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 Entered dateEvent description
ENS 546976 May 2020 14:11:00This 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a general containment isolation signal affecting more than one system. On March 8, 2020, at approximately 2021 CDT, Browns Ferry Nuclear Plant Unit 2 experienced an unexpected loss of the 2A Reactor Protection System (RPS). This resulted in Primary Containment Isolation System (PCIS) groups 2, 3, 6, and 8 isolations, and the initiation of Standby Gas Treatment Trains A and B, and Control Room Emergency Ventilation System Train A. All affected safety systems responded as expected. Plant conditions which initiate PCIS Group 2 actuations are Reactor Vessel Low Water Level (Level 3) or High Drywell Pressure. The PCIS Group 3 actuations are initiated by Reactor Vessel Low Water Level (Level 3) or Reactor Water Cleanup Area High Temperature. The PCIS Group 6 actuations are initiated by Reactor Vessel Low Water Level (Level 3), High Drywell Pressure, or Reactor Building Ventilation Exhaust High Radiation (Reactor Zone or Refuel Zone). The PCIS Group 8 actuations are initiated by Low Reactor Vessel Water Level (Level 3) or High Drywell Pressure. At the time of the event, these conditions did not exist; therefore, the actuation of the PCIS was invalid. The RPS MG Set trip was believed to have been caused by an intermittent short across a spike suppressor, which led to a loss of generator output signal to a voltage regulator. The affected components have been replaced. There were no safety consequences or impact to the health and safety of the public as a result of this event. This event was entered into the Corrective Action Program as Condition Report 1593265. The NRC Resident Inspector has been notified of this event.