ENS 43381
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ENS Event | |
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07:11 May 24, 2007 | |
Title | Manual Reactor Scram Due to Electro-Hydraulic Control (Ehc) System Leak |
Event Description | On 05/24/2007 at 0211 CDT Browns Ferry Unit 1 initiated a Manual reactor SCRAM due to an Electro-Hydraulic Control (EHC) System pressure lowering and reservoir level lowering due to an EHC system leak. The leak was from #6 Main Turbine Combined Intermediate Valve (CIV). All Systems responded as required to the manual SCRAM signal. No Emergency Core Cooling System (ECCS) initiations occurred as a result of the manual SCRAM signal. Reactor water level was maintained in the normal band during the SCRAM. There were no Primary Containment Isolation signals received during the SCRAM. The EHC leak was stopped due to reservoir level depletion and EHC pumps being secured. There were no indications of main steam relief valves (MSRVs) opening. Reactor pressure is being controlled using Main Steam Line Drains. Reactor Level is being maintained in band using Control Rod Drive pumps. Repair of the EHC leak is in progress.
The Scram was characterized as uncomplicated. All rods fully inserted. The only significant equipment out of service at the time was RCIC. When the leak was initially discovered, it was about 60 drops per minute. When repairs were attempted, the piping separated and approximately 600 gallons of EHC fluid was discharged out the break onto the turbine building floor. Cleanup of the EHC fluid is in progress and environmental monitoring is in place to assure no offsite release of the spill. The licensee notified the NRC Resident Inspector. |
Where | |
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Browns Ferry Alabama (NRC Region 2) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-2.48 h-0.103 days <br />-0.0148 weeks <br />-0.0034 months <br />) | |
Opened: | Tim Boland 04:42 May 24, 2007 |
NRC Officer: | Bill Huffman |
Last Updated: | May 24, 2007 |
43381 - NRC Website | |
Unit 1 | |
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Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Startup (3 %) |
After | Hot Shutdown (0 %) |
Browns Ferry with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 569902024-02-24T08:19:00024 February 2024 08:19:00
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Scram Discharge Volume (Sdv) High Water Level ENS 468052011-05-02T11:26:0002 May 2011 11:26:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Specified System Actuation Due to a Emergency Diesel Generator Output Breaker Trip ENS 468012011-04-29T04:38:00029 April 2011 04:38:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Primary Containment Isolation System Actuation Due to Loss of Power from a Diesel Generator ENS 467932011-04-27T22:01:00027 April 2011 22:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(xiii), Loss of Emergency Preparedness Notification of Unusual Event Due to Loss of Offsite Power ENS 465112010-12-26T22:20:00026 December 2010 22:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to High Vibration on Main Generator Exciter ENS 459902010-06-09T08:31:0009 June 2010 08:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to Closure of Main Steam Isolation Valves ENS 458882010-04-30T21:48:00030 April 2010 21:48:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Light Socket Short Causes Isolation Systems to Actuate ENS 453912009-09-30T04:23:00030 September 2009 04:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Unit 2 Manually Scrammed After Trip of an Operating Condensate Pump and Rapidly Lowering Rvwl ENS 452902009-08-24T23:50:00024 August 2009 23:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Condensate Booster Pump Trip Resulting in a Manual Reactor Scram ENS 448602009-02-18T09:51:00018 February 2009 09:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Due to Power Load Unbalance Signal on Main Generator Resulting in Reactor Scram ENS 448542009-02-16T11:13:00016 February 2009 11:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Loss of Stator Cooling Water ENS 445402008-10-05T03:08:0005 October 2008 03:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Following Reverse Power Signal on Main Generator ENS 441872008-05-05T08:32:0005 May 2008 08:32:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Loss of Power to Esf Buses During Transfer of Offsite Power Source ENS 438782008-01-01T03:40:0001 January 2008 03:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 3 Automatic Scram Due to Main Generator Load Reject Signal ENS 437182007-10-12T13:02:00012 October 2007 13:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Turbine Trip ENS 436132007-09-03T07:14:0003 September 2007 07:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Electro-Hydraulic Control (Ehc) System Leak ENS 435602007-08-11T22:51:00011 August 2007 22:51:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Scram Due to Neutron Monitoring Trip Signal ENS 434142007-06-09T16:00:0009 June 2007 16:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due Turbine Trip as a Result of High Moisture Separator Reheater Tank Level ENS 433812007-05-24T07:11:00024 May 2007 07:11:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Electro-Hydraulic Control (Ehc) System Leak ENS 431592007-02-09T18:08:0009 February 2007 18:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Reactor Scram Due to Low Reactor Water Level ENS 430922007-01-11T14:16:00011 January 2007 14:16:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram When Turbine Output Breakers Opened ENS 428132006-08-30T03:25:00030 August 2006 03:25:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram Due to Electro-Hydraulic Oil Leak ENS 427872006-08-19T16:05:00019 August 2006 16:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram of Unit 3 Due to the Loss of Both Reactor Recirculation Pumps ENS 421022005-10-31T19:18:00031 October 2005 19:18:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Trip of Main Turbine ENS 419972005-09-17T16:29:00017 September 2005 16:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to Maintenance ENS 418962005-08-05T22:08:0005 August 2005 22:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge Rps Actuation Due to Low Reactor Water Level Caused by Loss of Reactor Feed Pumps ENS 415952005-04-13T15:53:00013 April 2005 15:53:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Rps Actuation Due to an Invalid Atws Logic Actuation ENS 414042005-02-11T22:29:00011 February 2005 22:29:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to a Load Rejection ENS 412192004-11-23T16:02:00023 November 2004 16:02:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to Turbine Trip ENS 408622004-07-11T03:35:00011 July 2004 03:35:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Scram Due to an Upscale Trip on Intermediate Range Monitors ENS 408582004-07-09T03:32:0009 July 2004 03:32:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Scram Due to a Turbine Generator Load Rejection Signal 2024-02-24T08:19:00 | |
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