:on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4| ML17326A091 |
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Cook  |
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| Issue date: |
08/16/1999 |
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Orourke B AMERICAN ELECTRIC POWER CO., INC. |
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| Shared Package |
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| ML17326A090 |
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| References |
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| LER-99-019, NUDOCS 9908240285 |
| Download: ML17326A091 (5) |
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Similar Documents at Cook |
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text
NRC Form 366 U.S. NUCLEAR REGULATORYCOMMISSION (6-1996)
LICENSEE EVENT REPORT (LER)
(See reverse for required number of digits/characters for each block)
APPROVEO BY0MB NO. 3(504)104 EXPIRES 05/30/2001 ESTPAATED SVRDEN PER
RESPONSE
TO COMPLY WITH TI43 MANDATORY eIFORMATION COLLECTION REOVEST: 50 0 HRS. REPORTED LESSONS LEARNED ARE erCORPORATED trfo THE LICENSINO PROCESS ANO FED SACK TO INDVSTRY FORWARD COIVFAENTS REOARDINO SVRDEN ESTSJATE TO THE eIFORMATKNI ANO RECORDS MANAGEMENT SRANCH IT%
Faax V.S NVCLEAR REOIAATORY COLSJISSIOH. WASHNOTON. OC 20555000I, ANO TO THE PAPERWORK REDVCTION PROJECT (3I500IDII OFFCE OF ScrNAOEMENT AND SVOOET WASHrNOTONi DC 20500 FACILITYNAME(1)
Cook Nuclear Plant Unit 1 DOCKETNUMBER(2) 05000-315 PAOE (3) 1 of4 TITLE(4)
Victoreen Containment High Range Radiation Monitors Not Environmentally Qualified to Withstand Post-LOCA Conditions EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIESINVOLVED(8)
MONTH DAY 07 16 YEAR 1999 YEAR SEQUENTIAL NUMBER 1999
019 REVISION NUMBER 00 MONTH 08 DAY 16 YEAR 1999 FACILITYNAME D.C. Cook - Unit 2 FACILITYNAME DOCKET NUMBER 05000-316 DOCKET NUMBER OPERATING MODE (9)
THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR Ii: (Check one or mor 20.2201 (b) 20.2203(a)(2)(v) 50.73(a)(2)(i) e) (11) 50.73(a)(2)(viii)
POWER LEVEL (10) 0 20.2203(a)(1) 20.2203(a)(2)(i) 20.2203(a)(2)(ii) 20.2203(a)(2)(iii) 20.2203(a)(2)(iv) 20.2203(a)(3)(i) 20.2203(a)(3)(ii) 20.2203(a)(4) 50.36(c)(1) 50.36(c)(2)
LICENSEE CONTACT FOR THIS LER (12) 50.73(a)(2)(ii) 50.73(a)(2)(iii) 50.73(a)(2)(iv) 50.73(a)(2)(v) 50.73(a)(2)(vii) 50,73(a)(2)(x) 73.71 OTHER Speo/Y in Abstract betorv or nNRCForm3SSA NAME Ms. Brenda W. O'ourke, Compliance Engineer TELEPHONE NUMBER 0ndrrde Area Code)
(616) 465-5901 x2604 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 13
CAUSE
SYSTEM COMPON NT MAIJUFACTUR R REPORTABLE TO EPIX
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO EPIX SUPPLEMENTAL REPORT EXPECTED 14 YES IIYes com lete EXPECTED SUBMISSION DATE X
EXPECTED SUBMISSION DATE 15 MONTH DAY YEAR Abstract (Limitto 1400 spaces, I.e. ~ approximately 15 single-spaced typewritten lines) (16)
On May 21, 1999, during an Environmental Qualification (EQ) program self-assessment, preliminary review identified that the containment high range radiation monitors (HRRM) may not be environmentally qualified to withstand the effects of a Loss of Coolant Accident (LOCA). The self-assessment found that D.C. Cook's evaluation of NRC Information Notice (IN) 97-45, "Environmental Qualification Deficiency for Cables and Containment Penetration Pigtails," failed to adequately address the susceptibility of the containment HRRMs to moisture intrusion. IN'97-45 identified that electrical signal cables and connectors found in HRRMs are sensitive to moisture exposure effects, such as from a LOCA or pipe break event.
Industry events have identified that moisture intrusion into the cable jacket and connectors has resulted in erratic indication of radiation levels and loss of HRRM function. Based on continued evaluation of the EQ deficiencies, the Unit 1 and 2 HRRMs were declared inoperable on July 16, 1999.
The apparent cause was inadequate design control.
In response to NRC IN 89-63, a design change to the HRRM system added drainage features to several components.
However, the EQ requirement that the HRRM system be leaktight against possible moisture intrusion was not considered.
A permanent solution for the susceptibility of the HRRMs to moisture intrusion will be developed to support HRRM operability in Modes 1-4. Options for the permanent solution are currently under review and the method selected willbe implemented prior to Mode 4 for each unit. An evaluation of the as-built configuration for other low signal current application EQ equipment is also being performed to identify other electrical equipment that may be susceptible to moisture intrusion due to a LOCA and/or pipe break condition. This evaluation will be completed by September 30, 1999.
This condition has minimal safety significance due to the availability of alternate post-accident radiation monitoring instrumentation.
'3)'T)08240285 3)'T)08' PDR ADOCK 050003i 5 S
PDRU.s. NUCLEAR REGULATORYCOMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME (1)
Cook Nuclear Plant Unit 1 DOCKET NUMBER(2) 05000-315 YEAR LER NUMBER (6)
SEQUENTIAL NUMBER REVISION NUMBER PAGE (3) 2of4 TEXT (lfmore space is required, use adCh'tional copies ofNRC Form (366A) (17)
Conditions Prior to Event
Unit 1 was in Mode 5, Cold Shutdown Unit 2 was in Mode 5, Cold Shutdown 1999
019 00 Descri tion of Event On May 21, 1999, during an Environmental Qualification (EQ) program self-assessment, preliminary review identified that the Radiation Monitoring System's (RMS) [EIIS:IL]Victoreen containment high range radiation monitors (HRRM) may not be environmentally qualified to withstand the effects of a Loss of Coolant Accident (LOCA). The self-assessment found that D.C. Cook's evaluation of NRC Information Notice (IN) 97-45, "Environmental Qualification Deficiency for Cables and Containment Penetration Pigtails," failed to adequately address the susceptibility of the containment HRRMs to moisture intrusion.
IN 97-45 identified that electrical signal cables [EIIS:CBL1] and connectors [EIIS:CON] found in HRRMs are sensitive to moisture exposure effects, such as from a LOCA or pipe break event.
Industry events have identified that moisture intrusion into the cable jacket and connectors can result in erratic indication of radiation levels in containment.
In addition, Supplement 1 to IN 97-45 identified that HRRMs have experienced significant positive and negative current flow as a result of induced currents in Rockbestos coaxial signal cables when exposed to high temperature transient conditions.
As a result, the detection function of the HRRMs would be impacted.
Recent evaluation of the HRRM EQ deficiencies identified that in response to NRC IN 89-63, "Possible Submergence of Electrical Circuits Located Above the Flood Level Because ofWater Intrusion and Lack of Drainage," D.C. Cook added drainage features (e.g., weep holes and slits in sealtite flex conduit) to the HRRM electrical enclosures (conduit and junction boxes [EIIS:JBX])in containment.
However, this resulted in a non-leaktight HRRM configuration, potentially exposing the moisture sensitive components to LOCA conditions.
Based on above information, it was concluded that the Unit 1 and 2 HRRMs would not be capable of performing their intended design function. As a result, on July16, 1999, the HRRMs were declared inoperable at 1558 hours0.018 days <br />0.433 hours <br />0.00258 weeks <br />5.92819e-4 months <br />.
Cause of Event
The apparent cause was inadequate design control.
In response to NRC IN 89-63, a design change to the HRRM system added drainage features to several components.
However, the EQ requirement that the HRRM system be leaktight against possible moisture intrusion was not considered.
Subsequent opportunities to identify this condition were missed during D.C. Cook's evaluation of IN 97-45 and its supplement.
The concerns identified in the Information Notice were determined not to be applicable to D.C. Cook because the HRRMs use Brand Rex signal cabling versus Rockbestos cabling as described in IN 97-45.
Anal sis of Event This LER is being submitted in accordance with the requirements of 10CFR50.73(a)(2)(i)(B) for a condition prohibited by plant Technical Specifications.
TS 3.3.3.1 requires the containment HRRMs to be operable in Modes 1-4.
UFSAR Section 11.3, states that the Radiation Monitoring System is designed to perform two basic functions: 1) warn of any radiation hazards which might develop, and 2) give early warning which might lead to a radiation hazard or plant damage.
The RMS instruments are located at selected points in and around the plant to detect, compute, and record radiation levels. The components of the RMS are designed to operate during all expected environmental conditions for normal operation, and specific components are designed to operate during adverse or accident conditions. The subject radiation monitors include the Victoreen containment high range radiation monitors (1-VRA-1310/1410 and 2-VRA-2310/2410) which provide indication of containment radiation levels during post-LOCA conditions and are utilized in assessing possible core damage.U.s. NUCLEAR REGULATORYCOMMISSION (6-1998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME (1)
Cook Nuclear Plant Unit 1 OOCKET NUMBER(2) 05000-315 YEAR 1999 LER NUMBER (6)
SEQUENTIAL NUMBER 019 REVISION NUMBER 00 PAGE (3) 3of4 TEXT (ifmore space is required, use addi(tonal copies ofNRC Form (366A) (17)
A typical HRRM consists of a detector, associated Brand Rex triaxial cabling, conduit, junction boxes and Amphenol connectors.
Amphenol connectors are located at the penetration pigtails and other electrical cable connections, and at a junction box located at the top of the containment penetration flood-up tubes.
Each Amphenol connector is enclosed in a Raychem boot seal, with the associated detector cabling contained within a conduit system.
The junction box and conduit system contain weep holes which were added in response to NRC IN 89-63.
EQ testing performed by Victoreen in 1978 experienced numerous failures in attempting to qualify a connector assembly for in-containment LOCA use.
The only documented successful simulated LOCA testing was for cable and connectors that were enclosed in leaktight conduits.
This configuration prevents moisture intrusion into the cable and connectors during post-LOCA conditions.
NRC IN 97-45, identified potential EQ deficiencies associated with Rockbestos coaxial cables and Amphenol connectors used in containment HRRM systems.
Subsequent vendor EQ testing concluded that moisture could permeate the HRRM coaxial cable jacket during p LOCA and cause partial shorting of the monitor signal at the connectors.
Because of the small signal current output from the HRRMs (nominally pico-amperes),
partial shorting of the signal could result in loss of HRRM function.
In addition, Supplement 1 identified that HRRMs cabling is susceptible to thermally-induced currents as a result of extreme temperature transients.
Thermally-induced currents have been found to impact the accuracy of the HRRMs.
E In 1990, drainage features were added to D.C. Cook's HRRM system in response to NRC IN 89-63.
Industry concerns were identified regarding the lack of drainage holes in containment electrical enclosures that may become submerged during a LOCA event. Without the appropriate drainage, water could collect inside the enclosures and cause shorting of the electrical components contained in the enclosures.
Although D.C. Cook's HRRM conduit system contains weep holes, the moisture intrusion potential of the subject connectors is much more limited than that described in the Victoreen test reports and NRC IN 97-45.
In these tests, the coaxial cable and sealed connectors were directly exposed to steam and spray conditions, whereas D.C. Cook's cable and sealed connectors are contained within a conduit system.
Because of the additional protection given by the conduit system, the maximum amount of moisture that could potentially come in contact with the connectors is limited by the internal free air space of the conduit. During the increasing containment pressure portion of a LOCA transient, the steam would fillthe conduit, displacing the air inside the conduit and result in the trapped steam condensing on the colder cable and conduit internal walls. This amount of moisture intrusion is much more limited than would occur in an open system (i.e., with no conduit enclosure).
The design function of the containment HRRMs is to provide operators with post-LOCA indication of containment radiation levels which are also utilized in assessing possible core damage.
Although the identified EQ deficiencies could render the HRRMs inoperable following a LOCA, alternative means of performing this monitoring function exist through other post-accident monitoring instrumentation.
This includes the post-accident monitoring system and the post-accident grab sample pallet in accordance with plant emergency procedures.
Based on the above information, the identified condition has minimal safety significance due to the availability of alternate post-accident radiation monitoring instrumentation.
Corrective Actions
A permanent solution for the susceptibility of the HRRMs to moisture intrusion will be developed to support HRRM operability in Modes 1-4. Options for the permanent solution are currently under review and will be implemented prior to Mode 4 for each unit.
An evaluation of the as-built configuration for other low signal current application EQ equipment is being performed to identify other additional electrical equipment that may be susceptible to moisture intrusion due to a LOCA or pipe break condition. The evaluation will include a review of the current EQ Program documentation regarding requirements forU.S. NUCLEAR REGULATORYCOMMISSION (6-1 998)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITYNAME (1)
Cook Nuclear Plant Unit 1 DOCKET NUMBER(2) 05000-315 YEAR 1999 LER NUMBER (6)
SEQUENTIAL NUMBER 019 REVISION NUMBER 00 PAGE (3) 4 of 4 TEXT (lfmore space is required, use additional copies ofNRC Eorm (366A) (17) leaktight electrical enclosures.
This evaluation willbe completed by September 30, 1999.
Based on results of the evaluation, appropriate corrective actions will be taken to address any identified EQ discrepancies.
AEP:NRC:1260GH, "Enforcement Actions98-150, 98-151, 98-1 52 and 98-186 Reply to Notice Of Violation October 13, 1998", dated March 19, 1999, responded to identified programmatic weaknesses in the plant Design and Licensing Basis and the Training and Qualification of personnel.
The Engineering Leadership Plan establishes a configuration management program to control plant design and a new design control process, which includes design verification, design document control, vendor technical documentation control and testing of design changes.
As part of the Restart effort, an improved operating experience program is being developed.
In addition, the Expanded System Readiness Review project teams are evaluating operating experience information to assess whether applicable industry'issues have been adequately addressed for applicability to D.C. Cook.
Previous Similar Events
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| 05000316/LER-1999-001-01, Regarding Supplemental LER for Degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations | Regarding Supplemental LER for Degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000315/LER-1999-001, :on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405 |
- on 990106,noted That GE Hfa Relays Installed in EDGs May Not Meet Seismic Qualification.Caused by Operating Experience Info Incorrectly Dispositioned in 1985. Updated LER Will Be Submitted by 990405
| 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000316/LER-1999-001, :on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing |
- on 960610,degraded Component Cooling Water Flow to Containment Main Steam Line Penetrations,Identified on 990226.Caused by Inadequate Understanding of Design Basis.Additional Investigations Ongoing
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000315/LER-1999-002, :on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted |
- on 990112,determined That RCS Pressurizer PORVs Had Not Been Tested,Per Ts.Caused by Inadequate Scheduling Controls Allowing Personnel Error.Surveillance Procedure Was Completed & Updated LER Will Be Submitted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000316/LER-1999-002-01, :on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised |
- on 990415,discovered That TS 4.0.5 Requirements Were Not Met Due to Improperly Performed Test. Caused by Incorrect Interpretation of ASME Code.App J Testing Will Be Completed & Procedures Will Be Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000316/LER-1999-002, Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed | Forwards LER 99-002-00 Re TS 4.0.5 Requirements Not Being Met Due to Improperly Performed Test.Commitments Identified in Ler,Listed | | | 05000315/LER-1999-003, :on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors |
- on 990107,CR Pressurization Sys Surveillance Test Did Not Test Sys in Normal Operating Condition.Caused by Failure to Recognize Door 12DR-AUX415 as Part of CR Pressure Boundary.Performed Walkdown of Other Doors
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-004-01, Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed | Forwards LER 99-004-01 Re Failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed. Commitments Made by Util Are Listed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000315/LER-1999-004, :on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written |
- on 971030,failure to Perform TS Surveillance Analyses of Reactor Coolant Chemistry with Fuel Removed Was Noted.Caused by Ineffective Mgt of Tss.Chemistry Personnel Have Been Instructed on Requirement to Follow TS as Written
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-005, :on 940512,determined That RT Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed |
- on 940512,determined That RT Breaker Manual Actuations During Rod Drop Testing Were Not Previously Reported.Caused by Lack of Training.Addl Corrective Actions,Including Preventative Actions May Be Developed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000315/LER-1999-006, :on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold |
- on 990115,personnel Identified Discrepancy Between TS 3.9.7 Impact Energy Limit & Procedure 12 Ohp 4030.STP.046.Caused by Lack of Design Basis Control.Placed Procedure 12 Ohp 4030.STP.046 on Administrative Hold
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-007, :on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures |
- on 981020,calculations Showed That Divider Barrier Between Upper & Lower Containment Vols Were Overstressed.Engineers Are Currently Working on Analyses of Loads & Stress on Enclosures
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-008, :on 990115,plant Operators Reported Excessive Piping Vibration in RHR Rooms.Cause Unknown.Update to LER Will Be Submitted |
- on 990115,plant Operators Reported Excessive Piping Vibration in RHR Rooms.Cause Unknown.Update to LER Will Be Submitted
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-009, :on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation |
- on 990304,as-found RHR Safety Relief Valve Lift Setpoint Greater than TS Limit Occurred.Cause Investigation for Condition Has Not Been Completed.Update to LER Will Be Submitted,Upon Completion of Investigation
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000315/LER-1999-010, :on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design |
- on 990401,RCS Leak Detection Sys Sensitivity Not in Accordance with Design Requirements Occurred.Caused by Inadequate Original Design of Containment Sump Level. Evaluation Will Be Performed to Clearly Define Design
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000315/LER-1999-011, :on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared |
- on 990407,air Sys for EDG Will Not Support Long Operability.Caused by Original Design Error.Temporary Mod to Supply Makeup Air Capability in Modes 5 & 6 Was Prepared
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-012, :on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed |
- on 990420,concluded That Auxiliary Bldg ESF Ventilation Sys Not Capable of Maintaining ESF Room Temps post-accident.Caused by Inadequate Control of Sys Design Inputs.Comprehensive Action Plan Being Developed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000315/LER-1999-012-01, Re Auxiliary Building ESF Ventilation System May Not Be Capable of Maintaining ESF Room Temperature Post-Accident | Re Auxiliary Building ESF Ventilation System May Not Be Capable of Maintaining ESF Room Temperature Post-Accident | | | 05000315/LER-1999-013, :on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed |
- on 990327,safety Injection & Centrifugal Charging Throttle Valve Cavitation During LOCA Could Have Led to ECCS Pump Failure.Caused by Inadequate Original Design Application of Si.Throttle Valves Will Be Developed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(6) | | 05000315/LER-1999-014, :on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified |
- on 990521,determined That Boron Injection Tank Manway Bolts Were Not Included in ISI Program,Creating Missed Exam for Previous ISI Interval.Caused by Programmatic Weakness.Isi Program & Associated ISI Database Modified
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-015, :on 990408,RM Sys Was Not Tested IAW TS Srs. Caused by Inadequate Implementation of TS SRs in Plant Surveillance Procedures.Channel Functional Testing of RM Sys Unit Vent Effluent RMs Was Successfully Completed |
- on 990408,RM Sys Was Not Tested IAW TS Srs. Caused by Inadequate Implementation of TS SRs in Plant Surveillance Procedures.Channel Functional Testing of RM Sys Unit Vent Effluent RMs Was Successfully Completed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-016, :on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With |
- on 990615,TS Requirements for Source Range Neutron Flux Monitors Not Met.Caused by Failure to Understand Design Basis of Plant.Procedures Revised.With
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000315/LER-1999-017, :on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With |
- on 990625,noted That Improperly Installed Fuel Oil Return Relief Valve Rendered EDG Inoperable.Caused by Personnel Error.Fuel Oil Return Valve Was Replaced with Valve in Correct Orientation.With
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000315/LER-1999-018, :on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves |
- on 990629,determined That Valve Yokes May Yield Under Combined Stress of Seismic Event & Static,Valve Closed,Stem Thrust.Caused by Inadequate Design of Associated Movs.Operability Determinations Were Performed for Valves
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-019, :on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4 |
- on 990716,noted Victoreen Containment Hrrms Not Environmentally Qualified to Withstand post-LOCA Conditions.Caused by Inadequate Design Control.Reviewing Options to Support Hrrms Operability in Modes 1-4
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-020, :on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs |
- on 990727,EDGs Were Declared Inoperable.Caused by Inadequate Protection of Air Intake,Exhaust & Room Ventilation Structures from Tornado Missile Hazards. Implemented Compensatory Measures in Form of ACs
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000315/LER-1999-021, :on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed |
- on 990728,determined That GL 96-01 Test Requirements Were Not Met in Surveillance Tests.Caused by Failure to Understand Full Extent of GL Requirements. Surveillance Procedures Will Be Revised or Developed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000315/LER-1999-022, :on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary |
- on 990609,electrical Bus Degraded Voltage Setpoints Too Low for Safety Related Loads,Was Discovered. Caused by Lack of Understanding of Design of Plant.No Immediate Corrective Actions Necessary
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-023, :on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented |
- on 990907,inadequate TS Surveillance Testing of ESW Pump ESF Response Time Noted.Caused by Inadequate Understanding of Plant Design Basis.Surveillance Tests Will Be Revised & Implemented
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000315/LER-1999-024, :on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With |
- on 990708,literal TS Requirements Were Not Met by Accumlator Valve Surveillance.Caused by Misjudgement Made in Conversion from Initial DC Cook TS to W Std Ts.Submitted License Amend Request.With
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000315/LER-1999-027, LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination | LER 315/99-027-00, Underrated Fuses Used in 250 Vdc System Could Result in Lack of Protective Coordination | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) |
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