05000389/LER-2006-004

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LER-2006-004,
Docket Number
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation
3892006004R00 - NRC Website

FACILITY NAME (1) —DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)

Description of the Event

While returning to power following the SL2-16 outage, the turbine number 1 throttle valve (FCV-08-643) actuator experienced a severe DEH leak and a manual trip of the reactor/turbine was initiated. Operation procedures 2-E0P-01'"Standard Post Trip Actions," and 2-EOP-2, "Reactor Trip Recovery," were completed without contingencies and Unit 2 was stabilized in Mode 3. The DEH leak ceased when the turbine tripped.

All control rods fully inserted and no main steam safety valves (MSSV) lifted.

Feedwater to the steam generator was supplied by the main feedwater pumps and all safe shutdown equipment operated as designed.

Cause of the Event

The cause of the event was a blank flange being improperly attached to an auxiliary servo actuator body by Allen-head cap screws. Proper tightening of the flange to the servo actuator results in a deformation of the o-ring creating a tight seal against the nominal 2000-psi DEH pressure boundary. However, the blank flange was not fully torqued during assembly at the vendor's facility during an overhaul of the servo actuator. Upon disassembly of the blank flange the o-ring was found cut in one location and split in several others. Investigation of retaining head cap screws revealed the required torque value of 90 ft-lbs was not met, resulting in the sealing o-ring failure when subjected to the high DEH pressure. The mating surface of the bolted joint surfaces of the servo actuator and blank flange were found to be contaminated with rust as a result of improper mating of the bolted joint. The Root Cause determined the failed o-ring was a result of poor contractor workmanship and inadequate procedure guidance for torque verification following o-ring installation.

Analysis of the Event

This event is reportable under 10 CFR 50.73(a)(2)(iv)(A) as any event or condition that resulted in manual or automatic reactor trip. An extent-of-condition was performed which identified seven additional actuators had been recently rebuilt at the vendor's shop and installed in Unit 2 during SL2-16. This review determined the integrity of the bolted connections on these actuators could be verified by checking the gap between the actuator blocks and cover plates and by checking the applied torque of cover plate fasteners.

These tasks were performed with satisfactory results and Unit 2 was returned to power.

Although performed by highly experienced specialized workers, the cause of the failed o­ ring was over reliance on post assembly leak testing and inadequate procedure guidance lacking critical step verification.

Analysis of Safety Significance Given the turbine throttle valves are classified as Non-Nuclear Safety Related and based on the satisfactory inspection of all other valves in the extent of condition population and all plant systems actuated to perform their design safety function with no radiological events occurring, this event had no impact on the health and safety of the public.

FACILITY NAME (1) (SOCKETNUMBER (2) LER NUMBER (6) PAGE (3) St. Lucie Unit 2 05000389

Corrective Actions

The proposed corrective actions and supporting actions listed below are entered into the site corrective action program. Any, changes to the proposed actions will be managed under the commitment management change program.

1.Reassembly of the blank flange on the turbine number 1 throttle valve was performed following cleanup of the pressure boundary and installation of a new o-ring.(Completed) Visual inspections and torque checks of the additional bolted blank flanges assembled at the contractor's facility were performed to ensure the integrity of the pressure boundary. (Completed) 2.Assess the level of oversight needed for vendor shop work including attributes such as subject matter expert oversight/review of shop procedures, Quality Assurance procedure use and adherence, and follow guidance.(Due 11/1/06) Similar Events Review of industry operating experience for applicable industry events resulted in two relevant events involving improperly torqued fasteners:

1.A Salem Unit 2 event involved a power reduction and manual turbine trip due to a leak on a governor valve connection to its dump valve as a result of improper torquing of attachment bolts, which subsequently led to o-ring failure.

2.A power reduction and manual turbine trip also occurred at Catawba Unit 2 due to a significant EH fluid leak on a GE turbine combined intercept valve fast acting solenoid valve (FASV), as a result of under torqued fasteners and o-ring failure.

Several other similar events were also identified but were not relevant to St. Lucie:

1.A mis-machined actuator block at HE Robinson resulted in an EH leak. The leak was due to an o-ring installed in an area where an o-ring groove was not machined. The o-ring extruded because it was over-squeezed as a result of the lack of an o-ring groove.

2.North Anna had two failures involving a broken dump block check valve and a governor valve failure, and VC Summer had an EH leak due to a cut filter cover gasket. However, these events were not relevant to the PSL event.

Work orders and St. Lucie's corrective action program were also reviewed for issues involving DEH leaks at St. Lucie, from 2000 to present, and determined not to be relevant to this event.

Failed Components

Siemens TV Servo Actuator Throttle Valve #1FCV-08-643