05000295/LER-1979-072, Forwards LER 79-072/03L-0

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Forwards LER 79-072/03L-0
ML19210B258
Person / Time
Site: Zion File:ZionSolutions icon.png
Issue date: 10/24/1979
From: Wandke N
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
References
NUDOCS 7911050295
Download: ML19210B258 (2)


LER-1979-072, Forwards LER 79-072/03L-0
Event date:
Report date:
2951979072R00 - NRC Website

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Commonwealth Edison Zion Genereng Station Shiloh Blvd. & Lake Michigan Zicn,Illinoe 60099 Telephon',312/746-2084 October 24, 1979 Mr. James G. Keppler Regional Director Directorate of Regulatory Operations Region III U. S. Nuclear Regulatory Commission Glen Ellyn, Illinois 60137 i

Reference:

Zion Generating Station

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Docket No. 50-295/DPR-39 Technical Specification, Section 6.6.2

Dear Mr. Keppler:

Enclosed please find Reportable Occurrence Report No.

50-295/79-72 for Zion Generating Station.

This report is submitted to you in accordance with the requirements of the Technical Specification, Section 6. 6. 2.b (2),

which states that conditions leading to operation in a degraded mode permitted by a limiting condition for operation or plant shutdown required by a limiting condition for operation require a 30-day written report.

Very truly yours,

/

N. E. Wandke Superintendent FO/dh

Enclosure:

Reportable Occurrence Report No. 50-295/79-72 1410 269 gg @ #

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2 l During normal operating the Unit 1 cassive gas monitor, 1RT-PR15, I

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l failed low and would not reset.

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[ gas samples were taken off the steam pipe tunnel rad monitor, lRT-l PR07AB, as required by Tech Spec 3.14.1.c.

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on I implications and the health and safety of the general oublic were I

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h Ju Je 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIV2 ACTIONS h l The instrument fail settina of the module drifted out of calibration.

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above the normal background levels of the monitor, causinc it to I

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The monitor was functionally tested and returned to service.

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2, Fred Ost pg&L2 746-2094 e'w Nme or rnEoAnen