ENS 50467
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ENS Event | |
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15:50 Sep 18, 2014 | |
Title | Technical Specification Required Shutdown Due to Misaligned Control Rod |
Event Description | During the performance of PT-Q89, Control Rod Exercise Test, Rod G-3 in Shutdown Bank 'B' misaligned (stepped in) to approximately 195-200 steps indicated with group demand at 217 steps. The movable gripper fuse was suspect, found not blown [so further] troubleshooting required. At 1150 [EDT], the decision was made to reduce power to approximately 70% within two hours per I.T.S. [Improved Technical Specification] 3.1.4.b.2.2. The plant is currently stable at 68% power. I.T.S. 3.1.5.b.1 was also entered for Shutdown Bank 'B' less than allowable insertion limits at time 1228 [EDT] to be in Mode 3 in 6 hrs. (1828 [EDT]).
The licensee notified the New York Independent System Operator, the New York Public Service Commission and the NRC Resident Inspector. |
Where | |
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Indian Point New York (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
Time - Person (Reporting Time:+-2.82 h-0.118 days <br />-0.0168 weeks <br />-0.00386 months <br />) | |
Opened: | John Taylor 13:01 Sep 18, 2014 |
NRC Officer: | Howie Crouch |
Last Updated: | Sep 18, 2014 |
50467 - NRC Website | |
Unit 2 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (68 %) |
WEEKMONTHYEARENS 535892018-09-07T04:00:0007 September 2018 04:00:00
[Table view]10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Technical Specification Required Shutdown ENS 520392016-06-24T08:00:00024 June 2016 08:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Ts Required Shutdown Due to Leaking Service Water Weld on Ccw Hx ENS 507222015-01-08T12:00:0008 January 2015 12:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Loss of Both Channels of Refueling Water Storage Tank Instrumentation ENS 504672014-09-18T15:50:00018 September 2014 15:50:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Misaligned Control Rod ENS 478032012-04-04T09:00:0004 April 2012 09:00:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Static Inverter ENS 473142011-10-03T07:45:0003 October 2011 07:45:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unit 2 Entered Tech Spec 3.0.3 After Declaring All Three Containment Recirc Fan Coolers Inoperable ENS 466372011-02-22T19:25:00022 February 2011 19:25:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Service Water Piping Leak ENS 400692003-08-14T20:23:00014 August 2003 20:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Unusual Event Declared Due to Loss of Offsite Power Greater than 15 Minutes. 2018-09-07T04:00:00 | |
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