ENS 51003
ENS Event | |
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22:02 Feb 24, 2015 | |
Title | 60-Day Optional Telephone Notification of Invalid System Actuation Due to Motor Generator Output Breaker Trip |
Event Description | On February 24, 2015, at approximately 1702 CDT, while the plant was in cold shutdown, power was lost on the Division 1 reactor protection system (RPS) bus. This event resulted in the automatic closure of the Division 1 primary containment isolation valves in the residual heat removal (RHR) and reactor water cleanup systems. Additionally, the primary containment atmospheric monitoring system automatically actuated, and ventilation systems in the fuel building, auxiliary building, and control building shifted to emergency mode. The closure of the isolation valves in the residual heat removal system caused an automatic trip of the 'A' RHR pump, which had been in the shutdown cooling alignment. The equipment response to the isolation signal was as expected. This event is being reported in accordance with 10 CFR 50.73(a)(1) as an invalid actuation of the Division 1 primary containment isolation system.
The isolation was promptly diagnosed as having resulted from a trip of the output breaker of the RPS motor generator (MG) set 'A,' and not from a valid signal. Operators implemented the appropriate response procedures to align power to the bus via the alternate source, and began restoring the affected systems. The 'A' RHR pump was re-started within twelve minutes, during which time coolant temperature increased approximately seven degrees to a maximum of approximately 100F. Other affected systems were restored over the next few hours. The causal analysis concluded that the MG set output breaker tripped due to an overly conservative setpoint on the overvoltage trip relay. The low trip setpoint was a latent condition that had existed since the output voltage was raised in 1988 at the recommendation of the vendor, but at which time the trip setpoint was not changed. To correct this condition, the MG overvoltage trip setpoint was raised to restore adequate operating margin to the normal MG output voltage. At the time of the event, the plant was in MODE 5 with the reactor cavity flooded to greater than 23 feet above the vessel flange. The shutdown cooling system was promptly restored to service. This event was of minimal safety significance to the health and safety of employees and the public. The licensee has notified the NRC Resident Inspector. |
Where | |
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River Bend Louisiana (NRC Region 4) | |
Reporting | |
10 CFR 50.73(a)(1), Submit an LER, Invalid Actuation | |
Time - Person (Reporting Time:+1361.27 h56.72 days <br />8.103 weeks <br />1.865 months <br />) | |
Opened: | Russell Zahorchak 14:18 Apr 22, 2015 |
NRC Officer: | Charles Teal |
Last Updated: | Apr 22, 2015 |
51003 - NRC Website | |
WEEKMONTHYEARENS 541212019-04-30T11:50:00030 April 2019 11:50:00
[Table view]10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephonic Notification Due to Invalid Actuation of a General Containment Isolation Signal ENS 517842016-01-10T08:43:00010 January 2016 08:43:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of the Primary Containment Isolation Logic ENS 510032015-02-24T22:02:00024 February 2015 22:02:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Telephone Notification of Invalid System Actuation Due to Motor Generator Output Breaker Trip ENS 507742014-12-06T16:12:0006 December 2014 16:12:00 10 CFR 50.73(a)(1), Submit an LER 60 Day Optional Report - Half Scram and a Division 2 Primary Containment Isolation Signal ENS 468442011-03-20T12:24:00020 March 2011 12:24:00 10 CFR 50.73(a)(1), Submit an LER "a" Train Reactor Protection System Unexpectedly De-Energized Resulting in a Half Scram Signal ENS 445172008-08-01T00:30:0001 August 2008 00:30:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Containment Isolation Valves Due to a Power Failure ENS 443472008-06-02T11:24:0002 June 2008 11:24:00 10 CFR 50.73(a)(1), Submit an LER Invalid System Actuation of Division 1 Containment Isolation Valves ENS 442782008-04-23T20:56:00023 April 2008 20:56:00 10 CFR 50.73(a)(1), Submit an LER 60-Day Optional Notification of Invalid Specified System Actuation ENS 430122006-09-29T18:33:00029 September 2006 18:33:00 10 CFR 50.73(a)(1), Submit an LER Invalid Specific System Actuation ENS 408472004-05-22T09:29:00022 May 2004 09:29:00 10 CFR 50.73(a)(1), Submit an LER Invalid Actuation of Division 1 Primary Containment Isolation Due to Loss of a Rps Bus 2019-04-30T11:50:00 | |