Similar Documents at Hatch |
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Georgia %er company Corrsctsd Copy
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Telephone 404 S26 6526 unit numbar.
Mailsng Ariaress:
Post Office Box 4545 Atlanta, Georgia 30302 Georgia Power L T. Gucws tv. caeo reyfnc sp3teir '
Manager Nuclear Safety and Licensing 0166C November 4, 1986 U. S. Nuclear Regulatory Comission Document Control Desk Washington, D. C.
20555 Attached is Licensee Event Report 50-366/1985-038, Rev.
2.
This report meets the reporting requirements of 10 CFR 50.73(a)(2)(iv).
Sincerely, ntr -F - -
e L. T. Gucwa LGB/lc Enclosure c: Georgia Power Company Nuclear Regulatory Commission f1r. t. P. O'Reilly Dr. J. N. Grace, Regional Administrator Mr. J. T. Beckham, Jr.
Mr. P. Holmes-Ray, Senior Resident Mr. H. C. Nix, Jr.
Inspector - Hatch GO-NORMS
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ASST 1 ACT <tuswt le #400 assces, t e., seerewnevery Missa ya,ee spece typewerrren anset (161 At approximately 0200 CST on 12/22/85, with Unit 2 operating at 2428 MWt (approximately 100% rated power), plant personnel determined that power had been lost on the "A" R2 actor Protection System (RPS) bus.
This loss of power resulted in a half reactor scram; a half group isolation signal on primary containment isolation valves in valve groups 1, 2, and 5; a trip of the main steam line radiation monitors 2Dll-K603A and 2Dll-K603C; and the automatic start of the
'A' standby gas treatment train.
An immediate investigation determined that subsequent to the performance of the weekly "APRM INSTRUMENT F. T.
C." procedure (34SV-C51-002-2), operations personnel were replacing the cover on reactor scram relay 2C71-K14C when the relay's coil power supply fuse blew and de-energized the relay. This tripped the output circuit breakers on RPS motor / generator set 2C71-S001A, resulting in the loss of power on the "A"
RPS bus, and a reactor-half-scram.
Subsequent to replacing the relay fuse, the half scram was reset, and the plant rsturned to normal operation at approximately 1000 CST on 12/22/85.
Plant engineered safety f eatures responded to the loss of power on the "A" RPS bus as expected. Thercfare, the health and safety of the public were not adversely affected.
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This 30 day LER is required by 10CFR 50.73 (a) (2) (iv) because of the unplanned actuation of Engineered Safety Features (ESPs).
At approximately 0200 CST on 12/22/85, with the plant operating at 2428 MWt (approximately 100% rated power), plant personnel determined that power had been lost on the
'A' Train of the Reactor Protection System (RPS).
An immediate investigation showed that the following sequence of events took place:
1.
The required weekly performance of the "ARPM INSTRUMENT F. T. &
C." procedure (34SV-C51-002-2) had just been completed.
2.
Following completion of that procedure, operations personnel were replacing the cover (it had been removed for visual observation of the relay) on reactor scram relay 2C71-K14C when the coil power supply fuse on that device (2C71-F14C) blew.
3.
The blowing of the fuse de-energized the scram relay and tripped the "A"
RPS bus motor / generator set (2C71-S001A) output breakers, resulting in loss cf power on RFS bus "A".
4.
The loss of power on the "A" RPS bus resulted in the following:
a.
A reactor half-scram signal occurred.
b.
A half-group isolation signal was received for certain primary containment isolation valves in valve groups 1, 2, and 5.
The following valves isolated as required:
- 1) Reactor water sample line inboard isolation valve 2B31-F019 (group 1).
- 2) Drywell equipment drain sump discharge inboard isolation valve 2Gll-F019 (group 2).
- 3) Drywell floor drain sump discharge inboard isolation valve 2Gll-F003 (group 2).
- 4) Reactor water cleanup system inboard suction isolation valve 2G31-F001 (group 5).
c.
Main steam line radiation monitors 2Dll-K603A and 2Dll-K603C went to their fail safe condition (tripped) on loss of supply voltage.
d.
The
'A' Standby Gas Treatment automatically started.
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Oparations personnel immediately began an investigation to identify the cause of the blown fuse; however, the cause was not positively identified.
It is postulated that during the replacement of the cover on 2C71-K14C, the relay was bumped, thus causing ons or more energized relay contacts to briefly contact a neutral point within the rolcy. This contact caused a momentary surge of current of sufficient strength to blow ths fuse, and at the same time cause the RPS motor / generator output circuit breakers to trip.
It should be noted that the removal / replacement of the relay covers is an extremely tedious action, and it must be performed weekly for the surveillance earlier spscified.
Subsequent to the investigation, the following actions were taken to restore tne Unit to normal operating status:
1.
Reactor scram relay fuse 2C71-F14C was replaced.
2.
The RPS motor generator set (2C71-S001A) output circuit breakers were reset.
3.
The half-group isolation signal was reset, and each of the valves which had isolated was returned to its normally open position.
4.
The supply power for Main Steam Line radiation monitors 2Dll-K603A and 2Dll-K603C was restored.
5.
The "A" Standby Gas Treatment train was shut down, and its controls were returned to the standby mode.
6.
The reactor half-scram was reset.
Subsequent to the above actions, the plant resumed normal operation at approximately 1000 CST on 12/22/85.
After er t'.gineering evaluation of the event, the "APRM INSTRUMENT F. T.
C."
procedure (34SV-051-002-2) was revised on 07/31/86 to eliminate the requirement to remo\\t the covers from reactor scram relays (2C71-K14A through H) when the weekly funct. onal test and calibration is performed. The weekly status of the reactor scram relay.c is verified by the reactor auto scram trip system alarm annunciator on control room ptnel 2Hil-P603.
The " Reactor Protection System /APRM LSFT" procedure (34SV-C71-006-2), whose effective date is 10/6/86, now accomplishes the 18 month logic system functional test requirement for the reactor scram relays.
The reactor scram relay covers will be removed during parformance of procedure 34SV-C71-006-2 to verify reactor scram relay function once svary 18 months, instead of weekly as previously required by procedure 34SV-C51-002-2.
Procedure 345V-C71-006-2 satisfies the requirement of Technical Specifications section 4.3.1.2, item 2.
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00RC PeNo MSA U.8 BOUCLEM MGOULAfoAY Coassimacos LICENSEE EVENT REPORT (LER) TEXT CONTINUATION Areaoveo owe o. sino-oio.
EMPiR!S e/3,46 PACIL87V feanse (1p DoCatY seuessem (23 Len asynssen tel Past is
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.ssumwmacs -mewnn There have been no past e.milar events where a RFS bus lost its power because of a blown reactor scram relay fuse.
Plant engineered safety features responded as expected to the loss of power on the "A"
RPS bus.
Therefore, the health and safety of the public were not adversely affected by this event.
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| 05000366/LER-1985-001-01, :on 850119,reactor Scrammed.Caused by Failure of Inboard Msiv.Procedure HNP-2-3111 Revised to Allow 2-minute Wait Between Operating MSIV Cycle to Prevent Isolation of Drywell Pneumatic Sys |
- on 850119,reactor Scrammed.Caused by Failure of Inboard Msiv.Procedure HNP-2-3111 Revised to Allow 2-minute Wait Between Operating MSIV Cycle to Prevent Isolation of Drywell Pneumatic Sys
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-001, :on 850105,reactor Water Cleanup Sys Automatically Isolated Due to High Differential Flow Trip Signal.Caused by Air Trapped in Sensing Lines of Sys Inlet Flow Transmitter G31-N036 |
- on 850105,reactor Water Cleanup Sys Automatically Isolated Due to High Differential Flow Trip Signal.Caused by Air Trapped in Sensing Lines of Sys Inlet Flow Transmitter G31-N036
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-002-01, :on 850429,spurious Reactor Protection Sys (RPS) Logic Actuation Occurred Twice.Caused by Spurious Electrical Noise in intermediate-range Monitor Channel.Rps Trips Reset |
- on 850429,spurious Reactor Protection Sys (RPS) Logic Actuation Occurred Twice.Caused by Spurious Electrical Noise in intermediate-range Monitor Channel.Rps Trips Reset
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-002, :on 850113,safety Relief Valve B Failed to Open.Caused by Open Links.Links Closed |
- on 850113,safety Relief Valve B Failed to Open.Caused by Open Links.Links Closed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-003-01, :on 850106,reactor Protection Sys Logic Actuation Occurred During Completion of Maint Activities on Reactor Low Water Level Instrument 1B21-N080A,due to Backfilling 1B21-N080A Before Return to Svc |
- on 850106,reactor Protection Sys Logic Actuation Occurred During Completion of Maint Activities on Reactor Low Water Level Instrument 1B21-N080A,due to Backfilling 1B21-N080A Before Return to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-003, :on 850107,Group 5 Isolation Occurred from Reactor Water Cleanup High Differential Temp.Cause Attributed to Short Circuit During Corrective Maint on Resistance Temp Detector |
- on 850107,Group 5 Isolation Occurred from Reactor Water Cleanup High Differential Temp.Cause Attributed to Short Circuit During Corrective Maint on Resistance Temp Detector
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-004, :on 850121 & 23,ESF Actuation Occurred.Caused by Reactor Protection Sys B Motor Generator Set Tripping Due to Failed Voltage Regulator.Regulator Replaced & Adjusted. Motor Generator Tested & Returned to Svc |
- on 850121 & 23,ESF Actuation Occurred.Caused by Reactor Protection Sys B Motor Generator Set Tripping Due to Failed Voltage Regulator.Regulator Replaced & Adjusted. Motor Generator Tested & Returned to Svc
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-004-01, :on 850130,reactor Bldg & Refueling Floor Standby Gas Treatment Sys Supply Dampers Control Logic Determined to Fail Closed on Loss of Electrical Power.Design Change Requested |
- on 850130,reactor Bldg & Refueling Floor Standby Gas Treatment Sys Supply Dampers Control Logic Determined to Fail Closed on Loss of Electrical Power.Design Change Requested
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000321/LER-1985-005, :on 850123,plant Shut Down.Caused by Exhaust Diaphragm of HPCI Rupturing Due to Defective Seal on Exhaust Line.Diaphragm Replaced.Leak Rate Test Performed Satisfactorily |
- on 850123,plant Shut Down.Caused by Exhaust Diaphragm of HPCI Rupturing Due to Defective Seal on Exhaust Line.Diaphragm Replaced.Leak Rate Test Performed Satisfactorily
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-005-01, :on 850329,determined That Battery Surveillance Procedure Contained Acceptance Criteria That Did Not Satisfy Tech Specs.Caused by Procedural Inadequacy.Procedure Being Revised |
- on 850329,determined That Battery Surveillance Procedure Contained Acceptance Criteria That Did Not Satisfy Tech Specs.Caused by Procedural Inadequacy.Procedure Being Revised
| 10 CFR 50.73(a)(2)(1) | | 05000321/LER-1985-006-01, :on 850130 & 0202,reactor Tripped When Main Transformer 3 Phase Main Generator Output Line Fell.Caused by Incorrect Tensile Strength of Insulators Holding Power Line.New Insulators Installed |
- on 850130 & 0202,reactor Tripped When Main Transformer 3 Phase Main Generator Output Line Fell.Caused by Incorrect Tensile Strength of Insulators Holding Power Line.New Insulators Installed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-006, :on 850124,calibr Head Correction Data for RCIC Steam Line Differential Pressure Transmitters 2E51-N057A & 2E51-N057B Determined Incorrect.Caused by Error in Procedure.Rcic Declared Inoperable |
- on 850124,calibr Head Correction Data for RCIC Steam Line Differential Pressure Transmitters 2E51-N057A & 2E51-N057B Determined Incorrect.Caused by Error in Procedure.Rcic Declared Inoperable
| 10 CFR 50.73(a)(2)(i) | | 05000366/LER-1985-007-01, :on 850210,reactor Water Cleanup Inboard Isolation Valve 2G31-F001 Isolated Due to False Trip Signal from Inlet Temp Instrument 2G31-N661A.Caused by Poor Connection Between Trip Card & Edge Connector |
- on 850210,reactor Water Cleanup Inboard Isolation Valve 2G31-F001 Isolated Due to False Trip Signal from Inlet Temp Instrument 2G31-N661A.Caused by Poor Connection Between Trip Card & Edge Connector
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-007, :on 850109,Tech Spec Requirements for New Setpoint for HPCI Low Steam Line Pressure Instrument Not Met.Caused by Loss of Administrative Controls.Instrument Recalibr |
- on 850109,Tech Spec Requirements for New Setpoint for HPCI Low Steam Line Pressure Instrument Not Met.Caused by Loss of Administrative Controls.Instrument Recalibr
| 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-007, :on 850210 & 24,reactor Water Cleanup Inboard Isolation Valve 2G31-F001 Isolated as Result of False Trip Signal.Caused by Bad Connection Where Trip Card 2G31-N661A Plugged Into Connector |
- on 850210 & 24,reactor Water Cleanup Inboard Isolation Valve 2G31-F001 Isolated as Result of False Trip Signal.Caused by Bad Connection Where Trip Card 2G31-N661A Plugged Into Connector
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-008, :on 850109,electrical Overspeed Trip Did Not Actuate within Specified Limits of Tech Specs.Electrical Overspeed Repaired.On 850111,RCIC Isolated.Caused by High Exhaust Diaphragm Pressure.Diaphragm Replaced |
- on 850109,electrical Overspeed Trip Did Not Actuate within Specified Limits of Tech Specs.Electrical Overspeed Repaired.On 850111,RCIC Isolated.Caused by High Exhaust Diaphragm Pressure.Diaphragm Replaced
| 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-008-01, :on 850420,reactor Water Cleanup Outboard Isolation Valve 2G31-F004 Isolated on High Differential Flow.Caused by Flow Fluctuation During Valving in of Filter Demineralizer 2A.Valve Opened |
- on 850420,reactor Water Cleanup Outboard Isolation Valve 2G31-F004 Isolated on High Differential Flow.Caused by Flow Fluctuation During Valving in of Filter Demineralizer 2A.Valve Opened
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-009-01, :on 850319,RCIC Steam Supply Primary Containment Inboard Isolation Valve 2E51-F007 Inadvertently Closed.Caused by Personnel Error.Isolation Logic Reset & Valve Returned to Open Position |
- on 850319,RCIC Steam Supply Primary Containment Inboard Isolation Valve 2E51-F007 Inadvertently Closed.Caused by Personnel Error.Isolation Logic Reset & Valve Returned to Open Position
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(s)(2)(iv) | | 05000321/LER-1985-009, :on 850123,clearance Hold Tags Placed on Wrong Switches,Resulting in Inability of Ball Valves to Close. Caused by Personnel Error.Responsible Personnel Counseled. Tags Placed on Correct Switches |
- on 850123,clearance Hold Tags Placed on Wrong Switches,Resulting in Inability of Ball Valves to Close. Caused by Personnel Error.Responsible Personnel Counseled. Tags Placed on Correct Switches
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-010-01, :on 850409,certain Valves Discovered Leaking in Excess of Limits Specified in Tech Spec Sections 3.6.1.2.b & C.Valves Will Be Repaired & Tested |
- on 850409,certain Valves Discovered Leaking in Excess of Limits Specified in Tech Spec Sections 3.6.1.2.b & C.Valves Will Be Repaired & Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000321/LER-1985-010, :on 850116,reactor Scrammed on Reactor Vessel Low Water Level Signal.Caused by Vital Ac Power Supply Trip. Personnel Restored Reactor Level to Normal |
- on 850116,reactor Scrammed on Reactor Vessel Low Water Level Signal.Caused by Vital Ac Power Supply Trip. Personnel Restored Reactor Level to Normal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-010-01, :on 850116,reactor Scram on Low Level Water Signal Received.Caused by Ac Power Supply Trip & Runback of Feedpumps a & B.Personnel Restored Level to Normal Via Feedpump a & Booster Pumps |
- on 850116,reactor Scram on Low Level Water Signal Received.Caused by Ac Power Supply Trip & Runback of Feedpumps a & B.Personnel Restored Level to Normal Via Feedpump a & Booster Pumps
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-011, :on 850401,main Steam Line Monitor B High Trip Setpoint Set at 3.2 Times Full Power Background.Caused by Personnel Communication Error.Setpoint Data Will Be Retrieved in Person Rather than Via Telephone |
- on 850401,main Steam Line Monitor B High Trip Setpoint Set at 3.2 Times Full Power Background.Caused by Personnel Communication Error.Setpoint Data Will Be Retrieved in Person Rather than Via Telephone
| 10 CFR 50.73(a)(2)(vi) | | 05000321/LER-1985-011-01, :on 850424,Train a of Standby Gas Treatment Sys Started.Caused by Inadequate Special Instructions Which Failed to Give Detailed Instructions for Returning Battery Charger to Svc.Train a Returned to Normal |
- on 850424,Train a of Standby Gas Treatment Sys Started.Caused by Inadequate Special Instructions Which Failed to Give Detailed Instructions for Returning Battery Charger to Svc.Train a Returned to Normal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-012-01, :on 850409,unplanned Actuation of Reactor Protection Sys Occurred.Caused by Failure of Main Steam Line Radiation Detectors Due to Loose & Saturated Power Cables. Cables Replaced |
- on 850409,unplanned Actuation of Reactor Protection Sys Occurred.Caused by Failure of Main Steam Line Radiation Detectors Due to Loose & Saturated Power Cables. Cables Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-012, :on 850324,reactor Water Cleanup Primary Containment Isolation Valves Closed Due to Leak Detection Isolation Signal.Manual Isolation Valves Replaced |
- on 850324,reactor Water Cleanup Primary Containment Isolation Valves Closed Due to Leak Detection Isolation Signal.Manual Isolation Valves Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-013-01, :on 850411,while in Refueling Mode,Full Reactor Scram Indicated.Investigation Determined That Full Reactor Protection Sys Logic Actuation Occurred.Caused by hi-hi Signal from Source Range Monitors |
- on 850411,while in Refueling Mode,Full Reactor Scram Indicated.Investigation Determined That Full Reactor Protection Sys Logic Actuation Occurred.Caused by hi-hi Signal from Source Range Monitors
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-013, :on 850216,drywell Floor Drain Total Leakage Exceeded Max Limit.Caused by Shaft Seal 1 on Reactor Recirculation Pump B Leaking Excessively.Shaft Seal Cartridge Replaced |
- on 850216,drywell Floor Drain Total Leakage Exceeded Max Limit.Caused by Shaft Seal 1 on Reactor Recirculation Pump B Leaking Excessively.Shaft Seal Cartridge Replaced
| 10 CFR 50.73(a)(2)(1) | | 05000321/LER-1985-014, :on 850128,instrumentation & Controls Personnel Discovered That RCIC Pump Suction Pressure Instrument Procedure Not Performed Until 850204.Caused by Personnel Error.Personnel Reinstructed |
- on 850128,instrumentation & Controls Personnel Discovered That RCIC Pump Suction Pressure Instrument Procedure Not Performed Until 850204.Caused by Personnel Error.Personnel Reinstructed
| 10 CFR 50.73(a)(2)(i) | | 05000366/LER-1985-014, :on 850510,seven Safety Relief Valves Serving Automatic Depressurization Sys Function Opened,Constituting ESF Actuation.Caused by Procedural Rev Deficiency.Personnel Counseled on Need for Accurate Revs |
- on 850510,seven Safety Relief Valves Serving Automatic Depressurization Sys Function Opened,Constituting ESF Actuation.Caused by Procedural Rev Deficiency.Personnel Counseled on Need for Accurate Revs
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-015-01, :on 850415,reactor Protection Sys Logic Actuation Occurred Due to Spurious Actuation in Other Sys Channel.Caused by Intermediate Range Monitor Spurious Electrical Noise.Preventing Noise Unachievable |
- on 850415,reactor Protection Sys Logic Actuation Occurred Due to Spurious Actuation in Other Sys Channel.Caused by Intermediate Range Monitor Spurious Electrical Noise.Preventing Noise Unachievable
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-016-01, :on 850519,RCIC Pump Failed to Meet Rated Flow Requirement of 400 Gpm at Normal Reactor Vessel Operating Pressure.Caused by Failure of RCIC Sys Automatic Control Amplified Circuit Board.Circuit Board Replaced |
- on 850519,RCIC Pump Failed to Meet Rated Flow Requirement of 400 Gpm at Normal Reactor Vessel Operating Pressure.Caused by Failure of RCIC Sys Automatic Control Amplified Circuit Board.Circuit Board Replaced
| 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-016, :on 850425,during Testing of Main Steam Safety Relief Valves,Four Valves Failed to Lift within Range Required by Tech Spec 3.4.2.1.Caused by Valve Pilot Setpoint Drift.Pilot Assemblies Refurbished & Retested |
- on 850425,during Testing of Main Steam Safety Relief Valves,Four Valves Failed to Lift within Range Required by Tech Spec 3.4.2.1.Caused by Valve Pilot Setpoint Drift.Pilot Assemblies Refurbished & Retested
| 10 CFR 50.73(a)(2)(1) | | 05000321/LER-1985-017, :on 850515,determined Cable Tray Support 33 Located in Cable Spreading Room Could Experience Overloading During OBE or Sse.Caused by A/E Design Error.Cable Support Modified.Part 21 Related |
- on 850515,determined Cable Tray Support 33 Located in Cable Spreading Room Could Experience Overloading During OBE or Sse.Caused by A/E Design Error.Cable Support Modified.Part 21 Related
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000366/LER-1985-017-01, :on 850430 & 0501,molded Case Circuit Breakers Trip Setpoints &/Or Breaker Locations Contrary to Specified Setpoints or Locations of Tech Spec Table 3.8.2.6-1.Caused by Inadequate Instructions.Tech Specs Amended |
- on 850430 & 0501,molded Case Circuit Breakers Trip Setpoints &/Or Breaker Locations Contrary to Specified Setpoints or Locations of Tech Spec Table 3.8.2.6-1.Caused by Inadequate Instructions.Tech Specs Amended
| 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-017, :on 850430 & 0501,molded Case Circuit Breakers Discovered W/Trip Setpoints &/Or Breaker Locations Contrary to Tech Spec Table 3.8.2.6-1.Caused by Inadequate Instructions for Implementing Design Change |
- on 850430 & 0501,molded Case Circuit Breakers Discovered W/Trip Setpoints &/Or Breaker Locations Contrary to Tech Spec Table 3.8.2.6-1.Caused by Inadequate Instructions for Implementing Design Change
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(1) | | 05000321/LER-1985-018, :on 850515,safety Relief Valve a Activated & Remained Open & Reactor Manually Scrammed.Caused by Falling Water from Control HVAC Creating Excessive Moisture in Panel 1H11-P926.HVAC Filter Train Maint Done |
- on 850515,safety Relief Valve a Activated & Remained Open & Reactor Manually Scrammed.Caused by Falling Water from Control HVAC Creating Excessive Moisture in Panel 1H11-P926.HVAC Filter Train Maint Done
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) | | 05000366/LER-1985-018-01, :on 850603,during Load Reduction to Take Div of Plant Svc Water Out of Svc,Turbine Trip & Subsequent Reactor Scram Received on High Moisture Separator Reheater Level Signal.Caused by High Level Trip Signal |
- on 850603,during Load Reduction to Take Div of Plant Svc Water Out of Svc,Turbine Trip & Subsequent Reactor Scram Received on High Moisture Separator Reheater Level Signal.Caused by High Level Trip Signal
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-019, :on 850403 & 05,reactor Water Cleanup (RWCU) Sys Pump Suction Primary Containment Valves 1G31-F001 & 1G31-F004 Isolated Three Times.Caused by High Ambient Temp in RWCU Pump Rooms 1A & 1B |
- on 850403 & 05,reactor Water Cleanup (RWCU) Sys Pump Suction Primary Containment Valves 1G31-F001 & 1G31-F004 Isolated Three Times.Caused by High Ambient Temp in RWCU Pump Rooms 1A & 1B
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-019-01, :on 850429,during Cold Shutdown,Reactor Water Cleanup Primary Containment Inboard Isolation Valve 2G31-F001 Isolated.Caused by Personnel Error.Resistance Temp Detectors Relabeled |
- on 850429,during Cold Shutdown,Reactor Water Cleanup Primary Containment Inboard Isolation Valve 2G31-F001 Isolated.Caused by Personnel Error.Resistance Temp Detectors Relabeled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-020, :on 850726,RWCU Pump Inboard & Outboard Suction Isolation Valves Isolated on High Sys Differential Flow. Caused by Leakage Past RWCU Loop a Resin Strainer Drain Valves.Investigation Continuing |
- on 850726,RWCU Pump Inboard & Outboard Suction Isolation Valves Isolated on High Sys Differential Flow. Caused by Leakage Past RWCU Loop a Resin Strainer Drain Valves.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-020-01, :on 850726,reactor Water Cleanup Pump Inboard & Outboard Suction Isolation Valves 2G31-F001 & 2G31-F004, Isolated on High Sys Differential Flow.Caused by Filter Demineralizer Not Being Completely Filled |
- on 850726,reactor Water Cleanup Pump Inboard & Outboard Suction Isolation Valves 2G31-F001 & 2G31-F004, Isolated on High Sys Differential Flow.Caused by Filter Demineralizer Not Being Completely Filled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-020, :on 850415,special Purpose Procedure Directing Implementation of Direct Conversion Reactor on Plant Standby Gas Treatment Sys in Violation of Tech Specs.Caused by Inadequate Technical Review of Procedures |
- on 850415,special Purpose Procedure Directing Implementation of Direct Conversion Reactor on Plant Standby Gas Treatment Sys in Violation of Tech Specs.Caused by Inadequate Technical Review of Procedures
| 10 CFR 50.73(a)(2)(vi) | | 05000366/LER-1985-021-01, :on 850707,during Reactor Water Cleanup Sys Procedure,Inboard & Outboard Suction Isolation Valves Isolated.Caused by Misaligned Position Indicators.Repairs in Progress |
- on 850707,during Reactor Water Cleanup Sys Procedure,Inboard & Outboard Suction Isolation Valves Isolated.Caused by Misaligned Position Indicators.Repairs in Progress
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-021, :on 850707,reactor Water Cleanup Pump Inboard & Outboard Suction Isolation Valves Isolated on High Sys Differential Flow.Caused by Incompletely Closed Valves Due to Misaligned Indicators.Valves Closed |
- on 850707,reactor Water Cleanup Pump Inboard & Outboard Suction Isolation Valves Isolated on High Sys Differential Flow.Caused by Incompletely Closed Valves Due to Misaligned Indicators.Valves Closed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-021, :on 850612,plant Personnel Determined That Fire Protection Valve Cycling Procedures Could Make Valves Inaccessible During Operations to Be Cycled Once Every 18 Months Rather than Every 12 Months |
- on 850612,plant Personnel Determined That Fire Protection Valve Cycling Procedures Could Make Valves Inaccessible During Operations to Be Cycled Once Every 18 Months Rather than Every 12 Months
| 10 CFR 50.73(a)(2)(vi) | | 05000321/LER-1985-022, :on 850527,operations Personnel Determined That Reactor Water Cleanup Pump Suction Inboard Primary Containment Isolation Valve Isolated on High Ambient Temp in Reactor Water Cleanup Pump Room 1A |
- on 850527,operations Personnel Determined That Reactor Water Cleanup Pump Suction Inboard Primary Containment Isolation Valve Isolated on High Ambient Temp in Reactor Water Cleanup Pump Room 1A
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000366/LER-1985-022-01, :on 850814,personnel Determined That Monthly Channel Check for Drywell High Range Pressure & Radiation Instrumentation Not Performed Per Tech Specs. Caused by Personnel Error |
- on 850814,personnel Determined That Monthly Channel Check for Drywell High Range Pressure & Radiation Instrumentation Not Performed Per Tech Specs. Caused by Personnel Error
| 10 CFR 50.73(a)(2)(1) | | 05000366/LER-1985-023, :on 850515,performance of Channel Logic Response Time Procedure Actuated LPCI Sys Signal.Caused by Error in Procedure Instructions.Personnel Reviewed & Corrected Procedure |
- on 850515,performance of Channel Logic Response Time Procedure Actuated LPCI Sys Signal.Caused by Error in Procedure Instructions.Personnel Reviewed & Corrected Procedure
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000321/LER-1985-023-01, :on 850616,reactor Water Conductivity Monitoring Inoperable Due to Conductivity Cell.Caused by Broken Gauge Which Had Been Removed on 850614.Reactor Water Conductivity Cell Reestablished |
- on 850616,reactor Water Conductivity Monitoring Inoperable Due to Conductivity Cell.Caused by Broken Gauge Which Had Been Removed on 850614.Reactor Water Conductivity Cell Reestablished
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(1) |
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