05000316/FIN-2018003-01
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Finding | |
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Title | Misaligned Heater Level Column Valves Leads to Manual Reactor Trip |
Description | A self-revealed, Green finding was identified when the operators manually tripped the Unit 2 reactor in response to a hi-hi level in the Left Moisture Separator Drain Tank. On May 6, 2018, the Unit 2 reactor was at approximately 12 percent power following a startup at the conclusion of the spring 2018 refueling outage. While the station continued to make preparations to start the main turbine and synchronize with the grid, the moisture separator drain tank hi level alarm was received and remained standing for the better part of the shift. The drain tank collects condensed steam and water from the moisture separator reheater and associated high pressure turbine exhaust lines and routes it either to the condenser or #4 feedwater heaters. The day shift operators were hesitant to continue on with starting the main turbine until the cause of the alarm could be determined. Due to a series of miscommunications between day shift, night shift, the outage control center, and personnel performing troubleshooting, the night shift crew believed it was acceptable to continue with the turbine startup with the alarm still standing. The turbine was synchronized to the grid and power was stabilized at approximately 29 percent power with the alarm in for most of the turbine startup and synchronization. The alarm cleared for a period of time at 29 percent power, but then returned along with the hi-hi drain tank level alarm. Per the alarm response procedures, the operators tripped the reactor and main turbine to protect the turbine from excessive water in the system. Later investigation by the site revealed that the level columns for the #4 feedwater heaters had been left isolated following work and testing associated with the replacement of the #5 feedwater heaters. While the Operations Department had completed a valve lineup on the system per their startup procedures, which put the level columns in service, the Projects Department had not finished all of the work on the heaters at the time the lineup was performed. As a result, workers subsequently isolated the columns to complete testing after the Operations lineup was complete. A step in the Projects test procedure EC51366TP001 directed workers to specifically inform the operators that the level columns were isolated following testing and that the system was ready to be lined up per operations procedures. However, the workers did not provide that detail, and simply stated that the test was complete. As a result, operations did not know the valves had been taken out of alignment. Contributing to the issue, the outage schedule did not provide any logic ties to ensure all work was complete on the heaters before allowing operations to do their valve lineups. With the level columns isolated during startup, the #4 heaters indicated an erroneous level. This resulted in the operators believing that the heaters were at a normal operating level when in fact, they were full. Therefore, when the operators (per procedure) opened a high pressure turbine exhaust valve to the 4A heater, this created a pathway for water to flow from the #4 heaters, through the high pressure turbine exhaust lines, and into the moisture separator drain tank. The excessive flow of water caused the hi and hi-hi alarms in the drain tank which then led to the reactor/turbine trip. |
Site: | Cook |
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Report | IR 05000316/2018003 Section 4OA2 |
Date counted | Sep 30, 2018 (2018Q3) |
Type: | Finding: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | J Ellegood T Taylor B Bergeon J Cassidy N Fields T Go M Learn N Shah K Riemer |
CCA | H.5, Work Management |
INPO aspect | WP.1 |
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Finding - Cook - IR 05000316/2018003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Cook) @ 2018Q3
Self-Identified List (Cook)
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