05000251/LER-1981-007, Forwards LER 81-007/03L-0

From kanterella
Jump to navigation Jump to search
Forwards LER 81-007/03L-0
ML17340B299
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 05/26/1981
From: Schmidt A
FLORIDA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17340B301 List:
References
NUDOCS 8106080359
Download: ML17340B299 (2)


LER-1981-007, Forwards LER 81-007/03L-0
Event date:
Report date:
2511981007R00 - NRC Website

text

I V, QVsss Qss+IVlISVIIFEIVSI~ I"I 4O lWV.

v

~. =-

<LORIOA POWER & LIGHTCOMPANY May 26,-'1981 PRN-LI-81-254.

's Mr. James P.v O'Reilly, Director, Region II Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission 101 Marietta Street, Suite 3100 Atlanta,. Georgia 30303

Dear Mr. O'.Reilly:

REPORTABLE OCCURRENCE 2Sl-81W7 TURKEY POINT UNIT 4 DATE OF OCCURRENCE:

APRIL 26 1981 TECHNICAL SPECIFICATION 3.4.4.3 COMPONENT COOLING WATER LEAKAGE The attached Licensee Event Report is being submitted in accordance with Technical Specification 6,9 to provide 30 day notification of the subject occurrence.

Very truly yours, A.

chmidt Vice President Power Resources PLP/cab Attachment

'ef Jube 08 198t

. +~>i ten~

cc:

Director, Office of Inspection.and Enforcement (30 Harold F. Reis, Esquire File 933.1 TP "ooaog~

PEOPLE... SERVING PEOPLE

NRC FORM 2$$

(7 77l LlCEiVSEE EVENT REPORT U. S. NUCI,EAR AEQUI,ATQRYCOMMISSION CONTROL SLQCK:

I

~0:

Pl I T Pl S I

I l

IQI (PLEASE PAINT OR TYPE AI.LAEQUIREQ INFQRMATIQNI 4

Ie QP 41 1 1 1

1 Q~ Qc 1

CON'T

~0 1

0 2

3 LICCNSSS COOS LICSCVSS eueJMSCR 1$

LCCCVSC TYPC J0 SI C*r ia RCPORT IL +S OO~~'OO Q

40 41 CQCXST NVMSCR ia ia

'VCNT QATC 14 1$

plCPQATQAC $

40 EVENT OESCAIPTION ANO PAQSASLE CONSEQUENCES QIO Duri'n ower o erat o

e w

level alarm and an increasing containment sump level led operations person-nel to a failed flex tallic a

down heat exchanger..

CCW was isolated to the heat exchanger.

This failure r

is reportable because T.S. 3.4.4.3 requires all valves, piping, and interlocks to be o erable.

I 3

1 4

leakage by using an off normal operations procedure.

The heat exchanger w

isolated and will be re aired durin the next outa e.

SYSTC'4

CAUSE

CAUSE

COMP, VALV4 CQQC CQOC 5VSCQOC COMPONENT COO C 3UCCQQC SUSCQOC I.L~JQII L~JQ L~JGS <<E <<<<8 uCQ W~GE 9

lu II I2 Ia

'S 19 20 SCQTJCNTIAl OCCIRRRCNCS ACPCA.

Pl CVI5 I0 N LSRIRO SVCNT Y'CAA RCPORT NO.

CQQC

.VQ.

QTT RCPORT

~81

~

~00 7

~r

~QZ

~z,

~

~p' I

12 24 24

S 29 0

~ I 22 ACTION SVEUAC CSSCC

~

SHVTQQVIN

  • T.ACICMCNT VPRQM PRIME CQMP.

CQM NON CN T TAKEN ACTION ON PLANT MCTCNQO HOURS ~2~

SUSMITTCO 40AR4 >VS.

SVPPUCR VANVSACTVACR LOQLICC LLCO Lpee ~u LJQ LJQ LLOC ~T" 14 24 11 40, 41 44 41 CAUSE OESCRIPTION ANO COAREC. IVS ACTIONS Q27

~

~I 0

The excess letdown heat: exch'r was identified as the source of the 077ICR STATUS Q NA 44 VITYQ>S 44 NAME QF PREPAAEA L

PACE 4

1 3 9r FACILITY

- 5TATvs,. ~ POYICR o

i '

QR ~lo 0Q~

'2 9, Io I2 Ls ACTIVITY 'QN TCNT

  • RCLCASSO OS ACLCASC R

AMQVNI'QSACTI

~IS )~Z Qs.

~ZQS.

NA 10 II

>CR50NNCL CXPCSVASS uuMSCR,~

TYPE

. QCSCRIPTION~

C

'14

. ~ir ~00 QOT ~ZsQe.'A I

3 PCRSONNCI PNJURI$ 3,, "L NUMSCR

~

QCSCRIPTICNQAI C

~001.0'O

".r NA 1

3' II I2 LCSsct CA QAMACis ~ 0 SACILITYQ42

~ VPCi 023 RIPEICN CZ ~zQ2'A

)

PUSLIC:. Y

ssu20

'cscRISY:CN Q 0

t NIQ<<.

NA 3 )'O 20 10 T

30 PIRC US-Qccll Y sa 30

. (305 52-3801 MCTIRCO QS OISCQVCRY OISCQVCRY OCSCRIPTIQN QS2

~AQSI Off Normal Procedure 45 4$

LOCATICNOS RELEASE QS NA