alternative to Extend First Containment Inservice Inspection Interval CNL-24-075, Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and W2024-11-27027 November 2024 Response to Request for Additional Information for Application to Revise Function 5 of Technical Specification Table 3.3.2-1, Engineered Safety Feature Actuation System Instrumentation, for the Sequoyah and Watts Bar (SQN-TSTS-23-02 and WBN ML24297A4632024-11-21021 November 2024 – Environmental Assessment and Finding of No Significant Impact Related to Recapture of Low-Power Testing Time CNL-24-080, Response to Request for Additional Information Regarding Application to Revise Updated Final Safety Analysis Report Regarding Changes to Hydrologic Analysis (WBN-19-011)2024-11-20020 November 2024 Response to Request for Additional Information Regarding Application to Revise Updated Final Safety Analysis Report Regarding Changes to Hydrologic Analysis (WBN-19-011) IR 05000390/20240032024-11-13013 November 2024 Integrated Inspection Report 05000390/2024003, 05000391/2024003 & 07201048/2024001 CNL-24-021, Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020)2024-11-12012 November 2024 Application to Revise Technical Specification Limiting Condition of Operation 3.5.2, ECCS – Operating, Note 1 to Include Residual Heat Removal Pump Flow Paths (SQN-TS-23-04 and WBN-TS-23-020) CNL-24-014, License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22)2024-11-0404 November 2024 License Amendment Request to Revise the Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 Technical Specifications to Use Online Monitoring Methodology (SQN-TS-24-02 and WBN-TS-23-22) IR 05000390/20250102024-11-0404 November 2024 Notification of an NRC (FPTI) (NRC Inspection Report 05000390/2025010 0500039/ 2025010) (RFI) CNL-24-064, Response to Request for Additional Information Regarding the Watts Bar Nuclear Plant, Unit 2 Steam Generator Tube Inspection Report for U2R52024-11-0404 November 2024 Response to Request for Additional Information Regarding the Watts Bar Nuclear Plant, Unit 2 Steam Generator Tube Inspection Report for U2R5 CNL-24-074, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-10-23023 October 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions ML24290A1202024-10-17017 October 2024 Operator Licensing Examination Approval 05000390/2024301 and 05000391/2024301 ML24282B0412024-10-15015 October 2024 Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2 and Watts Bar Nuclear Plant, Units 1 and 2 ML24261C0062024-10-0404 October 2024 Correction to Amendment No. 134 to Facility Operating License No. NPF-90 and Amendment No. 38 to Facility Operating License No. NPF-96 ML24260A1682024-10-0404 October 2024 Regulatory Audit Summary Related to Request to Add and Revise Notes Related to Technical Specification Table 3.3.2-1, Function 5 ML24284A1072024-09-26026 September 2024 Affidavit for Request for Withholding Information from Public Disclosure for Sequoyah Nuclear Plant, Units 1 and 2, and Watts Bar Nuclear Plant, Units 1 and 2 CNL-24-047, Decommitment of Flood Mode Mitigation Improvement Systems2024-09-24024 September 2024 Decommitment of Flood Mode Mitigation Improvement Systems CNL-24-060, Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description2024-09-24024 September 2024 Supplement to Request for Approval of the Tennessee Valley Authority Nuclear Quality Assurance Program Description ML24262A0602024-09-23023 September 2024 Summary of August 19, 2024, Meeting with Tennessee Valley Authority Regarding a Proposed Supplement to the Tennessee Valley Authority Nuclear Quality Assurance Plan CNL-24-065, Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-09-18018 September 2024 Tennessee Valley Authority – Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation IR 05000390/20240052024-08-28028 August 2024 Updated Inspection Plan and Assessment Follow-Up Letter for Watts Bar Nuclear Plant, Units 1 and 2 - Report 05000390-2024005 and 05000391-2024005 ML24218A1442024-08-27027 August 2024 Issuance of Amendment Nos. 169 and 75 Regarding Technical Specification Surveillance Requirement 3.9.5.1 to Reduce the Residual Heat Removal Flow Rate IR 05000390/20244022024-08-20020 August 2024 – Security Baseline Inspection Report 05000390-2024402 and 05000391/2024402 - Public CNL-24-061, Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08),2024-08-19019 August 2024 Supplement to Application to Revise Function 5 of Technical Specification Table 3.3.2-1, ‘Engineered Safety Feature Actuation System Instrumentation,’ for the Sequoyah and Watts Bar (SQN-TS-23-02 and WBN-TS-23-08), ML24219A0262024-08-12012 August 2024 Request for Withholding Information from Public Disclosure IR 05000390/20240022024-08-0707 August 2024 Integrated Inspection Report 05000390/2024002 and 05000391/2024002 Rev ML24204A2652024-07-25025 July 2024 Regulatory Audit Summary Related to Request to Revise Technical Specification Surveillance Requirement 3.9.5.1 to Reduce the Residual Heat Removal Flow Rate ML24199A0012024-07-22022 July 2024 Clarification and Correction to Exemption from Requirement of 10 CFR 37.11(c)(2) ML24172A1342024-07-15015 July 2024 Exemptions from 10 CFR 37.11(C)(2) (EPID L-2023-LLE-0024) - Letter ML24170A8002024-07-15015 July 2024 Issuance of Amendment Nos. 168 and 74 Regarding Revision to Technical Specification Table 1.1-1 for Required Number of Fully Tensioned Reactor Pressure Vessel Head Closure Bolts IR 05000390/20244402024-07-12012 July 2024 95001 Supplemental Inspection Supplemental Report 05000390-2024440 and 05000391-2024440 and Follow-Up Assessment Letter 05000391/LER-2024-003, Inoperability of Both Trains of Unit 2 Low Head Safety Injection2024-07-11011 July 2024 Inoperability of Both Trains of Unit 2 Low Head Safety Injection ML24131A0012024-07-0202 July 2024 Issuance of Amendment Nos. 167 and 73 Regarding Adoption of Technical Specification Task Force Traveler TSTF-427-A, Revision 2 CNL-24-052, Response to Request for Additional Information Regarding Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14)2024-06-27027 June 2024 Response to Request for Additional Information Regarding Application to Modify the Technical Specification Surveillance Requirement 3.9.5.1 (WBN-TS-21-14) CNL-24-018, License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources – Operating to Clarify Requirements for Diesel Generator Testing (WBN-TS2024-06-25025 June 2024 License Amendment Request for Adoption of Technical Specification Task Force Traveler TSTF-276-A, Revision 2, Regarding TS 3.8.1 AC Sources – Operating to Clarify Requirements for Diesel Generator Testing (WBN-TS ML24089A1152024-06-21021 June 2024 Transmittal Letter, Environmental Assessments and Findings of No Significant Impact Related to Exemption Requests from 10 CFR 37.11(c)(2) ML24141A0482024-05-17017 May 2024 EN 56958_1 Ametek Solidstate Controls, Inc ML24100A7642024-05-16016 May 2024 Issuance of Amendment No. 166 Regarding Revision to Technical Specification 3.8.2, AC Sources-Shutdown, to Remove Reference to C-S Diesel Generator (CNL-23-062) IR 05000390/20240012024-05-14014 May 2024 Integrated Inspection Report 05000390/2024001 and 05000391/2024001 CNL-24-040, Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions2024-05-0808 May 2024 Tennessee Valley Authority - Central Emergency Control Center Emergency Plan Implementing Procedure Revisions 05000391/LER-2024-002, Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO2024-05-0606 May 2024 Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO IR 05000391/20240072024-04-30030 April 2024 Assessment Follow-up Letter for Watts Bar Nuclear Plant, Unit 2 – Report 05000391/2024007 ML24120A1182024-04-29029 April 2024 – Notification of NRC Supplemental Inspection (95001) and Request for Information CNL-24-037, Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 422024-04-22022 April 2024 Clinch River, Sequoyah, Units 1 and 2, Watts Bar, Unit 1 and 2, Nuclear Quality Assurance Plan, TVA-NQA-PLN89-A, Revision 42 ML24087A1912024-04-18018 April 2024 Exemption from Select Requirements of 10 CFR Part 73, Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting 2024-09-05
[Table view] Category:Licensee Event Report (LER)
MONTHYEAR05000390/LER-2024-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-09-0505 September 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2024-003, Inoperability of Both Trains of Unit 2 Low Head Safety Injection2024-07-11011 July 2024 Inoperability of Both Trains of Unit 2 Low Head Safety Injection 05000391/LER-2024-002, Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO2024-05-0606 May 2024 Re Automatic Reactor Trip Due to Steam Generator 3 Level LO-LO 05000391/LER-2024-001, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2024-03-27027 March 2024 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2023-003-01, Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control2024-02-29029 February 2024 Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control 05000391/LER-2023-003, Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control2023-10-0303 October 2023 Automatic Reactor Trip Due to Loss of Main Feedwater Regulating Valve Control 05000390/LER-2023-001-01, Inadequate 10 CFR 50.59 Results in Failure to Obtain Prior NRC Approval for Condition Prohibited by Technical Specifications2023-09-27027 September 2023 Inadequate 10 CFR 50.59 Results in Failure to Obtain Prior NRC Approval for Condition Prohibited by Technical Specifications 05000391/LER-2023-002, Automatic Reactor Trip Due to Main Generator Protection Relay Actuation2023-08-24024 August 2023 Automatic Reactor Trip Due to Main Generator Protection Relay Actuation 05000391/LER-2023-001, Unanalyzed Condition Related to Loss of the 2A Emergency Diesel Generator During a Postulated Appendix R Fire2023-07-20020 July 2023 Unanalyzed Condition Related to Loss of the 2A Emergency Diesel Generator During a Postulated Appendix R Fire 05000390/LER-2023-001, Interpretation of Technical Specification (TS) Table 1.1-1 Leads to a Condition Prohibited by TS2023-07-0303 July 2023 Interpretation of Technical Specification (TS) Table 1.1-1 Leads to a Condition Prohibited by TS 05000391/LER-2021-001, Automatic Reactor Trip on Main Turbine Trip Caused by Main Feed Pump Trip Due to Low Condenser Vacuum2021-05-10010 May 2021 Automatic Reactor Trip on Main Turbine Trip Caused by Main Feed Pump Trip Due to Low Condenser Vacuum 05000390/LER-2021-001, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2021-04-20020 April 2021 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2020-004, Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking2021-01-0707 January 2021 Steam Generators Degraded Due to Axial Outside Diameter Stress Corrosion Cracking 05000390/LER-2020-005, Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 2A-A Shutdown Board2021-01-0404 January 2021 Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 2A-A Shutdown Board 05000391/LER-2020-003, Re Low RHR Flow in Mode 6 Results in a Condition Prohibited by Technical Specifications2020-12-21021 December 2020 Re Low RHR Flow in Mode 6 Results in a Condition Prohibited by Technical Specifications 05000391/LER-2020-002, Re Two Pressurizer Safety Valves Outside of Technical Specification Limits Due to Set Point Drift2020-12-17017 December 2020 Re Two Pressurizer Safety Valves Outside of Technical Specification Limits Due to Set Point Drift 05000390/LER-2020-003, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-09-10010 September 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2020-001, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-07-15015 July 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2020-002, Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 1B-B Shutdown Board2020-07-14014 July 2020 Automatic Start of the Emergency Diesel Generators Due to an Equipment Failure During Transfer of Power Source for the 1B-B Shutdown Board 05000390/LER-2020-001, Manual Reactor Trip Due to Lowering Steam Generator Level Caused by a Hand Station Failure2020-04-17017 April 2020 Manual Reactor Trip Due to Lowering Steam Generator Level Caused by a Hand Station Failure 05000390/LER-2019-004, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2020-01-13013 January 2020 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2019-003, Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed2019-10-21021 October 2019 Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed 05000391/LER-2019-002, Breach Due to Penetration Boot Seal Separation Results in Shield Building Inoperability2019-08-19019 August 2019 Breach Due to Penetration Boot Seal Separation Results in Shield Building Inoperability 05000390/LER-2019-002, Loss of Control Room Emergency Air Temperature Control System Due to Air Filter Failure2019-08-0707 August 2019 Loss of Control Room Emergency Air Temperature Control System Due to Air Filter Failure 05000391/LER-2019-001, Regarding Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed2019-07-18018 July 2019 Regarding Manual Reactor Trip Due to Main Feedwater Regulating Valve Failing Closed 05000390/LER-2018-006, Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test2019-02-11011 February 2019 Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test 05000390/LER-2018-005, Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power2018-12-19019 December 2018 Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power 05000390/LER-2018-004, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open2018-11-13013 November 2018 Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000391/LER-2018-005, For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure2018-10-22022 October 2018 For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure 05000391/LER-2018-004, Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications2018-09-21021 September 2018 Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications 05000391/LER-2018-003, Reactor Trip Due to Main Generator Differential Relay Actuation2018-08-21021 August 2018 Reactor Trip Due to Main Generator Differential Relay Actuation 05000391/LER-2018-002, Loss of Shield Building Vacuum Due to Equipment Failure2018-07-0909 July 2018 Loss of Shield Building Vacuum Due to Equipment Failure 05000390/LER-2018-002-01, Shield Building Inoperability Due to Annulus Vacuum Transient2018-06-26026 June 2018 Shield Building Inoperability Due to Annulus Vacuum Transient ML18144A9982018-05-24024 May 2018 Ventilation System Inoperable Due to Main Control Room Door Being Left Open 05000390/LER-2018-002, Regarding Shield Building Inoperability Due to Annulus Vacuum Transient2018-03-19019 March 2018 Regarding Shield Building Inoperability Due to Annulus Vacuum Transient 05000390/LER-2017-016, Regarding System Actuations Due to Opening of Feeder Breaker to the 1B-B 6.9 Kv Shutdown Board2018-02-20020 February 2018 Regarding System Actuations Due to Opening of Feeder Breaker to the 1B-B 6.9 Kv Shutdown Board 05000391/LER-2017-006, Regarding Manual Reactor Trip in Response to Indication of Multiple Dropped Control Rods2018-02-0909 February 2018 Regarding Manual Reactor Trip in Response to Indication of Multiple Dropped Control Rods 05000391/LER-1917-005, Regarding Unplanned Emergency Core Cooling System Injection Into the Reactor Coolant System Due to Personnel Error2018-01-25025 January 2018 Regarding Unplanned Emergency Core Cooling System Injection Into the Reactor Coolant System Due to Personnel Error 05000390/LER-1917-015, Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications2018-01-0808 January 2018 Regarding Failure to Enter Limiting Condition of Operation Action Statement Results in a Condition Prohibited by Technical Specifications 05000390/LER-1917-014, Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function2017-12-20020 December 2017 Regarding Main Control Room Boundary Door Left Open Leading to a Loss of Safety Function 05000390/LER-1917-013, Regarding Incorrectly Adjusted Auxiliary Building Gas Treatment System Damper Leads to a Condition Prohibited by Technical Specifications2017-11-0606 November 2017 Regarding Incorrectly Adjusted Auxiliary Building Gas Treatment System Damper Leads to a Condition Prohibited by Technical Specifications 05000390/LER-1917-012, Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications2017-10-23023 October 2017 Regarding Error in Plant Emergency Procedures Leads to a Condition Prohibited by the Technical Specifications 05000390/LER-1917-011, Regarding Failure to Enter Technical Specification 3.6.3 for Containment Lsolation Valve2017-10-23023 October 2017 Regarding Failure to Enter Technical Specification 3.6.3 for Containment Lsolation Valve 05000390/LER-1917-010, Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board2017-10-10010 October 2017 Regarding Actuation of Turbine Driven Auxiliary Feedwater Pump Due to Loss of 6.9kV Shutdown Board 05000391/LER-1917-004, Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication2017-09-25025 September 2017 Regarding Manual Reactor Trip Due to Inoperable Rod Position Indication 05000390/LER-1917-008, Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation2017-08-14014 August 2017 Regarding Shield Building Inoperability and Potential Loss of Safety Function Resulting from Spurious Equipment Operation 05000390/LER-1917-007, Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance2017-08-0808 August 2017 Regarding Multiple Unreported Potential Loss of Safety Function Events Associated with Inoperable Single Train Systems Due to Misinterpretation of Reporting Guidance 05000390/LER-1917-006, Regarding Structural Degradation of 161 Kv Line Pole Leads to a Condition Prohibited by Technical Specifications2017-07-31031 July 2017 Regarding Structural Degradation of 161 Kv Line Pole Leads to a Condition Prohibited by Technical Specifications 05000390/LER-1917-005, Re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications2017-07-10010 July 2017 Re Isolation of the 1B-B Safety Injection Pump Leads to a Condition Prohibited by Technical Specifications 05000390/LER-1917-004, Regarding Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup2017-06-29029 June 2017 Regarding Manual Reactor Trips Due to Failed Reactor Coolant Pump Power Transfer During Plant Startup 2024-09-05
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LER-2018-003, Reactor Trip Due to Main Generator Differential Relay Actuation |
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Tennessee Valley Authority, Post Office Box 2000, Spring City, Tennessee 37381 August 21, 2018 10 cFR 50.73 ATTN: Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555-0001 Watts Bar Nuclear Plant, Unit 2 Facility Operating License No. NpF-96 NRC Docket No.50-391 subject: Licensee Event Report 3911201&-003-00, Reactor Trip Due to Main Generator Differential Relay Actuation This submittal provides Licensee Event Report (LER) 391t2018-OO3-00. This LER provides details concerning a plant trip as a result of an electrical issue with a main generator differential current relay circuit. This condition is being reported in accordance with 10 CFR 50.73(aX2XivXA) as an automatic actuation or the Reactor Protection System and the Auxiliary Feedwater Systems.
There are no new regulatory commitments contained in this letter. Please direct any questions concerning this matter to Kim Hulvey, wBN Licensing Manager, at (423) 365-7720.
Respectfully, Site Vice President Watts Bar Nuclear Plant Enclosure cc: See Page 2
U.S. Nuclear Regulatory Commission Page 2 August 21, 2018 cc (Enclosure):
NRC Regional Administrator - Region ll NRC Senior Resident lnspector - Watts Bar Nuclear Ptant
NRC FORM 366 (02-2018)
O"o'"*"ra U.S. NUCLEAR REGULATORY COMMISSION LICENSEE EVENT REPORT (LER)
APPROVED BY OMB: NO. 3100-0104 EstimaEd burden per Bsponse b comply wifrr this mandatory collection request 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />.
ReporEd lessons learned are incorporabd into the licensing process and Ed back b indusfy. Send comnents regarding burden estimab to the lnformation Services Branch [t-2 F43), u.s. Nuchar Regulabry commission, washington, DC 205s$0001,0r by e-mail to lnfocollec8. Resource@nrc.gov, and b flre Desk fficer, ffice of lnformati-on ard Reguldory Afiairs, NE0&10202, (31s0-0104), office, of Management and Budget Washingbn, DC 20503. lf a means used h impose an information collection does not display a cunenty valid OMB oonfol number, flre NRC may not conduct on sponsor, and a person is notreguircd b respond b, fie infomation collection.
- 1. Facility Name Watts Bar Nuclear Plant, Unit 2
- 2. Docket Number 05000391
- 3. Page 1 0F4
- 4. Title Reactor Trip Due to Main Generator Differential Relay Actuation
- 5. Event Date
- 6. LER Number
- 7. Report Date
- 8. Other Facilities lnvolved Monthl Day I Year year I S.quential I
Number Rev No.
Month I Day Year Facility Name N/A losooo 06 22 I 2018 2019 -003
- - 00 08 21 2018 Facility Name
- 9. Operating Mode I l. This Report is Submitted Pursuant to the Requirements of 10 CFR g: (Check a1 that apply) 1 n zo.2zo1(b) 2o.22os(aX3)(i) n 50.73(aX2XiiXA) tr 50.73(aX2XviiiXA) n 20.2201(d) tr 20.2203(aX3)(ii) n 50.73(aX2X.iXB) n 50.73(aX2XviiiXB) tl 2o.z2o3(a)(1) tr zo.22o3(aX4) tr 50.73(a)(2xiii) tr 50.73(aX2Xix)(A)
D 20.2203(aX2Xi) n 50.36(cXlXiXA)
X 50.73(aX2)(ivXA) n 50.73(a)(2Xx)
- 10. Power Level n 20.2203(aX2)(ii) n 50.36(cxl XiiXA) n 50.73(aX2XvXA) tr rc.r1(a)(4) 96 tr 20.2203(aX2)(i.i) tr 50.36(cX2) tr s0.73(aX2Xv)(B) n rs.r1(a)(s) n 2o.22os(aX2Xiv) tr 50.46(ax3)(ii) n 50.73(aX2)(v)(c) tl rc.72(a)(1) tr 20.2203(aX2Xv) n 50.73(aX2XiXA) tr 50.73(aX2)(vXD) n B.rz(a)(2xu tr 20.2203(aX2Xvi) tr 50.73(aX2)(iXB) tr 50.73(aX2Xvii) tr B.rr(a)(2xii) tr 50.73(aX2XiXc) n OTHER Specify in Abstract betow or in G. Failure mode, mechanism, and effeit of each faired component The likely failure mode of equipment associated with this event is an intermittent equipment failure between the neutral side current transformer of the main generator and the protectibn relays which led to actuation of the A phase main transformer differential current relay.
H. Operator actions
Operations personnel promptly stabilized the plant following the plant trip
l. Automatically and manually initiated safety system responses
The turbine trip resulted in a reactor trip. Safety systems responded as expected, including reactor trip and automatic initiation of AFW.
lll.
Cause of the Event
A. cause of each component or system failure or personnel error The troubleshooting performed following the event did not definitively identify the cause of the trip.
The most probable ctuse of the event is an intermittent equipment fiilure inifre n phase signal loop between the generator neutral current transformer (251'CT loop) {ElIS:XCT} ind the digitat protection relays (2-RLY-244-S300G3/1 and 2-RLY-244-M3425N2ietiys) which ted to actuation of the A phase main transformer differential current relay (287T){EllS:8i}.' The source of the intermittent equipment failure will be further investigated during tire Spring 2019 Unit 2 refueling outage.
B. Cause(s) and circumstances for each human performance related root cause
No human performance root causes are attributed to this event.
lV. Analysis of the Event On June 22,2018, an intermittent electrical equipment issue of slightly over one cycle (16.7 milliseconds) was measured on the A phase of the main transformer which caused an actuation of the digital protective relays, resulting in a. generatgr trip. The automatic Unit 2 reactor trip that occurred on Junj22, )Ot A is generally comparable to the Updated Final Safety Analysis Report (UFSAR) description of the Loss of External Electrical Load and/or Turbine Trip described in UFSAR Section t6.Z.l. Following the trif, Operations entered 2-E-O, Reactor Trip or Safety lnjection, and subsequenfly transitioned to Z-gS-0. t, Reactor Trip Response, to place Unit 2 in Mode 3 using procedure 2-GO-5, [Jnit Shutdown from 30 percent Reactor Power to Hot Standby. This reactor trip is considered uncomplicated.
V. Assessment of Safety Consequences
As described in the previous section, the trip that occurred was uncomplicated and is bounded by the loss of external electrical load event described in the UFSAR. A probabilistic risk analysis performed ior this event indicates the conditionalcore damage probability from this event is very small.
A. Availability of systems or components that could have performed the same function as the components and systems that failed during the event Not applicable.
B. For events that occurred when the reactor was shut down, availability of systems or components needed to shutdown the reactor and maintain safe shutdown conditions, remove residuai heat, control the release of radioactive material, or mitigate the consequences of an accident Not applicable.
C. For failure that rendered a train of a safety system inoperable, an estimate of the elapsed time from the discovery of the failure until the train was returned to service Not applicable.
Vl. Corrective Actions This event was entered into the T_elnessee Valley Authority (TVA) Corrective Action Program and is being tracked under Condition Report (CR) 1425291.
A. lmmediate Corrective Actions Operations personnel promptly stabilized the plant in Mode 3. A short term corrective action was taken to relocate the 287T differential trip signal to a different CT loop such that the one out of two taken twice logic and circuit protection is maintained. Future A phase current drop events on the 251 CT loop will be able to be monitored without causing a direct unit trip.
B. Corrective Actions to Prevent Recurrence or to reduce probability of similar events occurring in the future The intermittent equipment failure between the neutral side current transformer (251 CT loop) of the main generator and the digital protection relays (2-RLY-244-S300G3/1 and 2-RLy-244-M3425N2 relays) will be fully investigated and corrected during the Unit 2 Spring 2019 refueling outage.
Vll. Previous Similar Events at the Same Site LER 391/2016-008 describes a unit trip that occurred on August 20,2016 as a result of an internal fault on the 2B Main Bank Transformer. This event was most likely caused by an inadequate internal bus clearance as a result of either a latent design issue or initial installation error. While the event is associated with the main transformers, the equipment causes are different than this event.
Vlll. Additionallnformation None.
lX. Commitments None.Page 4 of 4
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05000391/LER-2018-002, Loss of Shield Building Vacuum Due to Equipment Failure | Loss of Shield Building Vacuum Due to Equipment Failure | | 05000390/LER-2018-002-01, Shield Building Inoperability Due to Annulus Vacuum Transient | Shield Building Inoperability Due to Annulus Vacuum Transient | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000390/LER-2018-002, Regarding Shield Building Inoperability Due to Annulus Vacuum Transient | Regarding Shield Building Inoperability Due to Annulus Vacuum Transient | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor | 05000391/LER-2018-003, Reactor Trip Due to Main Generator Differential Relay Actuation | Reactor Trip Due to Main Generator Differential Relay Actuation | | 05000390/LER-2018-004, Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open | Control Room Emergency Ventilation System Inoperable Due to Main Control Room Door Being Left Open | 10 CFR 50.73(a)(2) | 05000391/LER-2018-004, Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications | Failure to Implement Annunciator Response Process Results in a Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) | 05000390/LER-2018-005, Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power | Regarding Manual Reactor Trip Due to Failure of Reactor Coolant Pump to Transfer to Normal Power | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2) | 05000391/LER-2018-005, For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure | For Watts Bar Nuclear Plant, Unit 2, Automatic Reactor Trip Due to Turbine Control System Card Failure and Throttle Valve Closure | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(viii)(A) | 05000390/LER-2018-006, Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test | Containment Air Return Fan Inoperable for a Time Period Longer than Allowed by Technical Specifications Due to an Inadequate Post Maintenance Test | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) |
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