LER-1980-002, /01T-0:on 800405,while in Shutdown Mode W/Fuel Removed,Contaminated Demineralized Water Was Being Heated & Added to Primary Sys.Tube Leaks in Heat Exchanger Were Found Leaking Water Into River.Caused by Unloader Tube Failure |
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| 0101980002R01 - NRC Website |
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60 61 OOCXET NU.VSER 68 69 EVENT DATE 74 IS REPORT QATE dQ EVENT CESCRIPTICN AND PACBA8LE CONSECUENCES h ia}2 l While in the shutdown mode with all fuel removed, contaminated demineralized water was[
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o ATTACHMENT TO LICENSEE EVENT REPORT S0-002/OlT-0 COMMONWEAI.TH EDISCN COMPANY (CWE)
DRESDEN UNIT (ILDRS 1)
DOCKET 1 050-010 With the plant in the shutdown mode and with all fuel removed, a leak developed in the 3 unloader heat exchanger which resulted in a release of radioactive water from the primary system to the service water system.
This event led to a release to the environment.
From April 2 thru 5 in preparation for the 200 pound hydro on the primary system, required as a part of the pre chemical cleaning activities, contaminated danineralized water was added to the primary system through the "A" unloader heat exchanger. To maintain reactor vessel flange tempera-ture within Tech Spec limits, heating boiler steam was used to heat the makeup water. Heating boiler condensate was then returned to the service water header where it was discharged to the canal by a single service water pump rated at 4300 gpm.
Af ter the filling operations had begun, it was determined that leakage from the pri=ary system was above normal. However, it was believed that the leakage was contained and was into the newly installed chemical cleaning crossties acd the radvaste system. Consequently, opera: Ors were sent out to inspect for leakage pathways, but because of the high radia-tion fields, the inspection was severly limited to their length of :ime in radiation areas.
During this time, April i-3, several smaller fills were made to saintain level in the steam drum and efforts continued to locate the leakage.
3 oiler steam again was used to maintain temperature vi:h the s:eam supply being throttled as required. The staam supply was eventually isolated at 0053 on April 5.
Routine. daily discharge canal composi:e water samples for the period April 2-4 were within limits and were ao: significantly above reutinely observed values. However, on April 5 at 1110 Radiation ?rotection no:ified the operating Shif t Engineer that the Uni: 1 discharge canal sample seasured 1737pCisi A sixty minute isotopic crunt indica:ed that :encentra: ions in the discharge canal were 9.1" Of the MFC for the identified nuclides.
Later a 1000 minu:e count of the same sample revealed tha: the cencentrations were actually 14.3% of the MPC for':he identified nuclides.
At 1326 hours0.0153 days <br />0.368 hours <br />0.00219 weeks <br />5.04543e-4 months <br />, the 3 unloader heat exchanger was isolated and the condensate re: urn line :: the service water system was 7alved c1: sed.
Ac this time leakage fr m :he primary system fr:pped :: approximately 30 gallons / hour. At 1530 :he NRC Inergency Center was notified of the release lad an ini:ial es ima:c of :he :::21 : uria conten: was 2.93 millituries.
This was determined fr:m an estica:ed water loss of 53,000 gallons and a gr ss 10:171:7 of 1.1 x 10J pCi..&.
- ni:ial vater loss estimates were made fr:m :ne steam drum level recorder anc :he ac:ivity was decernined fr:m :he :encen:ra:icn af :he : ntamina:ed de dneralized va:er ir:m "A"
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storage tank which was used to fill :he primary system.
It was apparent at this time the "B" unloader had experienced tube failure and that water from the shell side was leaking into the tube (steam) side and being released through the condensate line Lato the service water.
On April 9 it was reported to NRC personnel that the total curie release was.135 curie. This was based on the revised volume of 76,000 gallons and concentrations, believed to be more indicative of the activity released, determined from a sample which was obtained from the shell side of the "3" unloader heat exchanger. At this time only the gross activity of the water was known and later isotopic analysis revealed the total curie release : be.620 curie. Also at this time we reported that the
=aximum concentration identified occurred on April 6 when a composite sample taken from the canal yielded an isotopic concentration for the mixture of 22*,'
of the MPC for the identified nuclides.
Based on the results of our investigation, the release does not pose a health or saf ety ha:ard to the public. Corrective steps will be taken to assure that an event of this nature does not occur again. These actions include:
- 1) replace the existing unloader heat exchanger after chemical cleaning;
- 2) cut and cap the 2" condensate crosstie to the service water prior to further use of the heat exchanger; 3) begin sampling service water for activity on a routine basis; 4) develop lower reporting / action levels for canal discharge and service water activities to give the opera-
- ors an earlier alert of possible unusual condi:1ons prior :o exceeding Tech Spec linics.
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DEVIATION REPORT
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Commonwealth Edison sTA UNIT YEAR N C.
0 1 30 - 5 PrRT lj T1 TLE OF OEVIATICN CCCU RRED Cnplanned and Uncontrolled Release of Radioactivity to Discharge Canal 4-5-30, 15,26 A,e IMd 3YSTEM AFFECTED PLANT CCN0lTIONS TESTING o d mary Sys tem S-D 0
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.rn e 1737.4 oci/L. (T.S. Limit 100 oci/L) with only one service water cump on (6000 gpm).
DESCRIPTION OF CAUSE Fairure of L "3"
unloading heat exchanger tube / tubes while heatinz reactor.
CTHER AP LI CABLE INFCPMATI CN
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| 05000249/LER-1980-001-03, /03L-0:on 800116,loss of Sampling Point Automatic Advance for Drywell Oxygen Analyzer Noted During Normal Operation.Caused by Electrical Failure of Stepping Switch Motor Part 808376.Motor Replaced & Advance Restored | /03L-0:on 800116,loss of Sampling Point Automatic Advance for Drywell Oxygen Analyzer Noted During Normal Operation.Caused by Electrical Failure of Stepping Switch Motor Part 808376.Motor Replaced & Advance Restored | | | 05000237/LER-1980-001, /03L-0 for Dresden, Unit 2 Re While Performing Weekly Turbine Control Valve Exercising, the 1/2 Scram on RPS Channel a Received from the Closure of 3 Turbine Control Valve Would Not Reset | /03L-0 for Dresden, Unit 2 Re While Performing Weekly Turbine Control Valve Exercising, the 1/2 Scram on RPS Channel a Received from the Closure of 3 Turbine Control Valve Would Not Reset | | | 05000010/LER-1980-001-03, /03L-0:on 800303,capacity in Unit 1 Fire Pump Found to Be in Need of Updating in Order to Be Equal to Unit 2/3 Fire Pump.Commitment Made to NRC to Increase Capacity.New Fire Pump Will Be Installed | /03L-0:on 800303,capacity in Unit 1 Fire Pump Found to Be in Need of Updating in Order to Be Equal to Unit 2/3 Fire Pump.Commitment Made to NRC to Increase Capacity.New Fire Pump Will Be Installed | | | 05000010/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000237/LER-1980-002, /03X-1 for Dresden Unit 3 Regarding During Normal Operation While Performing LPCI Monthly Surveillance, MO-3-1501-118 Valve Would Not Close | /03X-1 for Dresden Unit 3 Regarding During Normal Operation While Performing LPCI Monthly Surveillance, MO-3-1501-118 Valve Would Not Close | | | 05000249/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000010/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000010/LER-1980-002-01, /01T-0:on 800405,while in Shutdown Mode W/Fuel Removed,Contaminated Demineralized Water Was Being Heated & Added to Primary Sys.Tube Leaks in Heat Exchanger Were Found Leaking Water Into River.Caused by Unloader Tube Failure | /01T-0:on 800405,while in Shutdown Mode W/Fuel Removed,Contaminated Demineralized Water Was Being Heated & Added to Primary Sys.Tube Leaks in Heat Exchanger Were Found Leaking Water Into River.Caused by Unloader Tube Failure | | | 05000249/LER-1980-002-03, /03L-0:on 800122,while Performing LPCI Monthly surveillance,MO-3-1501-11B Valve Would Not Close. Reoccurrence on 800213.Investigation Revealed No Cause | /03L-0:on 800122,while Performing LPCI Monthly surveillance,MO-3-1501-11B Valve Would Not Close. Reoccurrence on 800213.Investigation Revealed No Cause | | | 05000010/LER-1980-003-02, Has Been Cancelled | Has Been Cancelled | | | 05000249/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000249/LER-1980-004-03, /03L-0:on 800202,while Increasing Load by 2 Mwe Per Hour,Alarms Received in Control Room Indicating Failed Jet Pump.Jet Pump 13 Failed.Cause & Corrective Action Will Be Described in Supplemental Rept | /03L-0:on 800202,while Increasing Load by 2 Mwe Per Hour,Alarms Received in Control Room Indicating Failed Jet Pump.Jet Pump 13 Failed.Cause & Corrective Action Will Be Described in Supplemental Rept | | | 05000010/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000010/LER-1980-004-03, /03L-0:on 800724,during Outage,While Processing Water in Holdup tank,98-h Elapsed W/O Sampling.Caused by Personnel Failure to Follow Procedure for Sampling Radwaste Storage Tanks.Personnel Reinstructed | /03L-0:on 800724,during Outage,While Processing Water in Holdup tank,98-h Elapsed W/O Sampling.Caused by Personnel Failure to Follow Procedure for Sampling Radwaste Storage Tanks.Personnel Reinstructed | | | 05000249/LER-1980-005-01, /01T-0:on 800213,while in S/D Mode,Msiv Scram Limit Switches Were Checked & of 16 Limit Switches,Two Found to Have Setpoints Greater than 10%.Caused by Switch Out of Calibr.Limit Switches Readjusted | /01T-0:on 800213,while in S/D Mode,Msiv Scram Limit Switches Were Checked & of 16 Limit Switches,Two Found to Have Setpoints Greater than 10%.Caused by Switch Out of Calibr.Limit Switches Readjusted | | | 05000249/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000249/LER-1980-006-03, /03L-0:on 800215,during Local Leak Rate Test Performed on a Feedwater Inboard Check Valve 3-220-58A Measured Leakage Exceeded Tech Specs.Caused by Worn Seat/ Disc Assembly Pins | /03L-0:on 800215,during Local Leak Rate Test Performed on a Feedwater Inboard Check Valve 3-220-58A Measured Leakage Exceeded Tech Specs.Caused by Worn Seat/ Disc Assembly Pins | | | 05000249/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000249/LER-1980-007-03, /03L-0:on 800209,during Local Leak Rate Test of Containment Vent Line,Measured Leakage Exceeded Tech Specs. Investigation Showed Valve AO-3-1601-23 Leaking Through. Caused by Normal Expected Wear of Rubber Seats | /03L-0:on 800209,during Local Leak Rate Test of Containment Vent Line,Measured Leakage Exceeded Tech Specs. Investigation Showed Valve AO-3-1601-23 Leaking Through. Caused by Normal Expected Wear of Rubber Seats | | | 05000249/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000249/LER-1980-008-03, /03L-0:on 800307,during Refueling Outage While Performing Temp Switch Calibr Surveillance,Three Temp Switches Failed to Trip Per Specs.Caused by Drift,Excessive Gap Between Actuator & Switch Plunger or Dirty Contacts | /03L-0:on 800307,during Refueling Outage While Performing Temp Switch Calibr Surveillance,Three Temp Switches Failed to Trip Per Specs.Caused by Drift,Excessive Gap Between Actuator & Switch Plunger or Dirty Contacts | | | 05000237/LER-1980-008, /03L-0 for Dresden, Unit 2 Re Equipment Operator Discovered Level in the 2/3 Diesel Generator Coolant Water Expansion Head Tank Overflowing Thru the Vent Line | /03L-0 for Dresden, Unit 2 Re Equipment Operator Discovered Level in the 2/3 Diesel Generator Coolant Water Expansion Head Tank Overflowing Thru the Vent Line | | | 05000249/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000249/LER-1980-009-03, /03L-0:on 800306,during Refueling Outage,While Performing LPCI Logic Tests,Injection Valve Mo 3-1501-22A Failed to Open.Caused by Loose Wire on Terminal Block in MCC-38-7 Due to Stripped Brass Screw | /03L-0:on 800306,during Refueling Outage,While Performing LPCI Logic Tests,Injection Valve Mo 3-1501-22A Failed to Open.Caused by Loose Wire on Terminal Block in MCC-38-7 Due to Stripped Brass Screw | | | 05000249/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000249/LER-1980-010, /03L-0 for Dresden Unit 3 Regarding Relief Valves Rv 1105A and 1105B Actuating at 1525 and 1520 PSIG Respectively | /03L-0 for Dresden Unit 3 Regarding Relief Valves Rv 1105A and 1105B Actuating at 1525 and 1520 PSIG Respectively | | | 05000249/LER-1980-011-03, /03L-0:on 800305,while Conducting Steam Line Area Temp Switch Calibr Surveillance,Temp Switch TS 3-261-17B Tripped Above Tech Specs.Caused by Dirt Deposits on Switch Actuation Plunger.Switch Cleaned,Adjusted & Tested | /03L-0:on 800305,while Conducting Steam Line Area Temp Switch Calibr Surveillance,Temp Switch TS 3-261-17B Tripped Above Tech Specs.Caused by Dirt Deposits on Switch Actuation Plunger.Switch Cleaned,Adjusted & Tested | | | 05000249/LER-1980-011, /03L-0 for Dresden Unit 3 Regarding Temperature Switch TS 3-261-17B Tripping at 203.1 Degrees Fahrenheit Which Is Above the Technical Specification | /03L-0 for Dresden Unit 3 Regarding Temperature Switch TS 3-261-17B Tripping at 203.1 Degrees Fahrenheit Which Is Above the Technical Specification | | | 05000249/LER-1980-012, /03L-0 for Dresden Unit 3 Regarding Fuel Pool Area ARM Channels a and B Tripping at Levels Exceeding the Technical Specification | /03L-0 for Dresden Unit 3 Regarding Fuel Pool Area ARM Channels a and B Tripping at Levels Exceeding the Technical Specification | | | 05000249/LER-1980-013, /03L-0 for Dresden Unit 3 Regarding B Feedwater Outboard Check Valve 3-220-62B Leakage Exceeding Limit for a Single Isolation Valve | /03L-0 for Dresden Unit 3 Regarding B Feedwater Outboard Check Valve 3-220-62B Leakage Exceeding Limit for a Single Isolation Valve | | | 05000249/LER-1980-015, /01T-0 for Dresden Unit 3 Regarding Discovery of Reactor Water Cleanup Mechanical Snubber Fully Retracted | /01T-0 for Dresden Unit 3 Regarding Discovery of Reactor Water Cleanup Mechanical Snubber Fully Retracted | | | 05000237/LER-1980-015, /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33A Was Found Inoperable During Routine Operability Surveillance | /03L-0 for Dresden, Unit 2 Re During Steady State Operation, Torus to Drywell Vacuum Breaker 2-1601-33A Was Found Inoperable During Routine Operability Surveillance | | | 05000237/LER-1980-016, /01T-1 for Dresden, Unit 2 Re While Shutdown and Conducting 300 Psi Primary System Hydrostatic Leak Inspection, Water Discovered Dripping from LPCI Check Valve Up Stream Drain Line | /01T-1 for Dresden, Unit 2 Re While Shutdown and Conducting 300 Psi Primary System Hydrostatic Leak Inspection, Water Discovered Dripping from LPCI Check Valve Up Stream Drain Line | | | 05000237/LER-1980-017, /03L-0 for Dresden, Unit 2 Re Double Valve Indication Was Observed on the HPCI Inboard Isolation Valve. Upon Trying to Cycle the Valve, the Valve Failed to Close | /03L-0 for Dresden, Unit 2 Re Double Valve Indication Was Observed on the HPCI Inboard Isolation Valve. Upon Trying to Cycle the Valve, the Valve Failed to Close | | | 05000249/LER-1980-017, /03L-0 for Dresden Unit 3 Regarding During Refueling Outage, While Conducting Operability Surveillance Test, U-3 Diesel Generator Failed to Start | /03L-0 for Dresden Unit 3 Regarding During Refueling Outage, While Conducting Operability Surveillance Test, U-3 Diesel Generator Failed to Start | | | 05000249/LER-1980-019-03, /03L-0:on 800420,during Switch Calibr Surveillance,Target Rock Relief Valve Press Switch PS-3-203-3A Tripped Below Tech Specs Limit.Caused by Setpoint Drift.Switch Readjusted within Tech Specs Limit | /03L-0:on 800420,during Switch Calibr Surveillance,Target Rock Relief Valve Press Switch PS-3-203-3A Tripped Below Tech Specs Limit.Caused by Setpoint Drift.Switch Readjusted within Tech Specs Limit | | | 05000249/LER-1980-019, Forwards LER 80-019/03L-0 | Forwards LER 80-019/03L-0 | | | 05000249/LER-1980-021, /01T-0 for Dresden Unit 3 Regarding During Startup Following Refueling Outage, Combinations of 3A Target Rock Valve and 3B, 3C and 3E Electromatic Relief Valves Failed to Open at Rated Reactor Pressure While Performing Operabil | /01T-0 for Dresden Unit 3 Regarding During Startup Following Refueling Outage, Combinations of 3A Target Rock Valve and 3B, 3C and 3E Electromatic Relief Valves Failed to Open at Rated Reactor Pressure While Performing Operability Surveilla | | | 05000249/LER-1980-021-01, /01T-0:on 800425,combinations of 3A Target Rock Valve & 3B,3C & 3E Electromatic Relief Valves Failed to Open at Rated Reactor Pressure.Caused by Improper Bolted Air Operator,Pilot Valve Problems & Jammed Cutout Switch | /01T-0:on 800425,combinations of 3A Target Rock Valve & 3B,3C & 3E Electromatic Relief Valves Failed to Open at Rated Reactor Pressure.Caused by Improper Bolted Air Operator,Pilot Valve Problems & Jammed Cutout Switch | | | 05000237/LER-1980-022, /03L-0 for Dresden Unit 3 Regarding During Normal Shutdown Conditions, IRM 12 Downscale Rod Block Was Found to Trip at 4/125 | /03L-0 for Dresden Unit 3 Regarding During Normal Shutdown Conditions, IRM 12 Downscale Rod Block Was Found to Trip at 4/125 | | | 05000237/LER-1980-023, /03L-0 for Dresden Unit 3 Regarding During Normal Operation with Reactor Level Instrument Surveillance in Progress, Level Switch LIS 3-263-58A Tripped at Less than Tech. Spec. Limit of 144 Inches | /03L-0 for Dresden Unit 3 Regarding During Normal Operation with Reactor Level Instrument Surveillance in Progress, Level Switch LIS 3-263-58A Tripped at Less than Tech. Spec. Limit of 144 Inches | | | 05000237/LER-1980-024, /03L-0 for Dresden, Unit 2 Re Drywell Oxygen Concentration Indication Failed Downscale in Violation of Tech. Spec. 3.7.A.6.d | /03L-0 for Dresden, Unit 2 Re Drywell Oxygen Concentration Indication Failed Downscale in Violation of Tech. Spec. 3.7.A.6.d | | | 05000237/LER-1980-025, /03L-0 for Dresden Unit 3 Regarding During Normal Operation While Performing Main Steam Line High Flow Isolation Surveillance, Flow Switch DPIS 3-261-2A Was Out of Tech. Spec. Limits, Table 3.2.1 | /03L-0 for Dresden Unit 3 Regarding During Normal Operation While Performing Main Steam Line High Flow Isolation Surveillance, Flow Switch DPIS 3-261-2A Was Out of Tech. Spec. Limits, Table 3.2.1 | | | 05000237/LER-1980-027, /03L-0 for Dresden, Unit 2 Re Dropping Load in Preparation for I.E.B. 80-17 Scram Tests, Low Level of Diesel Generator Coolant Present in the Water Tank Was Noticed by Equipment Operator | /03L-0 for Dresden, Unit 2 Re Dropping Load in Preparation for I.E.B. 80-17 Scram Tests, Low Level of Diesel Generator Coolant Present in the Water Tank Was Noticed by Equipment Operator | | | 05000249/LER-1980-028, Forwards LER 80-028/03L-0 | Forwards LER 80-028/03L-0 | | | 05000249/LER-1980-028-03, /03L-0:on 800718,during Setpoint Surveillance, Solenoid Valve for Torus to Reactor Bldg Vacuum Breaker 3-1601-20A Determined Inoperative,Preventing Valve from Opening.Caused by Mechanical Failure.Valve Replaced | /03L-0:on 800718,during Setpoint Surveillance, Solenoid Valve for Torus to Reactor Bldg Vacuum Breaker 3-1601-20A Determined Inoperative,Preventing Valve from Opening.Caused by Mechanical Failure.Valve Replaced | | | 05000249/LER-1980-030, /03L-0 for Dresden Unit 3 Regarding While Reducing Power for Manual Scram Required by I.E. Bulletin 80-17, Routine Surveillance of MSIV Closure Times Showed That MSIVs 3-203-2B and 2D Closed in Less than 3 Seconds | /03L-0 for Dresden Unit 3 Regarding While Reducing Power for Manual Scram Required by I.E. Bulletin 80-17, Routine Surveillance of MSIV Closure Times Showed That MSIVs 3-203-2B and 2D Closed in Less than 3 Seconds | | | 05000249/LER-1980-032, /03L-0 for Dresden Unit 3 Regarding During Normal Operations While Performing APRM Rod Block and Scram Functional Tests, APRM 3 Failed to Initiate a Rod Block | /03L-0 for Dresden Unit 3 Regarding During Normal Operations While Performing APRM Rod Block and Scram Functional Tests, APRM 3 Failed to Initiate a Rod Block | | | 05000249/LER-1980-033, Forwards LER 80-033/03L-0 | Forwards LER 80-033/03L-0 | | | 05000249/LER-1980-033-03, /03L-0:on 800724,during Normal operations,1/4-inch through-wall Leak Discovered in 3A Component Cooling Svc Water Pump Casing.Caused by Casting Hole on Bottom of Casing.Pump Removed & Hole Plugged | /03L-0:on 800724,during Normal operations,1/4-inch through-wall Leak Discovered in 3A Component Cooling Svc Water Pump Casing.Caused by Casting Hole on Bottom of Casing.Pump Removed & Hole Plugged | |
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